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34-155-23080

Well Details

Well ID: 34-155-23080
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Country: United States
State: Ohio
County: Trumbull
Municipality: Weathersfield Township
Operator Name: J WELL SERVICE INC
Well Pad ID:
Farm/Lease Name: CROOKS UNIT
License Status: Producing
License Date: 1987-03-31
Spud Date: 1987-06-12
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]]
Final Drill Date: 1987-06-18
Well Total Depth: 5050.00 ft
Configuration: Vertical
Latitude: 41.200000
Longitude: -80.720000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1987-03-31 2651 D & L ENERGY INC GeoDate 3/31/87
Oil and Gas 1987-03-31 Issued Date 3/31/87 Expired Date 3/30/88 Acres 0040474 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05050 Proposed Drill Depth 05050
Original Spud 1987-06-12 CHG. ACG. 11/21/87
Completed 1987-06-18 CHG. ACG. 11/21/87
Reached Total Depth 1987-06-18 CHG. ACG. 11/21/87
Construction Permit Expires 1988-03-30 CHG. ACG. 11/21/87
Completion Report Received 1988-10-31 CHG. ACG. 11/21/87
Change of Owner 2015-01-27 Operator changed from 2651, D & L ENERGY INC to 9426, BOBCATE WELL AND PIPELINE LLC
Record Last Modified 2017-02-15 CHG. ACG. 11/21/87

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4800 4908 40
4800 4908 40
2006-09-11 4890 4910 0
4890 4910 0
4800 4908 40

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 1000 Gal 0 FRAC: WATER, SAND, ACID
H2O 0 1500 Bbl 120000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 D & L ENERGY INC 32442.00 341.00 334
1989 D & L ENERGY INC 19065.00 124.00 365
1990 D & L ENERGY INC 12775.00 123.00 365
1991 D & L ENERGY INC 11.00 70.00 365
1992 D & L ENERGY INC 7114.00 0.00 365
1993 D & L ENERGY INC 8236.00 104.00 365
1994 D & L ENERGY INC 8241.00 48.00 365
1995 D & L ENERGY INC 7355.00 54.00 365
1996 D & L ENERGY INC 6339.00 65.00 365
1997 D & L ENERGY INC 5264.00 55.00 365
1998 D & L ENERGY INC 3722.00 53.00 365
1999 D & L ENERGY INC 4714.00 0.00 365
2000 D & L ENERGY INC 5048.00 120.00 365
2001 D & L ENERGY INC 4535.00 0.00 365
2002 D & L ENERGY INC 4701.00 61.00 365
2003 D & L ENERGY INC 4255.00 55.00 365
2004 D & L ENERGY INC 3031.00 0.00 365
2005 D & L ENERGY INC 4605.00 45.00 365
2006 D & L ENERGY INC 2985.00 0.00 365
2007 D & L ENERGY INC 3302.00 52.00 365
2008 D & L ENERGY INC 3155.00 0.00 366
2009 D & L ENERGY INC 4127.00 52.00 365
2010 D & L ENERGY INC 4585.00 0.00 365
2011 D & L ENERGY INC 4212.00 55.00 0
2012 D & L ENERGY INC 3926.00 0.00 365
2013 D & L ENERGY INC 3469.00 44.00 365
2014 D & L ENERGY INC 3121.00 0.00 365
2015 BOBCAT WELL & PIPELINE LLC 1680.00 0.00 261
2016 BOBCAT WELL & PIPELINE LLC 28.00 0.00 5
2017 BOBCAT WELL & PIPELINE LLC 0.00 16.00 2

