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Well ID: 34-155-21579 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Vienna Township | |
Operator Name: KLEESE DEVELOPMENT ASSOCIATES | |
Well Pad ID: | |
Farm/Lease Name: SOROKA | |
License Status: Plugged and Abandoned | |
License Date: 2019-09-17 | |
Spud Date: 1980-10-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-11-01 | |
Well Total Depth: 5179.00 ft | |
Configuration: Vertical | |
Latitude: 41.230000 | |
Longitude: -80.630000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-09-16 | 2125 EASTERN PETROLEUM CO GeoDate 9/16/80 |
Oil and Gas | 1980-09-16 | Issued Date 9/16/80 Expired Date Acres 0040000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1980-10-21 | |
Completed | 1980-11-01 | |
Reached Total Depth | 1980-11-01 | |
CO | 1996-10-03 | 213 LOMAK OPERATING CO GeoDate 9/16/80 |
Change of Owner | 2000-06-28 | Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2000-08-24 | Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 6805, GAS ACQUISITION COMPANY LTD |
Change of Owner | 2001-08-23 | Operator changed from 6805, GAS ACQUISITION COMPANY LTD to 6857, ANNAROCK PETROLEUM LLC |
Change of Owner | 2013-03-29 | Operator changed from 6857, ANNAROCK PETROLEUM LLC to 2655, KLEESE DEVELOPMENT ASSOCS |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4942 | 5010 | 18 |
4942 | 5010 | 18 | |
4942 | 5010 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1920 Bbl | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | GASEARCH INC | 6600.00 | 123.00 | 365 |
1985 | GASEARCH INC | 9859.00 | 125.00 | 365 |
1986 | EASTERN PETROLEUM CO | 6847.00 | 58.00 | 365 |
1987 | EASTERN PETROLEUM CO | 6143.00 | 90.00 | 365 |
1988 | EASTERN PETROLEUM CO | 5269.00 | 82.00 | 365 |
1989 | EASTERN PETROLEUM CO | 3511.00 | 50.00 | 365 |
1990 | EASTERN PETROLEUM CO | 3481.00 | 59.00 | 365 |
1992 | EASTERN PETROLEUM CO | 2395.00 | 58.00 | 365 |
1993 | EASTERN PETROLEUM CO | 2878.00 | 44.00 | 365 |
1994 | EASTERN PETROLEUM CO | 3227.00 | 44.00 | 365 |
1996 | RANGE OPERATING COMPANY | 3078.00 | 0.00 | 334 |
1997 | RANGE OPERATING COMPANY | 2972.00 | 0.00 | 305 |
1998 | RANGE OPERATING COMPANY | 3154.00 | 24.00 | 365 |
1999 | RANGE OPERATING COMPANY | 3557.00 | 0.00 | 273 |
2000 | ANNAROCK PETROLEUM LLC | 1098.00 | 18.00 | 53 |
2001 | ANNAROCK PETROLEUM LLC | 5150.00 | 0.00 | 365 |
2002 | ANNAROCK PETROLEUM LLC | 4069.00 | 0.00 | 365 |
2003 | ANNAROCK PETROLEUM LLC | 3686.00 | 45.00 | 365 |
2004 | ANNAROCK PETROLEUM LLC | 2753.00 | 41.00 | 365 |
2005 | ANNAROCK PETROLEUM LLC | 3065.00 | 27.00 | 365 |
2006 | ANNAROCK PETROLEUM LLC | 2385.00 | 0.00 | 365 |
2007 | ANNAROCK PETROLEUM LLC | 1899.00 | 0.00 | 365 |
2008 | ANNAROCK PETROLEUM LLC | 2253.00 | 0.00 | 365 |
2009 | ANNAROCK PETROLEUM LLC | 2096.00 | 0.00 | 365 |
2010 | ANNAROCK PETROLEUM LLC | 2044.00 | 21.00 | 365 |
2011 | ANNAROCK PETROLEUM LLC | 1872.00 | 30.00 | 365 |
2012 | ANNAROCK PETROLEUM LLC | 1101.00 | 66.00 | 366 |
2013 | ANNAROCK PETROLEUM LLC | 0.00 | 0.00 | 365 |
2015 | KLEESE DEVELOPMENT ASSOCIATES | 0.00 | 0.00 | 0 |
2016 | KLEESE DEVELOPMENT ASSOCIATES | 0.00 | 0.00 | 0 |
2017 | KLEESE DEVELOPMENT ASSOCIATES | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1044804050 | 2014-1-16 0:00: | PW | No Violations | 0.50 |
-2088803732 | 2019-12-3 0:00: | PB | No Violations | 8.00 |
1044804050 | 2014-01-16 | Production Wells | No Violations | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery consisted of a 50 barrel production tank, a concrete brine tank, and separator. There was a plug on the load line. The dike met containment requirements. An identification sign was posted at the separator with the previous owners information. The lease road was in good condition. I called Kleese and told them to post a new identification sign with the correct information. |
1553091375 | 2019-03-20 | Production Wells | Violations Noted | I conducted an inspection on this well. The well was equipped with a plunger lift assembly and not in production, at the time of this inspection. The gate valve on the tubing and the valve on the 2 inch flow line were both closed. There was a domestic line with a regulator plumbed off the 4.5 inch casing with an open valve. I spoke with landowner, Mr. Steve Soroka, who stated that he does not receive gas for domestic use and has not had domestic gas since 2013. Under Kleese Development Associates ownership, production records from 2015-2017 have been submitted as zero. Production records for 2018 were not available, at the time of this inspection. The diked tank battery was comprised of one 50 BBL tank. There was a mechanical separator outside of the diked tank battery with an open valve on the inlet side but a closed valve on the outlet side. The chart present on the separator was a large blot of ink and did not show any current production. No leaks were observed from the well or separator fittings at the tank battery. The identification sign was present on the well and had outdated owner/operator information and did not contain the well information. The lease access was stable. I attempted to contact Kleese Development Associates at the phone number on the posted identification on site. The phone number was a non working number. I contacted Kleese Development Associates at the phone number listed on the state database. The number was up to date and I left a meassage requesting a call back regarding the compliance issues addressed in this report. The well owner shall submit a written plugging schedule to Inspector Shannon Mullins at ODNR Division of Oil and Gas Resources Management, 3575 Forest Lake Drive, Suite 150, Uniontown, OH 44685 within 30 days. The well owner/operator will be notified if the plugging schedule is approved or denied. The Soroka #1 shall be plugged within 180 days. In the interim, the owner must correct the identification sign |
1574883397 | 2019-11-27 0:00 | PB | No Violations | |
1576772087 | 2019-11-26 0:00 | PB | No Violations | 4.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1553091375 | US-OH-115092 | 2019-03-21 | 9-9-05(A)10 | Failure to legibly identify well |
1553091375 | US-OH-115093 | 2019-03-21 | NONE | Well shall be plugged |
For data sources see[9]