If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-155-21671 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":41.24,"lon":-80.54,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Brookfield Township | |
Operator Name: VORTEX ENERGY LLC | |
Well Pad ID: | |
Farm/Lease Name: VARGA J | |
License Status: Producing | |
License Date: 1982-04-20 | |
Spud Date: 1982-05-30 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1982-06-04 | |
Well Total Depth: 5043.00 ft | |
Configuration: Vertical | |
Latitude: 41.240000 | |
Longitude: -80.540000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-04-20 | Issued Date 4/21/82 Expired Date 10/18/82 Acres 0049500 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05043 Proposed Drill Depth 05043 |
Original Spud | 1982-05-30 | |
Completed | 1982-06-04 | |
Reached Total Depth | 1982-06-04 | |
Completion Report Received | 1982-07-04 | |
Construction Permit Expires | 1982-10-18 | |
CO | 1982-12-03 | 54 TITAN ENERGY CORP GeoDate 4/20/82 |
Change of Owner | 1998-01-26 | Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET |
Change of Owner | 2017-06-22 | Operator changed from 1333, BIG SKY ENERGY INC to 9841, VORTEX ENERGY LLC |
Record Last Modified | 2017-06-22 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4841 | 4880 | 27 |
4841 | 4880 | 27 | |
4841 | 4880 | 27 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 126800 Gal | 70000 | FRAC: 127MG H2O, 70M SAND,230M N2,ACID | ||
N2 | 0 | 230 Mscf | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TITAN ENERGY CORP | 7119.00 | 226.00 | 0 |
1985 | TITAN ENERGY CORP | 5675.00 | 122.00 | 365 |
1986 | TITAN ENERGY CORP | 4368.00 | 144.00 | 365 |
1987 | TITAN ENERGY CORP | 3379.00 | 74.00 | 365 |
1988 | TITAN ENERGY CORP | 5128.00 | 142.00 | 365 |
1989 | TITAN ENERGY CORP | 3602.00 | 67.00 | 365 |
1990 | TITAN ENERGY CORP | 3761.00 | 68.00 | 365 |
1991 | TITAN ENERGY CORP | 1549.00 | 0.00 | 365 |
1992 | TITAN ENERGY CORP | 2935.00 | 70.00 | 365 |
1993 | TITAN ENERGY CORP | 1692.00 | 0.00 | 365 |
1994 | TITAN ENERGY CORP | 0.00 | 0.00 | 365 |
1997 | TITAN ENERGY CORP | 0.00 | 14.00 | 245 |
2000 | BIG SKY ENERGY INC | 4294.00 | 59.00 | 365 |
2001 | BIG SKY ENERGY INC | 3716.00 | 40.00 | 365 |
2002 | BIG SKY ENERGY INC | 3644.00 | 102.00 | 365 |
2003 | BIG SKY ENERGY INC | 3275.00 | 0.00 | 365 |
2004 | BIG SKY ENERGY INC | 2402.00 | 0.00 | 365 |
2005 | BIG SKY ENERGY INC | 2081.00 | 34.00 | 365 |
2006 | BIG SKY ENERGY INC | 2923.00 | 0.00 | 365 |
2007 | BIG SKY ENERGY INC | 1853.00 | 0.00 | 365 |
2008 | BIG SKY ENERGY INC | 2453.00 | 0.00 | 365 |
2009 | BIG SKY ENERGY INC | 2040.00 | 0.00 | 365 |
2010 | BIG SKY ENERGY INC | 1744.00 | 0.00 | 365 |
2011 | BIG SKY ENERGY INC | 1304.00 | 0.00 | 365 |
2012 | BIG SKY ENERGY INC | 450.00 | 55.00 | 366 |
2013 | BIG SKY ENERGY INC | 494.00 | 0.00 | 365 |
2014 | BIG SKY ENERGY INC | 407.00 | 24.00 | 365 |
2016 | BIG SKY ENERGY INC | 94.00 | 0.00 | 98 |
2017 | BIG SKY ENERGY INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TITAN ENERGY CORP | Brine | 0 | 0 |
1985 | TITAN ENERGY CORP | Brine | 0 | 365 |
1986 | TITAN ENERGY CORP | Brine | 0 | 365 |
1987 | TITAN ENERGY CORP | Brine | 0 | 365 |
1988 | TITAN ENERGY CORP | Brine | 0 | 365 |
1989 | TITAN ENERGY CORP | Brine | 0 | 365 |
1990 | TITAN ENERGY CORP | Brine | 0 | 365 |
1991 | TITAN ENERGY CORP | Brine | 0 | 365 |
1992 | TITAN ENERGY CORP | Brine | 0 | 365 |
1993 | TITAN ENERGY CORP | Brine | 0 | 365 |
1994 | TITAN ENERGY CORP | Brine | 0 | 365 |
1997 | TITAN ENERGY CORP | Brine | 245 | |
2000 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2001 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2002 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2003 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2004 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2005 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2006 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2007 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2008 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2009 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2010 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2011 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2012 | BIG SKY ENERGY INC | Brine | 0 | 366 |
