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Well ID: 34-155-21042 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Braceville Township | |
Operator Name: ATWOOD ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: MCGARRY | |
License Status: Orphan Well - Ready | |
License Date: 1987-10-28 | |
Spud Date: 1978-10-25 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1978-10-30 | |
Well Total Depth: 4546.00 ft | |
Configuration: Vertical | |
Latitude: 41.210000 | |
Longitude: -80.930000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Completion Report Received | 1978-02-08 | WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.
Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017 |
CO | 1978-10-03 | 277 ATWOOD ENERGY INC GeoDate 10/3/78 |
Original Spud | 1978-10-25 | WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.
Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017 |
Completed | 1978-10-30 | WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.
Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017 |
Reached Total Depth | 1978-10-30 | WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.
Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017 |
CO | 1987-10-28 | 277 ATWOOD ENERGY INC GeoDate 10/28/87 |
Unknown | 1987-10-28 | Issued Date 10/28/87 Expired Date 10/27/88 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1988-10-27 | WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.
Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017 |
Record Last Modified | 2017-02-21 | WELL REPORTED TO BE LEAKING BY AREA REALTOR. CHANGE STATUS TO NF PER INSPECTIONS ON FILE 3/31/16 ALE.
Per Richard Skmore Well was located on 12/22/2016 and Inspection report completed. Change Well Status from NF to PR.. Mkb 2/21/2017 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2002-11-25 | 4376 | 4440 | 18 |
4376 | 4440 | 18 | |
4376 | 4440 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 79000 Gal | 60000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ATWOOD ENERGY INC | 2097.00 | 95.00 | 0 |
1985 | ATWOOD ENERGY INC | 1891.00 | 0.00 | 0 |
1986 | ATWOOD ENERGY INC | 1387.00 | 87.00 | 365 |
1987 | ATWOOD ENERGY INC | 702.00 | 77.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ATWOOD ENERGY INC | Brine | 0 | 0 |
1985 | ATWOOD ENERGY INC | Brine | 60 | 0 |
1986 | ATWOOD ENERGY INC | Brine | 140 | 365 |
1987 | ATWOOD ENERGY INC | Brine | 70 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0951791127 | 2017-01-17 | Administrative Inspection | No Violations | I received a call from Terry Alberini (330-717-0113) from Tara Development in response to the letter I mailed concerning the well on their property. Mr. Alberini stated
Tara Development does own the property (Parcel 54-091401) where the tank battery and well are located. Mr. Alberini is unaware if the well is supplying domestic gas. Tara Development may be interested in taking ownership of the well and plans to contact Jim Adams from J Well to inspect the condition of the well and tank battery. I informed Mr. Alberini that the well is currently leaking gas. Further investigations will be conducted. |
1147369567 | 2016-12-22 | Production Wells | No Violations | |
1337605912 | 2012-05-18 | Production Wells | No Violations | On 5/18/2012, I conducted a production well inspection status check. I was unable to locate the lease road, tank battery, or well head. My review of the well file revealed one previous inspection on 10/24/2000 that stated: no well, tanks, or lease road was found and listed the well as a NOV under statute 1509.14 as a report of abandonment. However, the inspection report was followed by a complaint form dated 11/27/2002 revealing the well was owned by the landower for domestic use. |
1484841053 | 2017-01-19 | Production Wells | No Violations | |
1565268209 | 2019-8-8 0:00:0 | OR | No Violations | |
951791127 | 2017-1-17 0:00: | AM | No Violations | 0.20 |
For data sources see[9]