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34-155-24096

Well Details

Well ID: 34-155-24096
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Country: United States
State: Ohio
County: Trumbull
Municipality: Liberty Township
Operator Name: PAC DRILLING LLC
Well Pad ID:
Farm/Lease Name: PAC
License Status: Well Drilled
License Date: 2017-04-05
Spud Date: 2017-04-12
Spud Drilling Contractor: H A D INC
Final Drill Date: 2017-04-29
Well Total Depth: 7474.00 ft
Configuration: Horizontal
Latitude: 41.170000
Longitude: -80.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2017-02-08 Proposed Formations:CLINTON SAND, Issued Date:2/8/2017, Expired Date:2/8/2018 12:00:00 PM, Drilling unit acres:170.55, Proposed Well Type:OG, Proposed Well Class:POOL
APP 2017-04-05 Proposed Formations:CLINTON, Issued Date:4/5/2017, Expired Date:4/5/2019 12:00:00 PM, Drilling unit acres:170.55, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2017-04-29
Record Last Modified 2018-01-22
Construction Permit Expires 2018-04-05

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2017-09-14 H2O 0 1400 Bbl 0 Reliance Well Service Reliance Well Service was the stimulation contracor and Sure fire Wireline was the wireline contractor.

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2018 PAC DRILLING LLC 10048.00 1236.00 360

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2018 PAC DRILLING LLC Brine 733 360

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1005069064 2019-11-18 0:00 UP No Violations
-1144704030 2019-7-2 0:00:0 UP No Violations
-1241354431 2017-4-24 0:00: DD No Violations 2.00
-127449066 2017-10-2 0:00: UD No Violations 1.00
-1296309753 2017-8-1 0:00:0 CT No Violations 1.50
-1343619959 2017-8-24 0:00: UD No Violations 1.70
-1424715224 2017-6-15 0:00: DD No Violations 4.20
-1529829522 2017-9-14 0:00: CT No Violations
-1636024880 2017-8-16 0:00: UD No Violations
-1706054514 2017-11-7 0:00: UD No Violations 0.70
-1754423120 2017-5-1 0:00:0 UD No Violations 2.00
-1817745461 2017-5-8 0:00:0 UD No Violations 1.00
-1834271336 2017-6-1 0:00:0 DD No Violations
-1948455486 2017-10-19 0:00 UD No Violations 0.50
-213785068 2017-7-7 0:00:0 UD No Violations 4.00
-248164618 2017-7-10 0:00: UD No Violations 2.00
-271743436 2017-8-28 0:00: UD No Violations 2.50
-555150512 2017-4-12 0:00: DD No Violations 4.00
-555854563 2018-5-18 0:00: UL No Violations
-575159673 2017-8-25 0:00: WR No Violations
-883128395 2017-4-18 0:00: DD No Violations 1.00
0091257042 2017-04-14 Drill / Deepen / Reopen No Violations
0127449066 2017-10-02 Urban Drill / Deepen / Reopen No Violations I found the well in good repair on the day of my inspection. PAC Drilling has started building the tank battery. There are two (2) 210 bbl. storage tanks, a 100 bbl. storage tank, and a separator on site. The drilling pit is closed. There are 12 frac tanks on site. The access road is in good repair with a locked gate and identification sign.
0213785068 2017-07-07 Urban Drill / Deepen / Reopen No Violations
0248164618 2017-07-10 Urban Drill / Deepen / Reopen No Violations
0271743436 2017-08-28 Urban Drill / Deepen / Reopen No Violations
0450145374 2017-05-10 Drill / Deepen / Reopen No Violations I found the depth of the Hole #3 at 6,890. HAD is drilling at rate of 14.8 to 16.8 ft/hr through the Clinton Sandstone formation.
0514613019 2017-04-10 Drill / Deepen / Reopen No Violations I found the PAC Drilling working on the well pad. Stockpiles have been placed on the south and east sides of the pad. An earthen berm has been built on the north side. A drainage ditch has been constructed along the north side of the access road. Silt fences are in place along the access road. Grass seed and straw has been spread on both sides of the access road and on the berm.
0555150512 2017-04-12 Drill / Deepen / Reopen No Violations

-round container. The drilling permit was located in the doghouse.

