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| Well ID: 34-155-20754 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Trumbull | |
| Municipality: Bristol Township | |
| Operator Name: PETROX, INC | |
| Well Pad ID: | |
| Farm/Lease Name: HYDE WILLIAM & DORIS | |
| License Status: Final Restoration | |
| License Date: 1995-10-26 | |
| Spud Date: 1978-03-29 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1978-04-08 | |
| Well Total Depth: 4107.00 ft | |
| Configuration: Vertical | |
| Latitude: 41.400000 | |
| Longitude: -80.860000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1978-03-29 | |
| Completed | 1978-04-08 | |
| Reached Total Depth | 1978-04-08 | |
| CO | 1981-06-30 | 271 TGX CORP GeoDate 6/30/81 |
| CO | 1994-03-29 | 182 BELDEN & BLAKE CO GeoDate 6/30/81 |
| CO | 1995-10-11 | 1966 PETROX INC GeoDate 6/30/81 |
| CO | 1995-10-26 | 1966 PETROX INC GeoDate 10/26/95 |
| COMBINATION WELL | 1995-10-26 | Issued Date 10/26/95 Expired Date 10/25/96 Proposed Purpose OG Was Plug Supervised Y Who Superivsed KOHLPlug and Abandon Date 1/10/96 |
| Plugged/Abandoned | 1996-01-10 | |
| Construction Permit Expires | 1996-10-25 | |
| Record Last Modified | 2013-03-14 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 3927 | 4044 | 14 |
| 3927 | 4044 | 14 | |
| 3927 | 4044 | 14 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 1600 Bbl | 40000 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | TGX CORP | 376.00 | 47.00 | 0 |
| 1985 | TGX CORP | 265.00 | 79.00 | 245 |
| 1986 | TGX CORP | 261.00 | 47.00 | 117 |
| 1987 | TGX CORP | 62.00 | 0.00 | 45 |
| 1988 | TGX CORP | 107.00 | 78.00 | 65 |
| 1989 | TGX CORP | 67.00 | 48.00 | 243 |
| 1990 | TGX CORP | 16.00 | 0.00 | 153 |
| 1991 | TGX CORP | 9.00 | 44.00 | 123 |
| 1992 | TGX CORP | 2.00 | 0.00 | 365 |
| 1993 | TGX CORP | 0.00 | 0.00 | 0 |
| 1995 | BELDEN & BLAKE CORPORATION | 13.00 | 0.00 | 366 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | TGX CORP | Brine | 20 | 0 |
| 1985 | TGX CORP | Brine | 38 | 245 |
| 1986 | TGX CORP | Brine | 23 | 117 |
| 1987 | TGX CORP | Brine | 0 | 45 |
| 1988 | TGX CORP | Brine | 0 | 65 |
| 1989 | TGX CORP | Brine | 0 | 243 |
| 1990 | TGX CORP | Brine | 0 | 153 |
| 1991 | TGX CORP | Brine | 0 | 123 |
| 1992 | TGX CORP | Brine | 0 | 365 |
| 1993 | TGX CORP | Brine | 0 | 0 |
| 1995 | BELDEN & BLAKE CORPORATION | Brine | 4 | 366 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -263039160 | 2012-12-17 0:00 | FR | No Violations | 0.50 |
| 0263039160 | 2012-12-17 | Final Restoration | No Violations | I completed a final restoration inspection request by the landowner Mary King. My inspection found no producing well on the property. I researched our database and found the plugging permit, plugging report, and final restoration. The well was plugged by Leonard Wenger using PetroSet for Petrox, Inc. on 1/9/1996. The final restoration was completed by ODNR Inspector Jerry Kohl on 11/19/1998. |
| iDIAN00079 | 1998-11-19 | Final Restoration | No Violations | |
| iDIAN000794 | 1998-11-19 0:00 | FR | No Violations |
For data sources see[9]