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Well ID: 34-155-22953 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Howland Township | |
Operator Name: DUCK CREEK PETROLEUM LLC | |
Well Pad ID: | |
Farm/Lease Name: SIKO UNIT | |
License Status: Final Restoration | |
License Date: 2013-06-05 | |
Spud Date: 1986-07-19 | |
Spud Drilling Contractor: ADVENT DRLG | |
Final Drill Date: 1986-07-22 | |
Well Total Depth: 4530.00 ft | |
Configuration: Directional | |
Latitude: 41.270000 | |
Longitude: -80.810000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1986-06-02 | 1902 DUCK CREEK ENERGY INC GeoDate 6/2/86 |
Oil and Gas | 1986-06-02 | Issued Date 6/2/86 Expired Date Acres 0000000 Tool Type RTAF Proposed Formation Proposed Depth Proposed Drill Depth |
Original Spud | 1986-07-19 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
Completed | 1986-07-22 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
Reached Total Depth | 1986-07-22 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
Completion Report Received | 1986-11-10 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
CO | 1991-12-06 | 551 DUCK CREEK PETROLEUM GeoDate 6/2/86 |
APP | 1997-07-09 | 551 DUCK CREEK PETROLEUM Proposed Formation CLINTON Issued Date 7/9/97 Expired Date 7/9/98 6:00:00 AM |
APP | 2010-07-07 | Proposed Formations:CLINTON, Issued Date:7/7/2010, Expired Date:7/7/2011 6:00:00 AM, Drilling unit acres:47.89, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2013-06-05 | Proposed Formations:CLINTON, Issued Date:6/5/2013, Expired Date:6/5/2015 12:00:00 PM, Drilling unit acres:47.8, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-02-13 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
Construction Permit Expires | 2014-06-05 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
Record Last Modified | 2017-02-15 | PB DIRECTIONALLY DRIL 7-12-97 PERMIT EXPIRED. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4343 | 4439 | 18 |
4343 | 4439 | 18 | |
4343 | 4439 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 59300 Gal | 0 | FRAC: H2O |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | DUCK CREEK ENERGY INC | 0.00 | 0.00 | 0 |
1987 | DUCK CREEK ENERGY INC | 7902.00 | 155.00 | 365 |
1988 | DUCK CREEK ENERGY INC | 12174.00 | 70.00 | 365 |
1989 | DUCK CREEK ENERGY INC | 13729.00 | 68.00 | 365 |
1990 | DUCK CREEK ENERGY INC | 14965.00 | 66.00 | 365 |
1991 | DUCK CREEK ENERGY INC | 14236.00 | 0.00 | 365 |
1992 | DUCK CREEK PETROLEUM LLC | 11566.00 | 54.00 | 365 |
1993 | DUCK CREEK PETROLEUM LLC | 10807.00 | 0.00 | 365 |
1994 | DUCK CREEK PETROLEUM LLC | 9398.00 | 0.00 | 365 |
1995 | DUCK CREEK PETROLEUM LLC | 7911.00 | 0.00 | 365 |
1996 | DUCK CREEK PETROLEUM LLC | 1431.00 | 0.00 | 365 |
1997 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 365 |
1998 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
1999 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2000 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2001 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 365 |
2002 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2003 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2004 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2005 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 365 |
2006 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2007 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2008 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2009 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 365 |
2010 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2011 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
2012 | DUCK CREEK PETROLEUM LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1902819601 | 2014-2-13 0:00: | PB | No Violations | 4.50 |
-769523308 | 2014-7-1 0:00:0 | FR | No Violations | 0.50 |
0000PL3451 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0769523308 | 2014-07-01 | Final Restoration | No Violations | I was on location for a final restoration. I found during my inspection the site restored. The site was graded. Vegetation was well established. All production equipment was removed. All debris was removed. Above ground containers were used for all returns during the plugging of the well; no pits were used. A landowner waiver was received for the lease road. Restoration passed. |
1392735590 | 2014-02-12 | Plug / Plug Back | No Violations | My inspection found that Nicks Well Plugging set the bottom plug for Duck Creek Petroleum. Plug #1 was set from 4,143 to 4,489. Nicks operator mixed and pumped 30 sacks of Class A cement through 1.5 tubing. The cement was displaced with 16 bbls of water. Next, the operator removed 4,265 of 1.5 tubing. Once the tubing was removed, Nicks operator ripped the 4.5 casing at 3,165. Nicks crew pulled 8 joints of 4.5 casing to set Plug #2 at the Big Lime formation first thing the next day. The well was shut-in overnight. |
1902819601 | 2014-02-13 | Plug / Plug Back | No Violations | I witnessed Nicks Well Plugging complete the plugging for Duck Creek Petroleum. Plug #2 was set from 2,550 to 2,850. Nicks operator established circulation with 30 barrels of water. The operator mixed and pumped 86 sacks of Class A cement. The cement was displaced with 40 barrels of water. Next, the operator pulled 57 joints of 4.5 casing. Plug #3 was set from 430 to surface. Nicks operator established circulation with 10 barrel of water. The operator mixed and pumped 131 sacks of Class A cement. I witnessed a good return of cement at surface. Nicks operator removed the final 10 joints of 4.5 casing and topped of the well with cement. After 15 minutes, the cement held static at surface. A total of 75 joints of 4.5 casing was removed from the well. All circulated water and cement was placed into a tarp covered half round container. |
PL3451 | PL | No Violations |
For data sources see[9]