If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-153-22969 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":41.02,"lon":-81.61,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: SCHREINER OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: L & L TRUCK SALES UNIT | |
License Status: Lost Hole | |
License Date: 2006-12-22 | |
Spud Date: 2006-08-30 | |
Spud Drilling Contractor: APPALACHIAN DRILLING | |
Final Drill Date: 2006-09-03 | |
Well Total Depth: 527.00 ft | |
Configuration: Vertical | |
Latitude: 41.020000 | |
Longitude: -81.610000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-01-06 | Proposed Formations:CLINTON, Issued Date:1/6/2006, Expired Date:1/6/2007 6:00:00 AM, Drilling unit acres:21.32, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2006-08-21 | Proposed Formations:CLINTON, Issued Date:8/21/2006, Expired Date:8/21/2007 6:00:00 AM, Drilling unit acres:21.32, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2006-09-03 | HOLE LOST DUE TO LACK OF SURFACE PIPE. SET@ 346' IN GLACIAL DRIFT AND MADE LOTS OF WATER WHEN OUT FROM SURFACE. WILL SKID ~200 FEET EAST AND RE-PERMIT PER BOB WORSTALL: 9-5- |
Reached Total Depth | 2006-09-03 | HOLE LOST DUE TO LACK OF SURFACE PIPE. SET@ 346' IN GLACIAL DRIFT AND MADE LOTS OF WATER WHEN OUT FROM SURFACE. WILL SKID ~200 FEET EAST AND RE-PERMIT PER BOB WORSTALL: 9-5- |
APP | 2006-12-22 | Proposed Formations:CLINTON, Issued Date:12/22/2006, Expired Date:12/22/2007 6:00:00 AM, Drilling unit acres:21.32, Proposed Well Type:OG, Proposed Well Class:POOL |
Construction Permit Expires | 2007-12-22 | HOLE LOST DUE TO LACK OF SURFACE PIPE. SET@ 346' IN GLACIAL DRIFT AND MADE LOTS OF WATER WHEN OUT FROM SURFACE. WILL SKID ~200 FEET EAST AND RE-PERMIT PER BOB WORSTALL: 9-5- |
Record Last Modified | 2014-07-10 | HOLE LOST DUE TO LACK OF SURFACE PIPE. SET@ 346' IN GLACIAL DRIFT AND MADE LOTS OF WATER WHEN OUT FROM SURFACE. WILL SKID ~200 FEET EAST AND RE-PERMIT PER BOB WORSTALL: 9-5- |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1243948210 | 2006-7-12 0:00: | DD | No Violations | |
0477992339 | 2006-12-19 | Plug / Plug Back | No Violations | Medina Supply was on site with 3 cubic yards of 9 sack grout to top off the surface plug on this well. The surface hole was originally plugged with the drilling rig on September 3. The grout filled the casing and stayed up. Attached is a copy of the Medina Supply ticket. |
1158065163 | 2006-09-05 | Drill / Deepen / Reopen | No Violations | Surface casing was set at 347 on August 31, 2006. On September 1, Appalachian went back to drilling and encountered more water, sand and gravel under surface casing. Attempts to dry up the hole and continue drilling were unsuccessful and the decision was made to squeeze cement below the casing on September 2. On September 3, Appalachian drilled through the squeeze and water continued to flow. At this time, Schreiner decided to plug and abandon the well and to skid the rig 200 feet to the east. The new location will require a new permit. The well was plugged on September 3. The plug job was not witnessed. Cement reportedly circulated to surface but when inspected on September 5, the plug had fallen approximately 150 feet. I spoke with Schreiner about topping off the plug cement. |
1161266263 | 2006-10-10 | Plug / Plug Back | No Violations | The top plug from this lost hole has fallen at least 150 and must be topped off. A ready-mix truck with nine sack grout will be acceptable to finish this job. Please schedule the truck as soon as possible and let me know the day and time. |
1243948210 | 2006-07-12 | Drill / Deepen / Reopen | No Violations | The drilling location has been built. The rig should arrive next week. |
477992339 | 2006-12-19 0:00 | PB | No Violations |
For data sources see[3]