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Well ID: 34-153-23137 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: DOMINION EAST OHIO | |
Well Pad ID: | |
Farm/Lease Name: GLICK | |
License Status: Storage Well | |
License Date: 2011-06-07 | |
Spud Date: 2011-12-03 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2011-12-17 | |
Well Total Depth: 4204.00 ft | |
Configuration: Vertical | |
Latitude: 40.940000 | |
Longitude: -81.530000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-06-07 | Proposed Formations:CLINTON, Issued Date:6/7/2011, Expired Date:6/6/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SO, Proposed Well Class:STOR |
Reached Total Depth | 2011-12-17 | |
Construction Permit Expires | 2012-06-06 | |
Completion Report Received | 2013-11-12 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2013-11-15 | 4039 | 4060 | 60 |
4039 | 4060 | 60 | |
4039 | 4060 | 60 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2012-01-25 | H2O | 15 | 57948 Gal | 62400 | Universal Well Services Inc. |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1061767981 | 2016-5-19 0:00: | PL | No Violations | |
-1097793910 | 2011-12-2 0:00: | UD | No Violations | |
-1098948624 | 2012-1-11 0:00: | UD | No Violations | |
-1297263145 | 2011-12-14 0:00 | UD | No Violations | |
-1379460900 | 2012-1-26 0:00: | SO | No Violations | |
-1532719012 | 2011-12-22 0:00 | UD | No Violations | |
-1893142174 | 2011-12-22 0:00 | PB | No Violations | |
-2009896275 | 2014-10-9 0:00: | SO | No Violations | 0.30 |
-388953942 | 2011-12-12 0:00 | UD | No Violations | |
-604271270 | 2016-5-19 0:00: | SO | No Violations | |
-708927146 | 2011-11-15 0:00 | UD | No Violations | |
-895850752 | 2015-7-30 0:00: | SO | No Violations | |
0199080689 | 2012-07-10 | Preliminary Restoration | No Violations | Preliminary Restoration is approved. |
0388953942 | 2011-12-12 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger Rig 17 is drilling ahead on fluid at 3800. The pits are fenced, lined and in good condition. |
0604271270 | 2016-05-19 | Storage Well | No Violations | I conducted a status check on this well. The well site is equipped with:
The lease access is stable and drivable. No violations found. |
0708927146 | 2011-11-15 | Urban Drill / Deepen / Reopen | No Violations | Dominion has a contractor on site to clear stumps before Daley Excavating starts grading the location. The lease road has been installed and the required identification is posted. |
0826620143 | 2018-06-15 | Storage Well | No Violations | I did a status check inspection for this storage well. The well is equipped with a master gate valve, two side gate valves and a meter run. The diked tank battery consists of a steel tank. The well is legibly identified. No compliance issues are cited at this time. |
0895850752 | 2015-07-30 | Storage Well | No Violations | I conducted a status check on this well. The well is equipped with a master gate valve and a side gate valve that were inspected by a third party company on 6/2015. There is a flow gate valve plumbed with a 3.00 line into a 100 BBL storage tank. All lids and hatches on the storage tank are closed and secure. There are two (2) tank drains on the storage tank and they are secured with valves and bull plugs in place. The tank battery is diked. The well is properly identified with a clear, legibly marked well identification sign mounted on the storage tank. There is a mechanical separator. The lease road is stable and drivable. No violations found. |
1061767981 | 2016-05-19 | Preliminary Restoration | No Violations | I conducted a preliminary restoration inspection on this well. The well is equipped with a master gate valve and a side gate valve. There is a flow gate valve plumbed with a 3.00 line into a 100 BBL storage tank. All lids and hatches on the storage tank are closed and secure. There are two (2) tank drains on the storage tank and they are secured with valves and bull plugs in place. The tank battery is diked. The well is properly identified with a clear, legibly marked well identification sign mounted on the storage tank. The lease access is stable. Preliminary restoration passed. |
1085596361 | 2011-01-09 | Storage Well | No Violations | Change in inspection type from Urban Drill to Storage well. Dominion personnel are on site to install the wellhead assembly. The pits are pumped down, fenced, lined and in good condition. Solidification is now scheduled for tomorrow morning. |
1097793910 | 2011-12-02 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger Drilling Rig 17 is starting to move on location and should spud late tonight. No violations at this time. |
1098948624 | 2012-01-11 | Urban Drill / Deepen / Reopen | No Violations | The drilling pits have been solidified and covered over. |
1240898917 | 2011-12-13 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger Rig 17 is hung in the hole at 3952. The plan is to back off the drill pipe/collars at the nearest free point and jar the remaining pipe out. |
