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34-155-22629

Well Details

Well ID: 34-155-22629
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Country: United States
State: Ohio
County: Trumbull
Municipality: Brookfield Township
Operator Name: VORTEX ENERGY LLC
Well Pad ID:
Farm/Lease Name: W F DEVELOPMENT
License Status: Producing
License Date: 1984-09-05
Spud Date: 1984-09-20
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1984-09-25
Well Total Depth: 5150.00 ft
Configuration: Vertical
Latitude: 41.240000
Longitude: -80.570000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-09-05 Issued Date 9/5/84 Expired Date 3/4/85 Acres 0088980 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05150 Proposed Drill Depth 05150
Original Spud 1984-09-20
Completed 1984-09-25
Reached Total Depth 1984-09-25
CO 1984-11-02 54 TITAN ENERGY CORP GeoDate 9/5/84
Completion Report Received 1984-11-09
Construction Permit Expires 1985-03-04
Change of Owner 1998-01-26 Operator changed from 54, TITAN ENERGY CORP to 1333, BARR ROBT/dba BIG SKY PET
Change of Owner 2018-09-11 Operator changed from 1333, BIG SKY ENERGY INC to 9841, VORTEX ENERGY LLC
Record Last Modified 2018-09-11

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4972 5027 22
4972 5027 22
4972 5027 22

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 172 Mscf 0
ACID 0 500 Gal 0 FRAC: H2O,SAND,N2
H2O 0 78414 Gal 65500

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TITAN ENERGY CORP 2535.00 58.00 0
1986 TITAN ENERGY CORP 4474.00 145.00 365
1987 TITAN ENERGY CORP 1267.00 68.00 365
1988 TITAN ENERGY CORP 4031.00 75.00 365
1989 TITAN ENERGY CORP 2645.00 38.00 365
1990 TITAN ENERGY CORP 2315.00 77.00 365
1991 TITAN ENERGY CORP 801.00 0.00 365
1992 TITAN ENERGY CORP 1170.00 0.00 365
1993 TITAN ENERGY CORP 154.00 0.00 365
1994 TITAN ENERGY CORP 0.00 0.00 365
1997 TITAN ENERGY CORP 0.00 0.00 245
2000 BIG SKY ENERGY INC 1878.00 78.00 365
2001 BIG SKY ENERGY INC 1549.00 40.00 365
2002 BIG SKY ENERGY INC 2004.00 0.00 365
2003 BIG SKY ENERGY INC 728.00 0.00 365
2004 BIG SKY ENERGY INC 1168.00 45.00 365
2005 BIG SKY ENERGY INC 2354.00 28.00 365
2006 BIG SKY ENERGY INC 1077.00 0.00 365
2007 BIG SKY ENERGY INC 2464.00 0.00 365
2009 BIG SKY ENERGY INC 2247.00 0.00 365
2010 BIG SKY ENERGY INC 1791.00 36.00 365
2011 BIG SKY ENERGY INC 1322.00 0.00 365
2012 BIG SKY ENERGY INC 744.00 0.00 366
2013 BIG SKY ENERGY INC 466.00 0.00 365
2014 BIG SKY ENERGY INC 176.00 0.00 365
2016 BIG SKY ENERGY INC 0.00 0.00 0
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TITAN ENERGY CORP Brine 0 0
1986 TITAN ENERGY CORP Brine 0 365
1987 TITAN ENERGY CORP Brine 0 365
1988 TITAN ENERGY CORP Brine 0 365
1989 TITAN ENERGY CORP Brine 0 365
1990 TITAN ENERGY CORP Brine 0 365
1991 TITAN ENERGY CORP Brine 0 365
1992 TITAN ENERGY CORP Brine 0 365
1993 TITAN ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 0 365
1997 TITAN ENERGY CORP Brine 245
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 365
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 365
2014 BIG SKY ENERGY INC Brine 0 365
2016 BIG SKY ENERGY INC Brine 0 0
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-126300911 2016-6-1 0:00:0 UP No Violations
-187511172 2018-3-22 0:00: UP No Violations
-341674289 2016-1-15 0:00: UP No Violations 0.50
-763539061 2018-7-31 0:00: UP No Violations 3.20
0000PL3682 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0026121767 2016-04-18 UrbanProduction Wells Violations Noted I was on location for a status check. The well is equipped with a plunger lift assembly and the valves on the wellhead were open. There is a domestic gas line coming off of the 4.5 casing. The tank battery consisted of a 100 BBL production tank, a 50 BBL brine tank and a mechanical separator. There was a chart box with a chart showing no production. The 100 BBL production tank was leaking at the base of the tank. A plug needs installed on the brine tank valve. There was an identification sign on the production tank that needs updated to reflect the current owner information. There is no dike around the tank battery. The lease road is in stable condition. The following items need addressed:

1) Update the signage at the tank battery and install at the wellhead. 2) Remove leaking production tank and any impacted soil from the tank battery. Replace the leaking tank. 3) Install a plug on the brine tank tank valve. 4) Install a new dike around the tank battery equipment. 5) The well needs shut in immediately per the temporary restraining order issued by the Trumbull County Court of Common Pleas, dated 4/11/2016.

0126300911 2016-06-01 UrbanProduction Wells No Violations I was on location for a civil action follow-up inspection. The well is equipped with a plunger lift assembly and the valves on the wellhead were closed. There is a domestic gas line coming off of the 4.5 casing. The tank battery consisted of a 100 BBL production tank, a 50 BBL brine tank and a mechanical separator. There was a chart box with a chart showing no production. The 100 BBL production tank was leaking at the base of the tank. A plug needs installed on the brine tank valve. There was an identification sign on the production tank was updated to reflect the current owner information. There is no dike around the tank battery. The lease road is in stable condition. The following items need addressed.

1) Remove leaking production tank and any impacted soil from the tank battery. Replace the leaking tank. 2) Install a plug on the brine tank tank valve. 3) Install a new dike around the tank battery equipment.

0187511172 2018-03-22 UrbanProduction Wells No Violations I conducted a compliance notice follow-up for compliance notice 26121767. The well is equipped with a plunger lift assembly and the annulus and flow line valves were closed. There was a domestic gas line coming off of the 4.5 inch casing. The tank battery consisted of a 100 BBL production tank, a 50 BBL brine tank and a mechanical separator. There was a chart box with a chart showing no production. The 100 BBL production tank has not been replaced and a plug needs installed on the brine tank valve. There was an identification sign on the production tank was updated to reflect the current owner information. There was no dike around the tank battery installed. The lease road was in stable condition.
0341674289 2016-01-15 UrbanProduction Wells No Violations I was on location for a status check. During my inspection, I found the well in production. The well is equipped with a plunger lift assembly. There is a domestic gas line coming off of the wells 4.5 casing. At this time, the 2 flow line valve and the domestic flow line valve were in the closed position. The tank battery has a 100 barrel production tank, a 50 barrel brine tank and a mechanical separator. There is a stenciled identification sign on the production tank. There is no dike around the tanks. The lease road is in stable condition.
0637745714 2019-02-15 UrbanProduction Wells No Violations I conducted a compliance notice follow-up for compliance notice 26121767 and complaint #5916 regarding a gas leak at the well, installation of identification on location, repairing/replacing the leaking production tank, and reinstalling the dike around the tank battery. At the time of this inspection, none of the above mentioned items have been addressed. The well was equipped with a plunger lift assembly and in production. There was a domestic gas line coming off of the 4.5 inch casing with an open valve. I observed no gas leak at the well location, during this inspection. The tank battery consisted of a 100 BBL production tank, a 50 BBL brine tank and a mechanical separator. The chart on the sales line showed production. The 100 BBL production tank has not been repaired or replaced and was actively leaking from the dump line hammer union. An identification sign had been stenciled on the production tank with new company name information but was missing the well information. No dike has been reinstalled around the tank battery. I contacted Vortex Energy and left a message regarding the compliance issues that still need taken care of. I also contacted the landowner/complaintant Ms. Gloria Douglas and informed her that the gas leak has been remedied.
