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Well ID: 34-157-21252 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Warwick Township | |
Operator Name: WILLISTON OIL CORP | |
Well Pad ID: | |
Farm/Lease Name: LICHTI RALPH H | |
License Status: Final Restoration | |
License Date: 1979-08-24 | |
Spud Date: 1970-08-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-10-13 | |
Well Total Depth: 970.00 ft | |
Configuration: Vertical | |
Latitude: 40.400000 | |
Longitude: -81.420000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1970-08-21 | REFERRED TO FIELD 4/26/06 FOR ORPHAN WELL REFERRAL. IPN GAS FOUND IN NSR. Orphan Well Case # 2014 07 008 |
Completed | 1970-10-13 | REFERRED TO FIELD 4/26/06 FOR ORPHAN WELL REFERRAL. IPN GAS FOUND IN NSR. Orphan Well Case # 2014 07 008 |
Reached Total Depth | 1970-10-13 | REFERRED TO FIELD 4/26/06 FOR ORPHAN WELL REFERRAL. IPN GAS FOUND IN NSR. Orphan Well Case # 2014 07 008 |
Completion Report Received | 1972-04-23 | REFERRED TO FIELD 4/26/06 FOR ORPHAN WELL REFERRAL. IPN GAS FOUND IN NSR. Orphan Well Case # 2014 07 008 |
CO | 1979-08-24 | 90 WILLISTON OIL CORP GeoDate 8/24/79 |
Plugged by Orphan Well Program | 2016-03-22 | Plugged by Orphan Well Program |
Plugged/Abandoned | 2016-03-22 | REFERRED TO FIELD 4/26/06 FOR ORPHAN WELL REFERRAL. IPN GAS FOUND IN NSR. Orphan Well Case # 2014 07 008 |
Record Last Modified | 2016-08-30 | REFERRED TO FIELD 4/26/06 FOR ORPHAN WELL REFERRAL. IPN GAS FOUND IN NSR. Orphan Well Case # 2014 07 008 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 924 | 930 | 21 |
924 | 930 | 21 | |
924 | 930 | 21 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | GAUGED ABOUT 76 MCFG, 390# ROCKS ABOUT 10# PER MIN. FIRST 3 MINS. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | SPARTA ENERGY CORP | 2549.00 | 0.00 | 0 |
1985 | SPARTA ENERGY CORP | 4511.00 | 0.00 | 330 |
1986 | APPALACHIAN EXPL INC | 8150.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | SPARTA ENERGY CORP | Brine | 0 | 0 |
1985 | SPARTA ENERGY CORP | Brine | 0 | 330 |
1986 | APPALACHIAN EXPL INC | Brine | 7 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1109810540 | 2015-10-7 0:00: | OR | No Violations | 4.00 |
-1810421844 | 2016-3-21 0:00: | PB | No Violations | 8.00 |
-603359174 | 2014-4-11 0:00: | PW | No Violations | |
-623432411 | 2016-3-16 0:00: | PB | No Violations | 2.00 |
-871203634 | 2016-3-21 0:00: | PB | No Violations | 8.00 |
0336321952 | 2016-03-17 | Plug / Plug Back | No Violations | Removing parted tubing from well. |
0506231508 | 2016-03-14 | Orphan | No Violations | On site to contact landowner and show location to Jason Nicholas (NWP) plugging contractor. |
0603359174 | 2014-04-11 | Production Wells | No Violations | This well is not producing. There is a hole in the 7 casing on the N side. The tubing is holed as well. The landowner saw the well flow saltwater when he was plowing his field. The well flows gas and brine at unpredictable intervals. There is a 6x3 puddle of briny water on the N side of the well. This is a Berea well. The owner is defunct. An orphan well complaint and matrix was filled out on this well and this information was turned over to the acting Tuscarawas County inspector for follow-up. |
0623432411 | 2016-03-16 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig crew preparing to weld a piece of 3 inch tubing on and also weld a 7 inch wellhead on to the 7 inch casing. The 7 inch casing has some water flow to it. An earthen pit was dug to help control the water long enough to complete the welding. |
0685835319 | 2016-03-22 | Plug / Plug Back | No Violations | Topped off casing. Cut casing 48 below grade. Rigged down, moving off locatio. |
0841900585 | 2015-12-02 | Orphan | No Violations | Check site to determine crop removal and land conditions. |
0871203634 | 2016-03-21 | Plug / Plug Back | No Violations | Shot casing, set rip plug, set surface plug. |
1109810540 | 2015-10-07 | Orphan | No Violations | Conducted pre-plug site inspection. Site conditions are acceptable for equipment mobilization and setup. |
1397831656 | 2014-04-15 | Production Wells | No Violations | On the day of my inspection I was accompanied by District Supervisor Brent Bear. Arriving on location we found the well idle. The well has severe corrosion to the casing and the tubing, pieces of the casing and tubing are missing. While on location the well blew saltwater out and on to the ground, an area of about 3 foot by 5 foot was impacted. The well is not equiped to control the flow of gas or fluids. Quantab high range were used to test for chlorides, the test was stopped at 7.8 units or 3420 ppm chlorides. This inspection is the follow up for complaint # 4657. Well needs to be plugged. |
1403807415 | 2014-06-04 | Orphan | No Violations
Since the field was recently planted in soybeans, Mr. Rummell requested that the well be plugged after he has harvested the soybeans. A right of entry has been obtained from the adjoining property to the south of the Rummel property and the well will be accessed off of Mud Run Road. The access road will be along the western edge of this property and then northeast across the Rummel property to the well. | |
1458237260 | 2016-03-17 | Plug / Plug Back | No Violations | |
1458839163 | 2016-03-16 | Plug / Plug Back | No Violations | Service rig and equipment moving onto location. |
1463063447 | 2016-05-12 | Final Restoration | No Violations | Appears to meet all requirements for final reclamation. |
1463411515 | 2016-05-16 | Final Restoration | No Violations | On the day of my inspection I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B). |
1810421844 | 2016-03-21 | Plug / Plug Back | No Violations | This well plugged and abandoned this date. See plug report for details. |
1999877409 | 2016-03-18 | Plug / Plug Back | No Violations | Set bottom plug. See plug report for details. |
336321952 | 2016-3-17 0:00: | PB | No Violations | 8.00 |
506231508 | 2016-3-14 0:00: | OR | No Violations | 4.00 |
685835319 | 2016-3-22 0:00: | PB | No Violations | 8.00 |
841900585 | 2015-12-2 0:00: | OR | No Violations | 3.00 |
For data sources see[9]