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Well ID: 34-155-21389 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Brookfield Township | |
Operator Name: D & L ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: HUBISH A | |
License Status: Final Restoration | |
License Date: 2013-05-10 | |
Spud Date: 1981-05-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-06-03 | |
Well Total Depth: 5134.00 ft | |
Configuration: Vertical | |
Latitude: 41.260000 | |
Longitude: -80.580000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-03-06 | 182 BELDEN & BLAKE CO GeoDate 3/6/81 |
Original Spud | 1981-05-26 | R.I. 3-12-81, R.I. 6-11-80 |
Completed | 1981-06-03 | R.I. 3-12-81, R.I. 6-11-80 |
Reached Total Depth | 1981-06-03 | R.I. 3-12-81, R.I. 6-11-80 |
CO | 1996-03-15 | 2651 D & L ENERGY INC GeoDate 3/6/81 |
APP | 2013-05-10 | Proposed Formations:CLINTON, Issued Date:5/10/2013, Expired Date:5/10/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-12-03 | R.I. 3-12-81, R.I. 6-11-80 |
Construction Permit Expires | 2016-11-15 | R.I. 3-12-81, R.I. 6-11-80 |
Record Last Modified | 2017-02-10 | R.I. 3-12-81, R.I. 6-11-80 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4884 | 4888 | 2 |
2006-09-11 | 4870 | 4880 | 5 |
4870 | 4880 | 5 | |
4870 | 4880 | 5 | |
2006-09-11 | 4892 | 4896 | 2 |
2006-09-11 | 4914 | 4924 | 5 |
2006-09-11 | 4898 | 4900 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1020 Bbl | 90000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | POWER GAS MARKETING & TRANS | 4701.00 | 66.00 | 0 |
1985 | BELDEN & BLAKE CORPORATION | 2541.00 | 49.00 | 0 |
1987 | BELDEN & BLAKE CORPORATION | 2753.00 | 57.00 | 365 |
1988 | BELDEN & BLAKE CORPORATION | 1884.00 | 32.00 | 151 |
1990 | BELDEN & BLAKE CORPORATION | 2590.00 | 62.00 | 349 |
1991 | BKK PROSPECTING LTD | 1991.00 | 0.00 | 365 |
1992 | BELDEN & BLAKE CORPORATION | 1483.00 | 29.00 | 237 |
1993 | BELDEN & BLAKE CORPORATION | 1530.00 | 0.00 | 349 |
1994 | BELDEN & BLAKE CORPORATION | 1446.00 | 0.00 | 347 |
1995 | BELDEN & BLAKE CORPORATION | 761.00 | 56.00 | 125 |
2011 | D & L ENERGY INC | 0.00 | 0.00 | 0 |
2012 | D & L ENERGY INC | 0.00 | 0.00 | 365 |
2013 | D & L ENERGY INC | 0.00 | 0.00 | 0 |
2014 | D & L ENERGY INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | POWER GAS MARKETING & TRANS | Brine | 0 | 0 |
1985 | BELDEN & BLAKE CORPORATION | Brine | 12 | 0 |
1987 | BELDEN & BLAKE CORPORATION | Brine | 13 | 365 |
1988 | BELDEN & BLAKE CORPORATION | Brine | 9 | 151 |
1990 | BELDEN & BLAKE CORPORATION | Brine | 28 | 349 |
1991 | BKK PROSPECTING LTD | Brine | 0 | 365 |
1992 | BELDEN & BLAKE CORPORATION | Brine | 18 | 237 |
1993 | BELDEN & BLAKE CORPORATION | Brine | 0 | 349 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 0 | 347 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 21 | 125 |
2011 | D & L ENERGY INC | Brine | 0 | |
2012 | D & L ENERGY INC | Brine | 0 | 365 |
2013 | D & L ENERGY INC | Brine | 0 | 0 |
2014 | D & L ENERGY INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1144355002 | 2014-5-28 0:00: | AM | No Violations | |
-1340095755 | 2015-12-7 0:00: | PB | No Violations | 1.00 |
-1636206385 | 2015-11-30 0:00 | PB | No Violations | 3.00 |
-1822945348 | 2015-12-2 0:00: | PB | No Violations | 2.50 |
-2128372012 | 2015-3-10 0:00: | UP | No Violations | 0.70 |
-717119826 | 2013-5-21 0:00: | AM | No Violations | 0.20 |
-931205925 | 2016-6-23 0:00: | FR | No Violations | 0.70 |
0105129607 | 2015-12-01 | Plug / Plug Back | No Violations | I was on location to witness J Well plug the well for D & L Energy. Appalachian Well Survey was arrived on location. The 1.5 tubing was shot-off at 3,622. Next, J Well pulled all of the tubing from the well. The well was shut-in for the night. |
0225748074 | 2010-12-30 | Production Wells | No Violations | FOLLOW UP TO NOV # 2123963566 Complaint ,Jim Hubish , [landowner] . Inspection of well showed 4.5 production casing with swedge to 1 domestic line , there is a .25 hole in swedge open to atmosphere . There is no tank battery facility for well . Wel |
0717119826 | 2013-05-21 | Administrative Inspection | No Violations | A plugging permit was filed and issued on 5/10/2013 per my request from an inspection on 1/29/2013. |
0931205925 | 2016-06-23 | Final Restoration | No Violations | At the time of my inspection, Mr. Hubish has ploughed the well location and planted crops. There was no production equipment associated with the well. There was no access road to the well. No pits were used during the plugging of the well. A Form 5 has been signed and submitted to waive the removal of the sales and flow lines. Final restoration passed. |
105129607 | 2015-12-1 0:00: | PB | No Violations | 3.00 |