2013 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2014 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2016 | BIG SKY ENERGY INC | Brine | 0 | 98 |
2017 | BIG SKY ENERGY INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1215781175 | 2016-4-7 0:00:0 | UP | No Violations | 0.50 |
-496994901 | 2019-3-12 0:00: | UP | No Violations | 0.40 |
0000PL4091 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0496994901 | 2019-03-12 | UrbanProduction Wells | No Violations | I conducted a compliance notice follow-up inspection for compliance notice 1462017995, regarding the cleanup of the oil impacted soil at the base of the 100 BBL tank and the residual oil along the side of the tank, the rebuilding of dike around the tank battery and repairing the leaking 2 inch flow line at the well. Identification also needed to be installed at the tank battery with updated owner and well information. At the time of my inspection, the well was in production and equipped with a plunger lift assembly. The gate valve on the tubing and the 2 inch flow line valve were open. There was oil along the 2 inch flow line below the elbow connection, prior to where the flow line was buried. The residual oil along the south side of the 100 BBL tank was still present and had not been cleaned off of the tank. The area of impact at the base of the tank was stained dark but no fresh oil was present or active leak observed, at the time of this inspection. The 100 BBL tank needs cleaned of the residual oil and the soil at the base of the tank needs removed and properly disposed of. The dike around the tank battery needs rebuilt. The identification still needs updated with current owner information. I contacted Vortex Energy, LLC and spoke with field superintendent, Greg Henderson regarding the cleanup of the oil on the tank and removal of the impacted soil at the base of the tank. I also discussed the reinstallation of the dike and updated identification. |
1215781175 | 2016-04-07 | UrbanProduction Wells | No Violations | I was on location in reference to compliance to Chiefs Order 2016-105. At the time of my inspection, I found the 2 flow line valve entering the separator in the open position. The 2 sales line valve coming off of the separator is in the open position. The two 2 flow line valves at the well are in the open position. There are no additional changes from my previous inspection on 21 March 2016. Photos were taken and available upon request. |
1459771707 | 2016-03-21 | UrbanProduction Wells | No Violations
| |
1462017995 | 2016-04-28 | Production Wells | Violations Noted | My inspection found the well to be equipped with a plunger lift unit. The valve leading from the wellhead to the flow line is closed. There is a domestic supply plumbed into the 4.5 casing. The tank battery consists of a 100 BBL production tank and a 50 BBL brine tank. The tank was overfilled at one point and the South side of the tank has oil down the side of it. There is a 3 ft by 5 ft oil saturated stone and soil at the base of the tank. The production tank needs wiped down, the oil saturated soil at the base of the tank needs removed and properly disposed of, and the dike around the tank battery needs rebuilt. The heated separator is outside of the tank battery with the proper spacing. The production chart was last changed on 2/29/16. The well was not in production at the time of the inspection. The identification sign is on the tank battery and needs to be updated. The lease road is in stable condition. |
99825231 | 2020-4-27 0:00: | UP | No Violations | |
PL4091 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1462017995 | US-OH-113374 | 2016-06-14 | Well operation causing pollution and contamination |
For data sources see[9]