0555854563 2018-05-18 UrbanPreliminary Restoration Violations Noted Access was gained through a locked gated on a graveled road. During my inspection I identified violations of OAC 1501-9-9-05 and OAC 1501-9-08 (N). The tank battery was surrounded with an earthen dike and an locked access door. There was only one (1) access door built into the fence. The tank battery consisted of three (3) 210 barrel stock tanks, one (1) 100 barrel brine tank and one (1) horizontal mechanical separator. Identifying signage was legible and on the ground, leaning against the fence. The tanks had the required carbon filters, pressure sealing hatches, pressure relief valves and lightning arrestor. The load lines were plugged, but not locked. The handles were removed. The eastern most 210 barrel and 100 barrel brine tanks did not have plugs in the two (2) inch bungs which allowed natural gas fumes to vent to the atmosphere. There dike and disturbed area around the tank battery was rough graded, but not seeded. Erosional features were present on the barren ground. There was non-essential items in and around the tank battery such as hand rails, a roll of geotex fabric lying along the road, plastic pipes, buckets and assorted fittings. The graveled access road continued to the wellhead. The area of disturbance was rough graded, but was void of vegetation and not stable. Non-essential materials, lumber, pallets and pipes were scattered around the perimeter of the disturbed area. There were erosional features crossing the location from north to south. I found a six (6) to eight (8) inch hole, near the former pit area, where water was observed flowing from and across location. I field tested the effluent from the hole and found the Chlorides level was less than 32 ppm and the pH was 6. The well was completed as an electric pumping well. The wellhead was not identified. The wellhead was fenced, but had gaps in fencing large enough as to offer no security. The access door was not locked. The stuffing box and tubing head were covered with grease and oil. The cel
0575159673 2017-08-25 Work Over Reconditioning No Violations I observed Team Services ( service rig contractor ) lowering a work string of 2.375 tubing and downhole mill assembly into the 4.5 production to mill and remove a composite bridge plug that had prematurely set. Baker Services were the tool and fishing consultants on location with Nicks Well Plugging suppling the pumping services. Plan forward was to isolate a previously stimulated stage ( stage had screened out ) with a bridge plug and perforate the next stage conveyed on tubing. Discussions with Rick Skidmore ( ODNR ), Jason Caldwell ( PAD Drilling ) and myself effected a plan to close the pit as soon as possible. Water trucks were scheduled to start removing the remaining fluid on 8/26/2017. Inspector Skidmore will follow up and confirm the timely pit closure. No violations identified during this inspection.
0700380224 2017-04-25 UrbanProduction Wells No Violations

-E-

0753872920 2017-09-18 UrbanProduction Wells No Violations There was not any activity on location. The frac job was completed on 9/15/2017. No violations.
0826787526 2017-06-23 Urban Drill / Deepen / Reopen No Violations
0883128395 2017-04-18 Drill / Deepen / Reopen No Violations
0902130929 2017-05-15 Drill / Deepen / Reopen No Violations
1003221899 2017-05-24 Drill / Deepen / Reopen No Violations I found the HAD rig has moved off location. The matting was being removed on the day of my inspection. The pit is still open. Spoke with Jeremy Caldwell on location. Mr. Caldwell requested leaving the pit open through perforation of the well and stimulation. Well stimulation is tenative for the week of 6/5/2017. Mr. Caldwell stated the water in the pit will be removed on 5/25/2017. There is an orange safety fence surrounding the pit.
1014656419 2017-10-02 Urban Drill / Deepen / Reopen No Violations I found the well shut-in on the day of my inspection. There are 12 frac tanks on location. Preliminary restoration has not begun at this time. The pits have been closed. PAC has begun building the tank battery with two (2) 210 bbl. storage tanks, a 100 bbl. storage tank, and a separator on location. The site is secure with a locked access road gate. There is an identification sign posted on the access road gate.
1241354431 2017-04-24 Drill / Deepen / Reopen No Violations

-owner of PAC Drilling. I instructed Mr. Caldwell to put the silt fence back in place. Mr. Caldwell stated the issue would be address immediately.

