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Well ID: 34-155-23302 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: PETROX, INC | |
Well Pad ID: | |
Farm/Lease Name: BURNACH | |
License Status: Final Restoration | |
License Date: 2013-10-21 | |
Spud Date: 1989-10-08 | |
Spud Drilling Contractor: [[EPC [EASTERN PETROLEUM]]] | |
Final Drill Date: 1989-10-14 | |
Well Total Depth: 4733.00 ft | |
Configuration: Vertical | |
Latitude: 41.230000 | |
Longitude: -80.750000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1989-09-14 | 2125 EASTERN PETROLEUM CO GeoDate 9/14/89 |
Oil and Gas | 1989-09-14 | Issued Date 9/14/89 Expired Date 9/14/90 Acres 0060478 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04733 Proposed Drill Depth 04733 |
Original Spud | 1989-10-08 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
Completed | 1989-10-14 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
Reached Total Depth | 1989-10-14 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
Completion Report Received | 1989-10-24 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
CO | 1996-10-03 | 213 LOMAK OPERATING CO GeoDate 9/14/89 |
Change of Owner | 1998-05-14 | Operator changed from 213, LOMAK OPERATING CO to 1966, PETROX INC |
APP | 1998-05-29 | Proposed Formations:CLINTON, Issued Date:5/29/98, Expired Date:5/29/99 6:00:00 AM, Drilling unit acres:60.478, Proposed Well Type:OG, Proposed Well Class: |
APP | 2013-10-21 | Proposed Formations:CLINTON, Issued Date:10/21/2013, Expired Date:10/21/2015 12:00:00 PM, Drilling unit acres:60.478, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-11-19 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
Construction Permit Expires | 2015-10-21 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
Record Last Modified | 2018-03-22 | LANDOWNER WAIVER APPROVED TO LEAVE FLOW LINE INTACT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4452 | 4570 | 0 |
4452 | 4570 | 0 | |
4452 | 4570 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | FRAC:WATER/SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | EASTERN PETROLEUM CO | 7180.00 | 1811.00 | 365 |
1992 | EASTERN PETROLEUM CO | 2286.00 | 747.00 | 365 |
1993 | EASTERN PETROLEUM CO | 4898.00 | 602.00 | 365 |
1994 | EASTERN PETROLEUM CO | 4816.00 | 372.00 | 365 |
1997 | RANGE OPERATING COMPANY | 222.00 | 33.00 | 92 |
1998 | PETROX, INC | 1793.00 | 128.00 | 180 |
2000 | PETROX, INC | 2132.00 | 239.00 | 365 |
2001 | PETROX, INC | 1067.00 | 59.00 | 365 |
2002 | PETROX, INC | 1555.00 | 51.00 | 336 |
2003 | PETROX, INC | 1315.00 | 0.00 | 365 |
2004 | PETROX, INC | 865.00 | 0.00 | 365 |
2005 | PETROX, INC | 1130.00 | 0.00 | 365 |
2006 | PETROX, INC | 1098.00 | 0.00 | 365 |
2007 | PETROX, INC | 471.00 | 45.00 | 365 |
2008 | PETROX, INC | 514.00 | 0.00 | 365 |
2009 | PETROX, INC | 515.00 | 0.00 | 253 |
2010 | PETROX, INC | 169.00 | 0.00 | 365 |
2011 | PETROX, INC | 8.00 | 0.00 | 365 |
2012 | PETROX, INC | 504.00 | 0.00 | 366 |
2013 | PETROX, INC | 283.00 | 0.00 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | EASTERN PETROLEUM CO | Brine | 2225 | 365 |
1992 | EASTERN PETROLEUM CO | Brine | 1656 | 365 |
1993 | EASTERN PETROLEUM CO | Brine | 1431 | 365 |
1994 | EASTERN PETROLEUM CO | Brine | 1102 | 365 |
1997 | RANGE OPERATING COMPANY | Brine | 45 | 92 |
1998 | PETROX, INC | Brine | 935 | 180 |
2000 | PETROX, INC | Brine | 928 | 365 |
2001 | PETROX, INC | Brine | 570 | 365 |
2002 | PETROX, INC | Brine | 825 | 336 |
2003 | PETROX, INC | Brine | 564 | 365 |
2004 | PETROX, INC | Brine | 675 | 365 |
2005 | PETROX, INC | Brine | 666 | 365 |
2006 | PETROX, INC | Brine | 628 | 365 |
