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Well ID: 34-153-22372 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: MOORE WELL SERVICES INC | |
Well Pad ID: | |
Farm/Lease Name: J M J DEVELOPMENT CO | |
License Status: Plugged and Abandoned | |
License Date: 2016-04-27 | |
Spud Date: 1987-07-23 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1987-07-27 | |
Well Total Depth: 4032.00 ft | |
Configuration: Vertical | |
Latitude: 41.300000 | |
Longitude: -81.450000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-06-11 | 140 KST OIL & GAS CO INC GeoDate 6/11/87 |
Oil and Gas | 1987-06-11 | Issued Date 6/11/87 Expired Date 6/10/88 Acres 0000000 Tool Type RTA Proposed Formation Proposed Depth 04032 Proposed Drill Depth 04032 |
Original Spud | 1987-07-23 | |
Completed | 1987-07-27 | |
Reached Total Depth | 1987-07-27 | |
Completion Report Received | 1987-09-15 | |
CO | 1995-12-05 | 182 BELDEN & BLAKE CO GeoDate 6/11/87 |
Change of Owner | 2001-06-20 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 5601, MOORE WELL SERVICES INC |
APP | 2016-04-27 | Proposed Formations:CLINTON, Issued Date:4/27/2016, Expired Date:4/27/2018 12:00:00 PM, Drilling unit acres:21, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-05-18 | |
Record Last Modified | 2017-02-15 | |
Construction Permit Expires | 2018-04-27 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3830 | 3892 | 0 |
3830 | 3892 | 0 | |
2006-09-11 | 3850 | 3892 | 102 |
3850 | 3892 | 102 | |
3830 | 3892 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 110000 Gal | 0 | FRAC W/110M GAL SLICKWATER |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | KST OIL & GAS CO INC | 10401.00 | 130.00 | 93 |
1988 | KST OIL & GAS CO INC | 27877.00 | 261.00 | 365 |
1989 | KST OIL & GAS CO INC | 17114.00 | 136.00 | 365 |
1990 | KST OIL & GAS CO INC | 11728.00 | 67.00 | 365 |
1991 | KST OIL & GAS CO INC | 10916.00 | 50.00 | 365 |
1992 | KST OIL & GAS CO INC | 9318.00 | 94.00 | 365 |
1993 | KST OIL & GAS CO INC | 7384.00 | 43.00 | 365 |
1994 | KST OIL & GAS CO INC | 4715.00 | 0.00 | 365 |
1995 | KST OIL & GAS CO INC | 3516.00 | 48.00 | 365 |
1996 | BELDEN & BLAKE CORPORATION | 4663.00 | 0.00 | 352 |
1997 | BELDEN & BLAKE CORPORATION | 3510.00 | 0.00 | 318 |
1998 | BELDEN & BLAKE CORPORATION | 2277.00 | 48.00 | 123 |
1999 | BELDEN & BLAKE CORPORATION | 1074.00 | 0.00 | 211 |
2000 | BELDEN & BLAKE CORPORATION | 917.00 | 0.00 | 345 |
2001 | BELDEN & BLAKE CORPORATION | 292.00 | 0.00 | 157 |
2002 | MOORE WELL SERVICES INC | 3992.00 | 61.00 | 322 |
2003 | MOORE WELL SERVICES INC | 3843.00 | 89.00 | 351 |
2004 | MOORE WELL SERVICES INC | 3088.00 | 41.00 | 365 |
2005 | MOORE WELL SERVICES INC | 2640.00 | 42.00 | 365 |
2006 | MOORE WELL SERVICES INC | 2916.00 | 36.00 | 357 |
2007 | MOORE WELL SERVICES INC | 2811.00 | 50.00 | 359 |
2008 | MOORE WELL SERVICES INC | 3068.00 | 16.00 | 365 |
2009 | MOORE WELL SERVICES INC | 2863.00 | 48.00 | 365 |
2010 | MOORE WELL SERVICES INC | 2869.00 | 37.00 | 365 |
2011 | MOORE WELL SERVICES INC | 3307.00 | 21.00 | 325 |
2012 | MOORE WELL SERVICES INC | 2847.00 | 21.00 | 366 |
2013 | MOORE WELL SERVICES INC | 3008.00 | 24.00 | 365 |
2014 | MOORE WELL SERVICES INC | 1959.00 | 24.00 | 365 |
2015 | MOORE WELL SERVICES INC | 2810.00 | 28.00 | 365 |
2016 | MOORE WELL SERVICES INC | 1693.00 | 43.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-296066717 | 2016-5-19 0:00: | PB | No Violations | |
0000PL4321 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0296066717 | 2016-05-19 | Plug / Plug Back | No Violations | I inspected that cement top level in the 8.625 casing and found it to be 50 below the wellhead. The cement top was solid and static. No violations. |
1463161384 | 2016-05-13 | Plug / Plug Back | No Violations | Since the P&A operations are scheduled to begin on 5/I6/2016, I inspected the wellhead area of the JMJ Devolment #1 to identify any surface gas which is associated with the shallow shale formatios in the area. I did not detect any gas surrounding the wellhead. I have asked for the dirt around the wellhead to be excavated so that the 8.625 surface casing is exposed. The well was produced by an electric pumping unit. The wellhead area was secured a chain link fence and the man door was locked. The required I.D. signage was posted on the fence. The tank battery consisted of one (1) 140 barrel oil tank, one (1) 50 barrel poly brine tank, one (1) vertical separator and gas measurement station. The tank battery was surrounded by an earthen dike and secured by a locked chain link fence. The gated lease road was graveled to tank battery. The required I.D. signage was posted on the tank batterys fence. There was a 2 line laying on top of the ground, previously used to deliver solvent to the well. I told Keith Moore that would have to be removed prior to final restoration approval. No violations identified during this inspection. |
1463492370 | 2016-05-17 | Plug / Plug Back | No Violations | Moore Well Service was removing the 2.375 tubing from the 4.5 production casing in preparation for plugging and abandonment. The placement of the cement plugs was rescheduled for 5/18/2016. No violations identified. |
PL4321 | PL | No Violations |
For data sources see[9]