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 D & L ENERGY INC Brine 0 334
1989 D & L ENERGY INC Brine 65 365
1990 D & L ENERGY INC Brine 50 365
1991 D & L ENERGY INC Brine 0 365
1992 D & L ENERGY INC Brine 0 365
1993 D & L ENERGY INC Brine 0 365
1994 D & L ENERGY INC Brine 50 365
1995 D & L ENERGY INC Brine 50 365
1996 D & L ENERGY INC Brine 0 365
1997 D & L ENERGY INC Brine 0 365
1998 D & L ENERGY INC Brine 27 365
1999 D & L ENERGY INC Brine 0 365
2000 D & L ENERGY INC Brine 0 365
2001 D & L ENERGY INC Brine 0 365
2002 D & L ENERGY INC Brine 55 365
2003 D & L ENERGY INC Brine 0 365
2004 D & L ENERGY INC Brine 0 365
2005 D & L ENERGY INC Brine 2 365
2006 D & L ENERGY INC Brine 50 365
2007 D & L ENERGY INC Brine 4 365
2008 D & L ENERGY INC Brine 0 366
2009 D & L ENERGY INC Brine 62 365
2010 D & L ENERGY INC Brine 0 365
2011 D & L ENERGY INC Brine 0
2012 D & L ENERGY INC Brine 0 365
2013 D & L ENERGY INC Brine 50 365
2014 D & L ENERGY INC Brine 0 365
2015 BOBCAT WELL & PIPELINE LLC Brine 261
2016 BOBCAT WELL & PIPELINE LLC Brine 0 5
2017 BOBCAT WELL & PIPELINE LLC Brine 1 2

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1224807451 2004-6-23 0:00: PW No Violations
-333194548 2007-11-15 0:00 PW No Violations
0000PL3351 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0278806471 2014-06-16 UrbanProduction Wells No Violations I was on location to perform a follow-up inspection. I found during my inspection that a new dike has not been built per my request. I called Dave Rice and left a message to return call concerning the dike. I received a return call from Rodney of Signature Earth Works. Rodney stated he was contracted by D & L to build the dike. Rodney said the work would begin tomorrow, 6/17/2014. I told Rodney a follow-up inspection would be performed by 6/20/2014.
0333194548 2007-11-15 Production Wells No Violations no violations .
0633333618 2005-07-21 Production Wells No Violations Case# 05-004 , Jean Real . Inspection showed no evidence at surface well or tank battery caused pine trees to die . No violations . RESOLVED .
0916595337 2018-08-13 Work Over Reconditioning No Violations I was on location with Inspector John Fleming, Emergency Operations Manager Andrew Adgate, Dave Rice (Bobcat), Petro Well Oilfield Services (PWS), and CES to observe repairs to the 4.5 production casing. PWS pulled one (1) joint of 1.5 tubing, attached a change over, and ran a joint of 2.375 tubing back in with an R4 packer. The packer was set and the pressure on the casing was mitigated for repairs. The bad section of casing was removed and a competent piece of casing with a collar was installed. The packer was removed and the tubing head was re-installed and the tubing slips and packing were replaced. The gate valve and lubricator were installed and the well is no longer leaking. No violations.
1055355946 2014-06-24 UrbanProduction Wells No Violations I was on location for a follow-up inspection. I found during my inspection that a new dike was built per my request.
1058806825 2014-04-18 UrbanProduction Wells No Violations My inspection found the well in production. The well was equipped with a plunger lift unit. A domestic gas line came off of the 4.5 casing. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank and a separator. The dike was weathered and not capable of meeting containment requirements. Identification signs were posted at the production tank. A bull plug was installed on the load line. There was a 16 day production chart inside the separator. The lease road was in stable condition. The well was placed into production prior to House Bill 278. I called Dave Rice and left a message to have a new dike build.
1130714422 2005-07-21 Production Wells No Violations no violations .,
1224807451 2004-06-23 Production Wells No Violations no violations .
278806471 2014-6-16 0:00: UP No Violations 0.50
423798936 2019-12-2 0:00: UP No Violations
633333618 2005-7-21 0:00: PW No Violations
916595337 2018-8-13 0:00: WR No Violations 5.80
PL3351 PL No Violations

For data sources see[9]

References