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34-155-23221

Well Details

Well ID: 34-155-23221
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: DEMSEY
License Status: Final Restoration
License Date: 2017-12-20
Spud Date: 1988-09-21
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1988-09-28
Well Total Depth: 5108.00 ft
Configuration: Vertical
Latitude: 41.130000
Longitude: -80.690000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1988-08-24 1702 LOMA ENTERPRISES INC GeoDate 8/24/88
Oil and Gas 1988-08-24 Issued Date 8/24/88 Expired Date 8/24/89 Acres 0040737 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05108 Proposed Drill Depth 05108
Original Spud 1988-09-21 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT
Completed 1988-09-28 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT
Reached Total Depth 1988-09-28 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT
Completion Report Received 1988-11-14 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT
Change of Owner 1999-10-14 Operator changed from 1702, LOMA ENTERPRISES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2010-05-06 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2017-12-20 Proposed Formations:CLINTON SANDS, Issued Date:12/20/2017, Expired Date:12/20/2019 12:00:00 PM, Drilling unit acres:40.737, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-01-25 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT
Record Last Modified 2019-06-05 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT
Construction Permit Expires 2019-12-20 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM PLUG STUTUS UPDATED PER PLUG REPORT

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4860 4908 21
4860 4908 21
4860 4908 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 83200 60000 FRAC:WATER/SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 LOMA ENTERPRISES INC 7061.00 165.00 357
1991 LOMA ENTERPRISES INC 15260.00 918.00 365
1992 LOMA ENTERPRISES INC 12717.00 574.00 365
1993 LOMA ENTERPRISES INC 10129.00 432.00 365
1994 LOMA ENTERPRISES INC 7117.00 382.00 365
1995 LOMA ENTERPRISES INC 7036.00 287.00 365
1996 LOMA ENTERPRISES INC 6726.00 204.00 365
1997 LOMA ENTERPRISES INC 6560.00 287.00 365
1998 LOMA ENTERPRISES INC 5749.00 156.00 365
1999 EXCO - NORTH COAST ENERGY INC 1602.00 0.00 91
2000 EXCO - NORTH COAST ENERGY INC 6330.00 131.00 365
2001 EXCO - NORTH COAST ENERGY INC 5782.00 75.00 365
2002 EXCO - NORTH COAST ENERGY INC 4827.00 64.00 365
2003 EXCO - NORTH COAST ENERGY INC 5827.00 145.00 365
2004 EXCO - NORTH COAST ENERGY INC 6011.00 115.00 365
2005 EXCO - NORTH COAST ENERGY INC 4681.00 156.00 365
2006 EXCO - NORTH COAST ENERGY INC 5144.00 62.00 365
2007 EXCO - NORTH COAST ENERGY INC 4602.00 116.00 365
2008 EXCO - NORTH COAST ENERGY INC 4540.00 71.00 366
2009 EXCO - NORTH COAST ENERGY INC 4059.00 75.00 365
2010 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 3850.00 129.00 0
2012 ENERVEST OPERATING LLC 4262.00 46.00 366
2013 ENERVEST OPERATING LLC 3706.00 33.00 365
2014 ENERVEST OPERATING LLC 2932.00 57.00 365
2015 ENERVEST OPERATING LLC 1921.00 44.00 365
2016 ENERVEST OPERATING LLC 2058.00 61.00 366
2017 ENERVEST OPERATING LLC 3194.00 123.00 365
2018 ENERVEST OPERATING LLC 271.00 0.00 211

