If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-153-22823 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":41.09,"lon":-81.57,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: EVERFLOW EASTERN PARTNERS LP | |
Well Pad ID: | |
Farm/Lease Name: ST SEBASTIAN | |
License Status: Producing | |
License Date: 1995-08-04 | |
Spud Date: 1995-08-05 | |
Spud Drilling Contractor: J & J DIRECTIONAL SERVICE | |
Final Drill Date: 1995-08-17 | |
Well Total Depth: 4373.00 ft | |
Configuration: Directional | |
Latitude: 41.090000 | |
Longitude: -81.570000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1995-08-04 | 84 EVERFLOW EASTERN PTNS L P GeoDate 8/4/95 |
Oil and Gas | 1995-08-04 | Issued Date 8/4/95 Expired Date 8/3/96 Acres 0021720 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04373 Proposed Drill Depth 04373 |
Original Spud | 1995-08-05 | |
Completed | 1995-08-17 | |
Reached Total Depth | 1995-08-17 | |
Completion Report Received | 1995-09-27 | |
Construction Permit Expires | 1996-08-03 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4080 | 4185 | 0 |
4080 | 4185 | 0 | |
2006-09-11 | 4105 | 4186 | 75 |
4105 | 4186 | 75 | |
4080 | 4185 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 116245 Gal | 80000 | FRAC W/116,245 GAL H20 & 80M# SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0861493179 | 2004-11-02 | Production Wells | No Violations | Rich Strawn with Everflow reported that vandals had opened the valves on the stock tanks and drained approximately 110 bbl of crude into the containment dike. A police report was filed. A small percentage of the release seeped through the western dike wall and affected an area 10 feet by 15 feet. The initial response included spreading sorbent materials outside of the dike and using Moore Well Services vac truck inside of the dike. Recovered oil was placed back into a stock tank for later recovery. The St. Sebastian #3-D well shares a common tank battery with the #1, #2-D and the Christ Methodist #1-D wells. Future reports will on reference the #1 well. If remediation continues in a timely fashion, no NOV will be issued. All valves will be locked. |
861493179 | 2004-11-2 0:00: | PW | No Violations |
For data sources see[9]