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Well ID: 34-157-21537 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Sugar Creek Township | |
Operator Name: SHETLER DAVID I & MARY M | |
Well Pad ID: | |
Farm/Lease Name: SHETLER SI & I E | |
License Status: Domestic Well | |
License Date: 1972-09-08 | |
Spud Date: 1972-10-23 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-09-21 | |
Well Total Depth: 4452.00 ft | |
Configuration: Vertical | |
Latitude: 40.520000 | |
Longitude: -81.660000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1972-09-08 | 139 MB OPERATING CO INC GeoDate 9/8/72 |
Original Spud | 1972-10-23 | RE-ISSUED 9-13-72. CHANGED STATUS FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 2/3/2016 CM. |
Completed | 1973-09-21 | RE-ISSUED 9-13-72. CHANGED STATUS FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 2/3/2016 CM. |
Reached Total Depth | 1973-09-21 | RE-ISSUED 9-13-72. CHANGED STATUS FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 2/3/2016 CM. |
Change of Owner | 2000-06-30 | Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2016-02-03 | Operator changed from 7578, ENERVEST OPERATING LLC to 9627, SHETLER DAVID I & MARY M |
Record Last Modified | 2016-02-03 | RE-ISSUED 9-13-72. CHANGED STATUS FROM PR TO DM PER TRANSFER FROM ENERVEST OPERATING LLC #7578 TO OWNER ON 2/3/2016 CM. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4230 | 4339 | 0 |
4230 | 4339 | 0 | |
4230 | 4339 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 88000 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RESOURCE AMERICA INC | 2519.00 | 0.00 | 365 |
1985 | RESOURCE AMERICA INC | 2758.00 | 0.00 | 365 |
1987 | RESOURCE AMERICA INC | 2145.00 | 0.00 | 365 |
1988 | MB OPERATING CO INC | 213.00 | 0.00 | 366 |
1989 | MB OPERATING CO INC | 2151.00 | 0.00 | 365 |
1990 | MB OPERATING CO INC | 1772.00 | 0.00 | 365 |
1991 | MB OPERATING CO INC | 2064.00 | 0.00 | 365 |
1992 | MB OPERATING CO INC | 1789.00 | 0.00 | 366 |
1993 | MB OPERATING CO INC | 1978.00 | 0.00 | 365 |
1994 | MB OPERATING CO INC | 1699.00 | 0.00 | 365 |
1995 | MB OPERATING CO INC | 790.00 | 0.00 | 365 |
1996 | MB OPERATING CO INC | 1382.00 | 0.00 | 366 |
1997 | MB OPERATING CO INC | 1316.00 | 0.00 | 365 |
1998 | MB OPERATING CO INC | 1169.00 | 0.00 | 365 |
1999 | MB OPERATING CO INC | 0.00 | 0.00 | 273 |
2000 | RANGE RESOURCES-APPALACHIA LLC | 852.00 | 0.00 | 365 |
2001 | RANGE RESOURCES-APPALACHIA LLC | 40.00 | 0.00 | 31 |
2004 | RANGE RESOURCES-APPALACHIA LLC | 210.00 | 0.00 | 306 |
2005 | RANGE RESOURCES-APPALACHIA LLC | 150.00 | 0.00 | 275 |
2006 | RANGE RESOURCES-APPALACHIA LLC | 162.00 | 48.00 | 275 |
2007 | RANGE RESOURCES-APPALACHIA LLC | 91.00 | 0.00 | 61 |
2009 | RANGE RESOURCES-APPALACHIA LLC | 24.00 | 0.00 | 31 |
2010 | ENERVEST OPERATING LLC | 166.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 103.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 33 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1221484561 | 2016-1-21 0:00: | EX | No Violations | 1.00 |
1221484561 | 2016-01-21 | Exempt Well Pre Transfer | No Violations | On the day of my inspection I found an 8 X 4 wellhead with a 4 inch valve, with a 4 X 2 swage in the top. The valve was in the closed position. There is a horizontal separator and a 210 bbl. Tank. The last year for reporting production was 2011. I received a phone call from Troy Well with EnerVest, stating that the gas leak has been repaired. Upon arrival on the location I found that repairs have been completed, and there are no signs of leakage at this time. The property owner is using domestic gas. |
1234438340 | 2015-12-21 | Exempt Well Pre Transfer | No Violations | On the day of my inspection I found an 8 X 4 wellhead with a 4 inch valve, with a 4 X 2 swage in the top. The valve was open. There is a gas leak at the wellhead. There is a separator and a 210 bbl tank the tank identification is not legible. The last year for reporting production was 2011. I talked to Troy Walls with Entervest and they will check out there gas leak. I refer to my inspection of 03/09/2015, as the leak has not been fixed. The property owner is using domestic gas. |
1425911224 | 2015-03-09 | Production Wells | No Violations | On the day of my inspection I found an 8 X 4 wellhead with a 4 inch valve, with a 4 X 2 swage in the top. The valve was open. There is a gas leak at the wellhead. In talking with the landowner in the summer months you can smell the gas at the house. There is a separator and a 210 bbl tank the tank Identification is not legible. The last year for reporting production was 2011. I talked to Troy Walls with Entervest and They will replace ID and check out there gas leak. |
For data sources see[9]