1296309753 2017-08-01 Completion Testing No Violations I was on location with Trumbull County Inspector Rick Skidmore to inspect this horizontal, Clinton Sandstone well pad following the well sanding off during Stage 1 of the frac job. Operations are currently on hold as PAC Drilling re-configures their plans for completing this well and there is no activity or personnel on location today. The well is currently shut-in with a frac (gate) valve and the annular valve between the 7 intermediate casing and 4.5 production casing is open and quiescent. There are 12-500 barrel frac tanks on the south side of the pad. There is a lined pit on the east side of the pad and the liner has a 15 long tear on the eastern, steep wall of the pit. The fluid level in the pit is 7-8 below the tear in the liner and is not an issue at this time. The silt fence was inspected and no off site sedimentation was found. The location is dry and the gate at the access road is locked. I found no violations at this time.
1298603826 2017-05-09 Urban Drill / Deepen / Reopen No Violations
1343619959 2017-08-24 Urban Drill / Deepen / Reopen No Violations
1424715224 2017-06-15 Drill / Deepen / Reopen No Violations
1493128091 2017-04-13 Drill / Deepen / Reopen No Violations

-round container.

1493214704 2017-04-25 Drill / Deepen / Reopen No Violations I was on location to witness the Blowout Prevention Test (BOP) for the surface casing. HAD Drilling applied 435 psi on the surface casing at 8:07 pm. After 15 minutes, the pressure held static at 435 psi. Test passed.
1493385026 2017-04-27 Drill / Deepen / Reopen No Violations
1494872209 2017-05-11 Drill / Deepen / Reopen No Violations I was on location to assess complaint #5605. I investigated and found no evidence of dumping into Crab Creek or the pond. Photos were taken and are available upon request. PAC has a pump and 4 flexible hose running down the hill side to pull fresh water for drilling and cementing operations. I spoke with Jody Stoyak, Liberty Township Trustee, and informed her of my findings.
1497278128 2017-05-26 Drill / Deepen / Reopen No Violations
1498051874 2017-06-20 Drill / Deepen / Reopen No Violations

-

PAC Drilling has defective casing above the plug. PAC Drilling will submit a detailed plan for repairing the defective casing to ODNR Inspector Rick Skidmore for approval.

1498225281 2017-06-20 Urban Drill / Deepen / Reopen No Violations

-

PAC Drilling has defective casing above the plug. PAC Drilling will submit a written detailed plan for repairing the defective casing to ODNR Inspector Rick Skidmore for approval.

1498651129 2017-06-27 Urban Drill / Deepen / Reopen No Violations
1499276780 2017-06-29 Urban Drill / Deepen / Reopen No Violations

