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Well ID: 34-155-21982 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Gustavus Township | |
Operator Name: ENERGY EXPLORATION & DEVELOPME | |
Well Pad ID: | |
Farm/Lease Name: MELONI S | |
License Status: Final Restoration | |
License Date: 2015-04-10 | |
Spud Date: 1981-10-05 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-10-13 | |
Well Total Depth: 4447.00 ft | |
Configuration: Vertical | |
Latitude: 41.430000 | |
Longitude: -80.700000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-09-14 | 224 ATLAS ENERGY GROUP INC GeoDate 9/14/81 |
Original Spud | 1981-10-05 | |
Completed | 1981-10-13 | |
Reached Total Depth | 1981-10-13 | |
Change of Owner | 2001-02-16 | Operator changed from 224, ATLAS ENERGY GROUP INC to 1919, EXPLORATION ENERGY INC |
Change of Owner | 2001-03-30 | Operator changed from 1919, EXPLORATION ENERGY INC to 6929, ENERGY EXPLORATION & DEVELOP. |
APP | 2015-04-10 | Proposed Formations:CLINTON, Issued Date:4/10/2015, Expired Date:4/9/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-11-12 | |
Construction Permit Expires | 2017-04-09 | |
Record Last Modified | 2017-12-27 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4286 | 4349 | 1 |
4286 | 4349 | 1 | |
4286 | 4349 | 1 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2002 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2003 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2004 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2005 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2006 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2007 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2008 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2009 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2010 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2011 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
2012 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 366 |
2014 | ENERGY EXPLORATION & DEVELOPME | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2002 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2003 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2004 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2005 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2006 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2007 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2008 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2009 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2010 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2011 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
2012 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 366 |
2014 | ENERGY EXPLORATION & DEVELOPME | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1208090598 | 2017-9-19 0:00: | FR | No Violations | 0.20 |
-2137686555 | 2014-4-22 0:00: | PW | No Violations | 0.50 |
-632468961 | 2014-5-16 0:00: | AM | No Violations | 0.50 |
0123237229 | 2014-04-14 | Administrative Inspection | No Violations | I performed an administrative inspection in reference to Compliance #189438888. My inspection of our database found Energy Exploration has failed to file for a plugging permit. I called the office of Energy Exploration and left a message. I instructed Energy Exploration to immediately file for a plugging permit. |
0189438888 | 2013-10-21 | Production Wells | Violations Noted | My inspection found the well not in production. The well had a closed ball valve and capped at the 4.5 casing with a 4 white PVC pipe marking the location in the field. I notice no production equipment associated with the well. Energy Exploration has filed zero annual production since 2001. I called John Ross at 330-637-4955 and left a message. I told John a compliance notice would be issue to plug or produce the well by 4/4/2014. |
0556427746 | 2015-06-29 | Production Wells | No Violations | I was on location for a follow-up inspection in reference to Chiefs Order 2015-140 and Compliance Notice No. 189438888. During my inspection, I found the well has not been plugged. The well is surrounded by soy beans. According to our RBDMS database, Energy Exploration has obtained a plugging permit dated 4/10/2015. I called and spoke with Energy Exploration about plugging the well. Energy Exploration stated J Well Service Inc. has been contracted to plug the wells. Next, I called and spoke with Jim Adams, owner of J Well Service Inc. Mr. Adams stated Energy Exploration gave him the approval to plug the well on 6/15/2015. I asked Mr. Adams to meet with me and the landowner, Michael Roscoe, to discuss plugging the well. Mr. Roscoe requested that Mr. Adams wait until late September to early October after the soy beans have been removed. Also, Mr. Roscoe stated plugging the well at this time with the current weather conditions could potentially damage crops. I told Mr. Roscoe and Mr. Adams the well shall be plugged immediately upon removal of the crops. |
0632468961 | 2014-05-16 | Administrative Inspection | No Violations | I performed a follow-up administrative inspection in reference to compliance notice #189438888. On 5/2/2014, I spoke with John Ross concerning the well. I instructed John to file for a plugging permit immediately. On 5/16/2014, I emailed Patty Nicklaus of ODNR concerning Energy Exploration filing for a plugging permit. Patty stated in the email that Energy Exploration had not filed for a plugging permit. I filed a copy of the email. |
1009034476 | 2015-10-05 | Production Wells | No Violations | I was on location for a follow-up inspection in reference to Chiefs Order 2015-140 and Compliance Notice No. 189438888. During my inspection, I found the crops have been removed for the season. I called and spoke with Jim Adams, plugging contractor for Energy Exploration. I informed Mr. Adams that the crops have been removed. |
1208090598 | 2017-09-19 | Final Restoration | No Violations | I was on location for a final restoration inspection. I found the well site graded. Agricultural crops and vegetation are well established. Pits were not used during the plugging operations. There were no production equipment and underground pipelines associated with the well. The access road has been restored. Final restoration passed. |
123237229 | 2014-4-14 0:00: | AM | No Violations | 0.30 |
1447772382 | 2015-11-09 | Production Wells | No Violations | I was on location for a status check. During my inspection, I found J Well moving on location to plug the well for Energy Exploration. J Well rigged up and tagged the bottom of the well at 4,405. Tubing will be used for the bottom plug. Plugging will begin 11/11/2015. |
1447777948 | 2015-11-12 | Plug / Plug Back | No Violations | I was on location to witness J Well plug the well for Energy Exploration. J Well ripped the 4.5 casing at 2,965 and pulled two joints to set the Big Lime plug. Plug #2 was set from 2,915 to 2,616. Petroset rigged up and established circulation with eight barrels of fresh water. Petroset mixed and pumped 75 sacks of Class A cement. The cement was displaced to 2,615 with 41 barrels of fresh water. Next, J Well pulled 74 joints of 4.5 casing for the Berea Sandstone and surface plug. Petroset rigged up and established circulation with seven barrels of fresh water. Petroset mixed and pumped 100 sacks of Class A cement. I witnessed good cement returned to surface. J Well removed the final 12 joints and the well was topped off with cement. After 20 minutes, the cement held static at surface. A half-round container was used for all circulated returns. A total of 88 joints of 4.5 casing was removed from the well. |
1796604322 | 2014-03-26 | Production Wells | No Violations | My inspection found the well still shut-in. There was no production equipment associated with well. There was no identification sign posted for the well. According to our database, Energy Exploration has reported zero production since 2001. Photos were taken of the well. I called Energy Exploration and left a message to immediately file for a plugging permit. Also, I stated there was still no identification sign. |
189438888 | 2013-10-21 0:00 | PW | No Violations | 0.50 |
2137686555 | 2014-04-22 | Production Wells | No Violations | I was on location to perform a follow-up inspection in reference to Compliance #189438888. My inspection found the well not in production. There was a 4 piece of PVC pipe marking the wells location. I contacted ODNR in Columbus on 4/21/2014 and found that Energy Exploration had not filed for a plugging permit. I took photos of the well. There was no production equipment associated with the well. |
556427746 | 2015-6-29 0:00: | PW | No Violations | 2.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0189438888 | US-OH-119032 | 2015-11-25 | Failure to legibly identify well | |
0189438888 | US-OH-119033 | 2015-11-25 | Well shall be plugged |
For data sources see[8]