1144355002 | 2014-05-28 | Administrative Inspection | No Violations | I conducted an administrative inspection in reference to compliance notice #2123963566. I spoke with Dave Rice of D & L Energy, who stated D & L was taking bids from a few plugging companies. At this time, there was no time table to actually plug the well. I will continue follow-up inspection. |
1340095755 | 2015-12-07 | Plug / Plug Back | No Violations | I was on location for a status check. During my inspection, I found the wellhead cut-off 30 below grade. The cement was static at surface. J Well was rigging down to move off location. There are no violations at this time. |
1359569791 | 2013-01-29 | UrbanProduction Wells | No Violations | I investigated an urban production well as a compliant request from attorney Molly Phillips for landowner, Jim Hubish. My inspection found a shut-in wellhead surrounded by thorns and weeds. There was no production equipment for the well. I researched our database and found ODNR Inspector Jerry Kohl issued a compliance notice for the well to be plugged on 12/30/2010. I found no application for a plugging permit in our database. D & L Energy reported zero production for 2011. The previous reported production was by Belden & Blake Corporation in 1995. I called Dave Rice of D & L Energy at 330-565-0430. I informed him about the order to plug the well issued by Jerry. I instructed him to file for a plugging permit by 3/1/2013. If a permit is not filed by this allotted time, a Chiefs Order will be issued. Since there has been no production since 1995 and there is no production equipment; this well should not be granted Temporary Inactive Status. |
1608135712 | 2010-12-30 | Production Wells | No Violations | FOLLOW UP TO NOV # 2123963566 Complainant ,Jim Hubish , [landowner] . Inspection of well showed 4.5 production casing with swedge to 1 domestic line. There is a .25 hole in swedge open to atmosphere. There is no tank battery facility for well. Well is idle at this time. I contacted company and spoke with Dave Rice. He advised me they plan to plug well when weather permits so they wont disturb the crop field. |
1636206385 | 2015-11-30 | Plug / Plug Back | No Violations | I was on location to witness J Well plug the well for D & L Energy. The cement contractor was on location. Petroset rigged up to the 4.5 casing and pressured up to 1,550 psi. Pressure held static for 15 minutes. Next, Petroset rigged up to the 1.5 tubing and pumped 18 barrels of fresh water. Thirteen barrels of water was needed to clear the tubing. Plug #1 was set from 4,870 to 4,600. Next, Petroset pumped an additional two barrels of fresh water, then mixed and bull headed 30 sacks of Class A cement with a yield of 1.36. The cement was displaced to 4,600 with 12 barrels of water. Petroset held pressure static on displaced cement for 10 minutes. Next, Petroset release pressure with zero barrels flowed back. J Well shut-in the well for the night. Appalachian Well Survey will be on location at 8 am tomorrow, December 1, 2015 to shoot off the tubing. |
1822945348 | 2015-12-02 | Plug / Plug Back | No Violations | I was on location to witness J Well plug the well for D & L Energy. J Well rigged up and pulled stretch on the 4.5 casing. Next, the rig operator ripped the casing at 3,472. One joint was pulled to set the Big Lime plug. Petroset is schedule for tomorrow, December 3, 2015. The well was shut-in for the night. |
2123963566 | 2010-12-30 | Production Wells | Violations Noted | Complaint ,Jim Hubish , [landowner] . Inspection of well showed 4.5 production casing with swedge to 1 domestic line , there is a .25 hole in swedge open to atmosphere . There is no tank battery facility for well . Well is idle at this time . I contacted company and spoke with Dave Rice , he advised me they plan to plug well when weather permits so they wont disturb the crop field. |
2128372012 | 2015-03-10 | UrbanProduction Wells | Violations Noted | I was on location for a status check. During my inspection, I found the well not in production. The wells 2 inch tubing reduced to 1 inch black iron flow line. The well is engulfed by weeds. There is no production equipment associated with the well. There is no identification posted. I spoke with Mr. Hubish on location. Mr. Hubish stated the well is not in operation. There is no lease road associated with the well. The proper identification sign will be posted by 6/1/2015. D & L has filed annual production from 2011 through 2013. Well shall be plugged by 9/10/2015. Photos were taken and are available upon request. |
225748074 | 2010-12-30 0:00 | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
2123963566 | US-OH-121670 | 2011-03-28 | Well shall be plugged | |
2128372012 | US-OH-121803 | 2016-01-05 | ID (a-i) |
For data sources see[9]