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 LOMA ENTERPRISES INC Brine 85 357
1991 LOMA ENTERPRISES INC Brine 318 365
1992 LOMA ENTERPRISES INC Brine 160 365
1993 LOMA ENTERPRISES INC Brine 86 365
1994 LOMA ENTERPRISES INC Brine 55 365
1995 LOMA ENTERPRISES INC Brine 66 365
1996 LOMA ENTERPRISES INC Brine 15 365
1997 LOMA ENTERPRISES INC Brine 90 365
1998 LOMA ENTERPRISES INC Brine 40 365
1999 EXCO - NORTH COAST ENERGY INC Brine 91
2000 EXCO - NORTH COAST ENERGY INC Brine 70 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 20 365
2004 EXCO - NORTH COAST ENERGY INC Brine 43 365
2005 EXCO - NORTH COAST ENERGY INC Brine 60 365
2006 EXCO - NORTH COAST ENERGY INC Brine 30 365
2007 EXCO - NORTH COAST ENERGY INC Brine 30 365
2008 EXCO - NORTH COAST ENERGY INC Brine 23 366
2009 EXCO - NORTH COAST ENERGY INC Brine 38 365
2010 EXCO - NORTH COAST ENERGY INC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 36
2012 ENERVEST OPERATING LLC Brine 18 366
2013 ENERVEST OPERATING LLC Brine 5 365
2014 ENERVEST OPERATING LLC Brine 2 365
2015 ENERVEST OPERATING LLC Brine 0 365
2016 ENERVEST OPERATING LLC Brine 0 366
2017 ENERVEST OPERATING LLC Brine 15 365
2018 ENERVEST OPERATING LLC Brine 0 211

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1044483337 2015-5-21 0:00: UP No Violations 1.00
-1387779631 2018-1-26 0:00: PB No Violations 4.00
-1435745520 2018-1-24 0:00: PB No Violations 12.00
-1552322645 2018-1-23 0:00: PB No Violations
1044483337 2015-05-21 UrbanProduction Wells No Violations I was on location for a follow-up inspection. During my inspection, I found majority of the broken up concrete with the half inch rebar removed. Fill dirt has been spread and compacted over the new 12 inch drainage pipe. Enervest has access to the tank battery and well by driving over the drainage pipe. I will continue to perform inspections while construction is in progress by Vallource. Additional photos were taken and are available upon request.
1387779631 2018-01-26 Plug / Plug Back No Violations Appalachian Well Survey was on location to set a bridge plug at 200 in side of the 8-5/8 casing. Chipco Cementing pumped a 150 cement plug. A cap was welded on the 8-5/8 casing with the ID.
1432207568 2015-05-11 UrbanProduction Wells No Violations I was on location to meet Larry Lower, field supervisor for Enervest, to discuss safety concerns around and at the well and production equipment. According to Mr. Lower, the company Vallource Star has been renovating the Steel Plant property. This construction has created limited access to perform maintenance on the tank battery and well. Mr. Lower stated the production tank has seven foot of oil and they are unable to get close enough to remove the product from the tank. During my inspection, I found:





Upon further inspection, I found the well in production. The well is equipped with a plunger lift assembly. The tank battery consists of a 100 barrel production tank, a 30 barrel brine tank and a mechanical separator. An identification sign is posted on the production tank.


1432300924 2015-05-12 Administrative Inspection No Violations





I told Vallource Star:


-1-02(E)(1), access down to the tank battery needs to be replaced to permit the ingress and egress for fire and emergency response.


Vallource Star stated they will address and correct all health and safety issues. I told Vallource Star that weekly inspections will be conducted until all health and safety issues are address. Also, I informed them that photos were taken and available upon request.

1435745520 2018-01-24 Plug / Plug Back No Violations I was with Inspector Shannon Mullins performing the plugging operation on the above location. Chipco Oil Field Svc were the plugging contractor and the Cementing Contractors. We set the Clinton, Big Lime plug and the Surface Plug.
1516741226 2018-01-23 Plug / Plug Back No Violations I was on location to witness the plugging of this well. Chipco, LLC was the contractor for Enervest operating and had pulled the 1.5 inch tubing from the well. A total of 4835 feet of tubing was removed. Chipco removed the seating nipple and downhole equipment, then ran the tubing back into the well to set the bottom plug. Additional joints of tubing were added until a depth of 4968 feet was reached to set the bottom plug. Prior to setting the plug, Chipco pumped 110 BBLs of water downhole and did not break circulation. Water pH was tested at 6 and the temperature was 35 degrees. The plug was set from 4968 to 4603 feet using the 1.5 inch tubing, and the cement was scaled and weighed 15.0 ppg. The well will be left overnight to allow for the cement to setup. No violations observed.
1552322645 2018-01-23 Plug / Plug Back No Violations I was with Inspector Shannon Mullins performing the plugging operation on the above location. Chipco Oil Field Svc were the plugging contractor and the Cementing Contractor.
1578928769 2020-1-13 0:00: FR No Violations 0.50

For data sources see[9]

References