2007 | PETROX, INC | Brine | 365 | |
2008 | PETROX, INC | Brine | 391 | 365 |
2009 | PETROX, INC | Brine | 404 | 253 |
2010 | PETROX, INC | Brine | 0 | 365 |
2011 | PETROX, INC | Brine | 140 | 365 |
2012 | PETROX, INC | Brine | 653 | 366 |
2013 | PETROX, INC | Brine | 245 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1001102184 | 2013-12-16 0:00 | UP | No Violations | 0.50 |
-1077053350 | 2013-11-19 0:00 | PB | No Violations | 6.50 |
-1314992996 | 2014-6-24 0:00: | FR | No Violations | 0.50 |
-1679275151 | 2012-6-14 0:00: | PW | No Violations | 0.50 |
-452164543 | 2013-11-18 0:00 | PB | No Violations | 6.00 |
0452164543 | 2013-11-18 | Plug / Plug Back | No Violations | I witnessed Nicks Well Plugging plug the well for Petrox, Inc. Nick removed 4,437 of 1.5 tubing from the well. Next, the operator pumped 10 bbls of water followed by bull heading 30 sacks of Class A cement with 50 lbs of Hauls for Plug #1. The plug was set from 4,286 to 4,578. Once the plug was in place, the well was shut-in overnight with 2,000 psi. |
1001102184 | 2013-12-16 | UrbanProduction Wells | No Violations | My inspection found all of the production equipment removed. Landowner waiver has been obtained for the lease road. Grading and seeding will be completed in early spring due to the weather. |
1077053350 | 2013-11-19 | Plug / Plug Back | No Violations | I witnessed Nicks Well Plugging plug for Petrox, Inc. Nick ripped the 4.5 casing at 3,343 and pulled 8 joints to set the Big Lime Plug #2. The operator established circulation with 10 bbls of fresh water and pumped 86 sacks of Class A cement. The cement was displaced with 43 bbls of fresh water. Plug #2 was set from 2,704 to 3,004. Next, Nick pulled 64 joints of 4.5 casing to set Plug #3 for the surface casing within the Ohio Shale. The operator established circulation with 15 bbls of fresh water and pumped 125 sacks of Class A cement. I witnessed good cement returned to surface. Plug #3 was set from 411 to surface. The operator pulled the remaining 12 joints and the cement was topped off. The cement was static after 20 minutes. A total of 84 joints of 4.5 casing was removed from the well. All circulated water and cement was pumped into tarp covered half round container. |
1314992996 | 2014-06-24 | Final Restoration | No Violations | I was on location to perform a final restoration. I found during my inspection that all production equipment had been removed. The site was graded. Vegetation was well established. There was no pits used during the plugging of the well. All debris was removed from the site. No landowner waiver for the lease road was required; access to the well and tank battery was by an asphalt driveway owned by the condominium complex. Final Restoration passed. |
1451084086 | 2014-04-18 | Plug / Plug Back | No Violations | My inspection found the well site not graded or seeded. All production equipment was removed from the location. I called Petrox, Inc. and left a message for an approximate date to complete the final restoration. |
1679275151 | 2012-06-14 | Production Wells | No Violations | On 6/14/2012, I completed a production well inspection status check. My inspection found the well was equipped with a pumping unit surrounded by a chain link fence that was in good condition. The tank battery contained two 100 barrel oil storage tanks, one 50 barrel brine storage tank, a separator, and the proper identification was posted. I noticed no visible spills or leaks. The lease road was in good condition and located between two pine trees, close to the entrance to the housing allotment. There are no violations at this time. |
For data sources see[9]