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Well ID: 34-155-22314 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Braceville Township | |
Operator Name: WAYNE HAMMOND ENTERPRISES INC | |
Well Pad ID: | |
Farm/Lease Name: HILAND | |
License Status: Producing | |
License Date: 1983-01-06 | |
Spud Date: 1983-02-03 | |
Spud Drilling Contractor: D A WALDRON | |
Final Drill Date: 1983-02-17 | |
Well Total Depth: 4435.00 ft | |
Configuration: Vertical | |
Latitude: 41.260000 | |
Longitude: -80.910000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-01-06 | Issued Date 12/30/82 Expired Date 6/28/83 Acres 0080000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04435 Proposed Drill Depth 04435 |
Original Spud | 1983-02-03 | IP. OIL = 1/2 BBL. |
Completed | 1983-02-17 | IP. OIL = 1/2 BBL. |
Reached Total Depth | 1983-02-17 | IP. OIL = 1/2 BBL. |
Construction Permit Expires | 1983-06-28 | IP. OIL = 1/2 BBL. |
CO | 1985-11-19 | 387 CHARLEBOIS ENERGY PROD IN GeoDate 1/6/83 |
Completion Report Received | 1985-12-30 | IP. OIL = 1/2 BBL. |
Change of Owner | 2005-12-29 | Operator changed from 387, CHARLEBOIS ENERGY PROD IN to 778, HAMMOND W ENTERPRISES INC |
Record Last Modified | 2017-02-15 | IP. OIL = 1/2 BBL. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4269 | 4302 | 11 |
4269 | 4302 | 11 | |
4269 | 4302 | 11 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 180 Mscf | 0 | |||
ACID | 0 | 500 Gal | 60000 | FRAC;H2O,SAND,N2 |
For data sources see[4]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | RAY PANDER TRUCKING INC | Brine | 80 | 335 |
2001 | WAYNE HAMMOND ENTERPRISES INC | Brine | 11 | 365 |
2002 | WAYNE HAMMOND ENTERPRISES INC | Brine | 0 | 365 |
2003 | WAYNE HAMMOND ENTERPRISES INC | Brine | 31 | 365 |
2004 | WAYNE HAMMOND ENTERPRISES INC | Brine | 27 | 365 |
2005 | WAYNE HAMMOND ENTERPRISES INC | Brine | 18 | 365 |
2006 | WAYNE HAMMOND ENTERPRISES INC | Brine | 21 | 365 |
2007 | WAYNE HAMMOND ENTERPRISES INC | Brine | 27 | 365 |
2008 | WAYNE HAMMOND ENTERPRISES INC | Brine | 25 | 365 |
2009 | WAYNE HAMMOND ENTERPRISES INC | Brine | 15 | 365 |
2010 | WAYNE HAMMOND ENTERPRISES INC | Brine | 0 | 365 |
2011 | WAYNE HAMMOND ENTERPRISES INC | Brine | 0 | 365 |
2012 | WAYNE HAMMOND ENTERPRISES INC | Brine | 41 | 366 |
2013 | WAYNE HAMMOND ENTERPRISES INC | Brine | 28 | 365 |
2014 | WAYNE HAMMOND ENTERPRISES INC | Brine | 0 | 365 |
2015 | WAYNE HAMMOND ENTERPRISES INC | Brine | 23 | 365 |
2016 | WAYNE HAMMOND ENTERPRISES INC | Brine | 66 | 365 |
2017 | WAYNE HAMMOND ENTERPRISES INC | Brine | 27 | 365 |
2018 | WAYNE HAMMOND ENTERPRISES INC | Brine | 7 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-532021766 | 2013-3-5 0:00:0 | PW | No Violations | 0.50 |
0000PL3922 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0532021766 | 2013-03-05 | Production Wells | No Violations | My inspection found the well equipped with a plunger lift unit. The tank battery contained one, 100 barrel production tank and a separator. The dike was highly weathered and not capable of containment requirements. The well was in production and the records were up to date on our database. There was a plug on the load line. The proper identification sign was posted. The lease road was in stable condition. This well share the tank battery with permit number 2-2123. I called the well tender, Jeremy Kohler, at 330-718-6335. I instructed him to build a new dike around the tank battery. |
1375099483 | 2013-07-29 | Production Wells | Violations Noted | My inspection found no dike built per my request on 3/5/2013. The tank battery contained a rusty, 100 barrel production tank and a rusty separator. I contacted Jeremy Kohler, the well tender, at 330-718-6335. I told Jeremy a compliance notice would be issued. I instructed him to have a new dike built and remove the overgrown weeds next to the separator by 8/9/2013. I asked Jeremy to paint the production tank and separator. According to Jeremy, Hammond Enterprises Inc. is owned by Ray Pander (300-654-2500). I called Ray Pander and left a message to return my call, so that I could obtain updated information. The proper identification was posted on the production tank. I took photos of the weathered dike. |
1407934835 | 2013-08-09 | UrbanProduction Wells | No Violations | I was on location for a follow-up inspection. I found a new dike built around the production equipment per my request. |
1787445885 | 2013-03-05 | Production Wells | No Violations | I followed up on a compliant filed by the landowner, Bryan Sommer. I called the Bryan and he said ODNR Inspector Jerry Kohl responded to the complaint. Jerry contacted the well tender to repair the leak immediately. I called the well tender, Jeremy Kohler, at 330-718-6335. He said the company completed the repair back in September 2012. I walked the flow line and found no further leaks. Also, my inspection of the tank battery and wellhead found no leaks or spills. |
PL3922 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1375099483 | US-OH-111123 | 2013-07-29 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[9]