1297263145 | 2011-12-14 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger and Baker Tool have successfully jarred the stuck collars and are recovering them at this time. They should be back to drilling later tonight or early tomorrow morning. |
1324655102 | 2011-12-15 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger Drilling Rig 17 is back to drilling on fluid at 4025. Anticipate reaching total depth tomorrow. The pits are fenced, lined and in good condition. The location and lease road have deteriorated due to activity and rainfall. Additional restoration work will be necessary when the time comes. |
1325007117 | 2011-12-21 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger is hung in the hole and has had no success jarring. The plan now is to backoff at 4032 leaving one collar, changeover sub and bit in the hole and plug back 300+. The hole will then be deviated 50 to the west. |
1325553260 | 2011-12-27 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger Rig 17 is going back to drilling and tagged the top of the kick plug at 3621. The hole will be deviated to the west approximately 50 and will bypass the lost hole, drill collar and bit. The drilling pits are fenced and lined. No violations at this time. |
1326731757 | 2012-01-06 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger Rig 17 has moved off location. The pits are fenced, lined and in good condition. The pits are scheduled to be solidified next week. |
1379460900 | 2012-01-26 | Storage Well | No Violations | The drilling pits have been solidified and covered over and the well has been fraced. Universal is on site to monitor flowback volumes and pressures. No violations at this time. |
1380893485 | 2012-01-12 | Urban Drill / Deepen / Reopen | No Violations | Daley Excavating requested and received permission to excavate and line a new pit to place and solidify drilling mud contained in a frac tank. |
1469981093 | 2017-07-26 | Storage Well | No Violations | At the time of this inspection, the well site is equipped with:
The lease access is stable and drivable. No violations were observed. |
1532719012 | 2011-12-22 | Urban Drill / Deepen / Reopen | No Violations | Kilbarger reached total depth on 12/17, mixed mud and started out of the hole. After pulling 2-1/2 stands, the pipe hung in the hole. At this point they could circulate but could not move uphole or downhole. All attempts to free the pipe, including unloading the hole and jarring were unsuccessful. During these attempts, circulation was lost and not recovered. Dominion ran a free point and Kilbarger backed the collars off leaving one collar, changeover sub and bit in the hole. Dominion ran a gyro and found the hole was straight. Kilbarger is preparing to run open ended drill pipe into the hole in order to set a kickoff plug. After the plug is set (later tonight), directional drillers will deviate around the equipment still in the hole and Kilbarger will again attempt to complete the well. |
1583950990 | 2020-3-11 0:00: | SO | No Violations | 0.50 |
1807143360 | 2011-11-10 | Urban Drill / Deepen / Reopen | No Violations | Dailey Excavating is building the lease road and location for this natrual gas storage well. Kilbarger Drilling Rig 17 will be moving on location after completing the Shreiner well. The required identification is posted at the entrance. |
1893142174 | 2011-12-22 | Plug / Plug Back | No Violations | Kilbarger Drilling reached TD at 4223 on December 17. After circulating for two hours, Kilbarger started out of the hole and became hung after pulling 2-1/2 stands (approximately 150). Kilbarger went back to bottom and circulated for another two hours and hung again at the same spot. This time, they could not move uphole or downhole. After jarring and working the pipe for two days, the rig broke down and the decision was made to plug back the well and deviate to the west. On December 21, Kilbarger backed off the bottom collar and prepared to spot a cement kickoff plug. On December 22, Universal spotted a 100 sack plug from 3987 to 3675. Universal broke and maintained circulation throughout the job. Plug down at 22:43 on December 22. Kilbarger tripped out of the hole to the bottom of surface casing and will shut down until December 27. |
199080689 | 2012-7-10 0:00: | PL | No Violations | |
2009896275 | 2014-10-09 | Storage Well | No Violations | I inspected Dominion East Ohio Gas storage well #1-S.The well is equipped with a master gate valve and a side gate valve. There was a sales line with a separator. There is a flow gate valve plumbed with a 3.00 line into a 100 BBL storage tank. All lids and hatches on the storage tank are closed and secure. There are two (2) pickup lines on the storage tank and they are secured with valves and bull plugs in place. The tank battery is diked. The well is properly identified with a clear, legibly marked well identification sign mounted on the storage tank. The storage equipment was surrounded by a locked, chain link fence with barb wire. The lease road is stoned and drivable. No violations found. |
46582985 | 2019-10-8 0:00: | SO | No Violations | 0.30 |
826620143 | 2018-6-15 0:00: | SO | No Violations | 0.50 |
For data sources see[5]