0763539061 2018-07-31 UrbanProduction Wells Violations Noted Follow-up to Complaint #5916 concerning a natural gas odor occurring near this Clinton Sandstone wellhead. My inspection found the wellhead equipped with 1.5 tubing and a plunger lift system. The 4.5 production casing and tubing flow line valves are closed and the well is currently not in production. I noticed a hissing sound 10 from the wellhead and found there is a gas leak occurring between the tubing and packing in the tubing head and also a minor leak at the packing between the 4.5 casing and 8.625 Braden head. There was no odor of natural gas in the surrounding area, and I did not smell gas until I was standing directly over the leak. The Ventis Pro 4 gas detector registered zero (0) LEL (lower explosive limit) during the inspection of the well and surrounding area. I found no evidence that brine or oil has leaked from the wellhead. Northeast Regional Supervisor Tom Hill contacted Big Sky Energy, while I was in route, to have someone meet on location to assess any issues. No Big Sky personnel responded to the request while I was on location. I spoke with the Complainant and told her of my findings. She said she was concerned that the recent drilling of a salt water injection well, 1800 to the southwest, was the cause of the issue. This natural gas leak is unrelated to the recent drilling activity. I advised the Complainant that the Division of Oil and Gas Resources Management will continue to monitor the leak and to avoid the area of the wellhead until the proper repairs could be made by the well owner. This well is just north of a residential area and the closest occupied dwelling is 125-130 south of the well. Due to the proximity of occupied dwellings, a Compliance Notice for general safety is being issued to Big Sky Energy Inc., to take corrective action immediately, and no later than 8/3/2018, to repair the leaks outlined above. Northeast Regional Supervisor Tom Hill is notifying Big Sky Energy Inc. owner, Bob Barr, of the Compliance Notice
1533313189 2018-08-03 UrbanProduction Wells No Violations I was on location to assess Compliance Notice # --treated separator is corroded with numerous holes. There was a chart box and 7-day chart inside the separator with no date. I obtained a second reading from the electronic timer at the wellhead which read 2 hours 59 minutes.
1533642855 2018-08-06 UrbanProduction Wells No Violations Follow up to Compliance Notice # -763539061 issued for general safety violations in regards to natural gas leaking at the wellhead and Complaint #5916. I was on location with Vortex Energy personnel to observe repairs being made to the wellhead. The pressure at the wellhead was sold down to 300psi and the tubing ring was tightened one (1) quarter turn and sealed the slips around the 1.5 tubing. The gate valve was closed and the hammer union between the tubing and the lubricator was replaced with a new union. The fittings on the copper line between the tubing port and the Logic controls were replaced. The brush around the wellhead was cut down and the wellhead and flow lines were painted. The minor bubbling around the 8.625 surface casing head will be addressed after the well has sold down further and will be plumbed in to the flow line with a check valve. I will inspect the well several more times to confirm that the repairs are sufficient prior to closing out the compliance notice and complaint.
1533750208 2018-08-08 UrbanProduction Wells No Violations Follow up to Compliance Notice # -763539061 and Complaint # 5916 issued in regards to a natural gas leak occurring at this wellhead. The leak at the tubing head was repaired on 8/6/18 by Vortex Energy personnel. I was on location today to confirm that the safety issue has been resolved and that the repairs at the wellhead were continuing to hold the 4.5 production casing head pressure below the tubing slips and seals. My inspection found 480psi on the tubing tee and no natural gas leaking from around the tubing slips. There is a minor effervescence around the 8.625 surface casing head and is not causing an odor or safety hazard. The Ventis Pro 4 registered zero (0) LEL (lower explosive limit) during the inspection. The Compliance Notice for general safety has been resolved and the odor complaint can be closed. No violations.
26121767 2016-4-18 0:00: UP No Violations
637745714 2019-2-15 0:00: UP No Violations 0.70
PL3682 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0026121767 US-OH-122698 2016-06-06 ID (a-i)
0026121767 US-OH-122699 2016-06-06 Well operation causing pollution and contamination
0026121767 US-OH-122700 2016-06-06 No SPCC dike/or failure to keep dike free of water or oil
0763539061 US-OH-128678 2018-09-04 General Safety

For data sources see[9]

References