-

1499953272 2017-07-12 Urban Drill / Deepen / Reopen No Violations I was on location to check the status of the casing repairs. The service rig was removing the 2.375 work string with a dressing mill attached after cleaning up the casing stump. No violations noted.
1500651944 2017-07-14 Drill / Deepen / Reopen No Violations I was on location to witness the pressure testing of the 4.5 11.6 lb/ft P-10 production casing. Contractors on location were Ohio Valley Energy Service Rig, O-Nine Down Hole Tools and Great Lakes Wellhead Testing ( GLWT ). The flanged wellhead was removed and Great Lakes Wellhead installed their flanged casing head. The line to the well was installed, meter recorder and lines were installed. GLWT build the pressure up slow and bleeding the air out of the lines. The pressure was taken to 7500 psi. and held for 30 minutes, there was a 150 psi pressure drop. Teat passed
1505399231 2017-09-13 Urban Drill / Deepen / Reopen No Violations I found Reliance Well Service and Sure Fire Wireline on location to perform well stimulation operations for PAC Drilling. Reliance pumped 500 gallons of 7.5% HCL for Stage 3 on Friday, September 8, 2017. Reliance started stimulation of Stage 3. The Stage reached 7,000 psi and PAC decided to shut down and pump an additional 500 gallons of 15% HCL. PAC waited 7 minutes then Reliance restarted stimulation operations.
1505482486 2017-09-14 Urban Drill / Deepen / Reopen No Violations I was on location to witness Reliance Well Service and SureFire Wireline stimulate the well for PAC Drilling. Upon arrival, Reliance was completing stage 5. Reliance completed stages 6 & 7 while I was on location. Each stage consisted of 50 shots. PAC Drilling used 500 gallons of 7.5% HCL after each stage perforation.
1507296077 2017-10-06 Urban Drill / Deepen / Reopen No Violations I found no change since the last inspection. PAC Drilling is still working on building the tank battery. The well site is secure with a locked gate at the access road entrance.
1507648646 2017-10-10 Urban Drill / Deepen / Reopen No Violations

-9-5. Two sides of the dike remain unbuilt. There is an identification sign on the gate at the access road entrance.

1507813766 2017-10-12 Urban Drill / Deepen / Reopen No Violations I found no change since the last inspection. The access road is secure with a locked gate and an identification sign is posted.
1508162704 2017-10-16 Urban Drill / Deepen / Reopen No Violations I found PAC Drilling still working on the construction of the tank battery. The 12 frac tanks are still on location.
1512140846 2017-12-01 UrbanPreliminary Restoration No Violations The well and tank battery was accessed through a gate and on a gravel driveway. The well was completed as a electric pumping well. I observed a dozer operator moving the topsoil to re-establish grade of the drill site. The wellhead had annular risers, which were partially opened and without any flow. The required pop off valves, for the annular risers, were not installed at the time of this inspection. The location had non-essential materials on the south side of the location, which will require removal. The tank battery was under construction. The equipment present was two (2) 210 barrel stock tanks, one (1) 140 brine tank and one 2410 horizontal separator. The equipment spacing requirements were compliant. The tank battery was surrounded with an earthen dike. A gas sales line, comprised of 2.375 upset pipe was laid to the tank battery. The preliminary restoration designation was not granted.
1514437142 2017-08-28 Urban Drill / Deepen / Reopen No Violations
1519861872 2017-12-18 UrbanProduction Wells No Violations I found PAC still working on building the tank battery and the preliminary restoration. The top soil stockpiles leveled and graded. A pumping unit has been installed onto the wellhead. Fence poles have been installed around the pumping unit. Seed has not been spread due to the winter weather. There is no urban safety equipment on the two (2) storage tanks at this time. I spoke with Jeremy Caldwell on location. Mr. Caldwell stated he was still working on the plumbing at the tank battery and electric at the pumping unit.
1529829522 2017-09-14 Completion Testing No Violations I was on location to assist Rick Skidmore in the monitoring of the stimulation of the P A C # 1H well. Reliance Well Service was the frac contractor and SureFire was the wireline ( plug and perf ) contractor. I observed stage # 6. Formation breakdown was 5450 psi. the stage treated at an average of 6200 psi at 24 barrels per minute. Total stage volume was 1400 barrels of fluid. No violations were identified during this inspection.
1636024880 2017-08-16 Urban Drill / Deepen / Reopen No Violations I found the well still shut-in on the day of my inspection. There are 12 Frac tanks still on location. The pit is open and surrounded by orange safety fencing. I called Jason and Justin Caldwell and left messages for a return call concerning the status of the well.
1706054514 2017-11-07 Urban Drill / Deepen / Reopen No Violations
1754423120 2017-05-01 Urban Drill / Deepen / Reopen No Violations
1780475795 2017-10-23 Urban Drill / Deepen / Reopen No Violations I found no one on location on the day of my inspection. There is a swab rig on location. The tank battery is still in the process of being built.
1817745461 2017-05-08 Urban Drill / Deepen / Reopen No Violations
1834271336 2017-06-01 Drill / Deepen / Reopen No Violations I conducted an inspection on this site. The well was being prepared to be perforated. Sediment and erosion controls on site needed some maintenance. Silt fence along the southwest corner needed to be installed accordingly. I contacted Jason Caldwell from PAC Drilling, Inc. about entrenching the silt fence along the boundary between the southwest to west area of the site. Signage at the entrance to the site was good and the access was stable. No other violations observed.
1907244576 2017-09-07 Urban Drill / Deepen / Reopen No Violations I found Jeremy Caldwell from PAC Drilling on location working on closing the pit. Carmeuse Lime and Stone delivered 78,740 pounds of Calciment.
1948455486 2017-10-19 Urban Drill / Deepen / Reopen No Violations I found Diamond Well Service on location swabbing the well for PAC Drilling. The 12 frac tanks are still on location. The access road is in good repair.
2054160082 2019-02-25 UrbanProduction Wells No Violations I conducted a compliance notice follow-up inspection for com-pliance notice 555854563, regarding multiple violations related to urban requirements that needed addressed at this well site location. At the time of this inspection, the lease access had a locked gate installed with required urban identification posted on the gate. The tank battery had the fencing installed around the production equipment and two man doors were installed and locked. The tank valves and pickup lines on the production tanks were all locked. The eastern most 210 BBL tank and 100 BBL brine tank still needed plugs in the two inch bungs on the top of the tanks installed. The dike surrounding the tank battery had been stabilized with vegetation. The west side of the tank battery fencing had green, privacy slats installed, but not on any other side of the fence. The non-essential items in and around the well and tank battery have been removed from the location. The well was fenced, with green privacy slats installed in the fencing. The gaps in the fence have been remedied and both areas of access to the well had locks. The stuffing box and tubing head were cleaned up and no longer covered in grease and oil. The cellar has been filled with stone and at the time of this inspection no oil or fluid was present. Pop-off valves have been installed on the 2 inch riser pipes plumbed off the annular space between the intermediate casing string and the production casing string, but pressure gauges were still needed. Legible identification with the required information per OAC 1501:9-9-05E(a-i) has been installed at the well and tank battery locations. Landscaping has been installed along the east and south sides of the fenced well location, however some areas at the well location still need established vegetation.

PAC needs to: 1) Place plugs into outlets on the top of the tank and place locks on the load lines (OAC 1501-9-9-05 E( 3 & 4 ) 2) Place gauges on all annular risers (OAC 1501

450145374 2017-5-10 0:00: DD No Violations 1.60
514613019 2017-4-10 0:00: DD No Violations 1.50
700380224 2017-4-25 0:00: UP No Violations 4.00
753872920 2017-9-18 0:00: UP No Violations
826787526 2017-6-23 0:00: UD No Violations 6.00
902130929 2017-5-15 0:00: DD No Violations 8.00
91257042 2017-4-14 0:00: DD No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0555854563 US-OH-126121 2018-05-25 9-05E1 ID (a-i)
0555854563 US-OH-126122 2018-05-25 9-05E2 FENCING (a-d)
0555854563 US-OH-126123 2018-05-25 9-05E3 LOCKS
0555854563 US-OH-126124 2018-05-25 9-05E4 TANKS (a-I)
0555854563 US-OH-126125 2018-05-25 9-05E5 OPERATIONMAINTANCE (a-c)
0555854563 US-OH-126126 2018-05-25 9-05E6 LANDSCAPING (a-c)
0555854563 US-OH-126127 2018-05-25 NONEC Failure to restore land surface within 9 mos.

For data sources see[8]

References