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34-157-21911

Well Details

Well ID: 34-157-21911
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Warren Township
Operator Name: ECO PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: DUTTON HATTIE
License Status: Final Restoration
License Date: 2016-02-03
Spud Date: 1973-04-04
Spud Drilling Contractor:
Final Drill Date: 1973-06-05
Well Total Depth: 5350.00 ft
Configuration: Vertical
Latitude: 40.500000
Longitude: -81.310000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1973-03-23 1383 OHIO L & M CO INC GeoDate 3/23/73
Original Spud 1973-04-04 REV. LOC. 4-4-73
Completed 1973-06-05 REV. LOC. 4-4-73
Reached Total Depth 1973-06-05 REV. LOC. 4-4-73
CO 1989-10-20 1383 OHIO L & M CO INC GeoDate 10/20/89
Unknown 1989-10-20 Issued Date 10/20/89 Expired Date 10/20/90 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 2013-11-13 Operator changed from 6288, ALLIANCE PETROLEUM CORPORATION to 201, GREEN GAS CO
APP 2016-02-03 Proposed Formations:CLINTON, Issued Date:2/3/2016, Expired Date:2/2/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-06-17 REV. LOC. 4-4-73
Change of Owner 2017-12-08 Operator changed from 201, GREEN GAS CO to 10021, ECO PRODUCTION LLC
Record Last Modified 2017-12-08 REV. LOC. 4-4-73
Construction Permit Expires 2018-02-02 REV. LOC. 4-4-73

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5191 5197 0
5191 5197 0
5191 5197 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2981 Bbl 40000
ACID 15 250 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OHIO L & M CO INC 2864.00 124.00 0
1985 L & M PETROLEUM CO 59.00 0.00 0
1986 L & M PETROLEUM CO 7.00 0.00 365
1987 L & M PETROLEUM CO 3.00 110.00 365
1990 OHIO L & M CO INC 17.00 0.00 365
1991 OHIO L & M CO INC 4.00 0.00 365
1993 OHIO L & M CO INC 294.00 0.00 365
2010 ALLIANCE PETROLEUM CORPORATION 410.00 0.00 365
2011 ALLIANCE PETROLEUM CORPORATION 0.00 0.00 365
2012 ALLIANCE PETROLEUM CORPORATION 0.00 0.00 366
2013 ALLIANCE PETROLEUM CORPORATION 0.00 0.00 273
2014 GREEN GAS CO 0.00 0.00 0
2016 GREEN GAS CO 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OHIO L & M CO INC Brine 0 0
1985 L & M PETROLEUM CO Brine 54 0
1986 L & M PETROLEUM CO Brine 0 365
1987 L & M PETROLEUM CO Brine 180 365
1990 OHIO L & M CO INC Brine 0 365
1991 OHIO L & M CO INC Brine 0 365
1993 OHIO L & M CO INC Brine 0 365
2010 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2011 ALLIANCE PETROLEUM CORPORATION Brine 0 365
2012 ALLIANCE PETROLEUM CORPORATION Brine 0 366
2013 ALLIANCE PETROLEUM CORPORATION Brine 0 273
2014 GREEN GAS CO Brine 0 0
2016 GREEN GAS CO Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1312704026 2016-5-11 0:00: PW No Violations 1.00
0044802321 2016-01-15 Administrative Inspection No Violations I received a letter from John Davis with Green Gas, stating a new timeline for working on the well. He stated they will clean up the location by April 1, 2016, and complete the plugging before June 9, 2016. I place a phone call to John Davis and let him know that his timeline is acceptable.
0890398584 2015-12-10 Production Wells Violations Noted I received a call from Kyle and Denise Dalcoma to do an inspection of the well on their property. I found that the trees and brush has grown over the top of the pump unit, and it appears that the well has not been produced for some time. The electric motor to operate the pumping unit has been removed and the horse head bridle is not hooked up. The valve were in the off position. Records indicate that 2010 was the last year for production, and there is no reported production for 2014. The owner/operator shall submit a written plugging schedule to Inspector Randy Akins at 2207 Reiser Ave. New Philadelphia, Ohio, 44663 within 30 day, per OAC 1501:9-11-05(B), and plug the well within 180 days. The owner/operator will be notified if the plugging schedule is approved or denied.
1026700376 2016-06-14 Production Wells No Violations Upon arrival on location I found that the crew is preparing for the service rig. The brush has been removed, and Thompson Well service is moving on location on June 15, 2016 To plug the well.
1059511873 2015-11-13 Production Wells No Violations I received a request form Kyle and Denise Dalcoma for an inspection of the well. On the day of my inspection I found a 4 X 2 inch wellhead with 2 inch tubing and rods. Operated by a pump jack. There is no motor to run the pump jack and the bridle cable is broken and is not connected to the horse head. The valves are in the closed position. There has not been any production scene 2010.
1312704026 2016-05-11 Production Wells No Violations This is a follow up inspection to an NOV issued on 12/11/2015 There has been no change in the status of the well. It is still idle and the valves are in the closed position. Green Gas has agreed to start site prep in April of 2016, and complete plugging by June 2016. At this time Green gas has not started to clean up the well location at this time.
1452086614 2016-01-06 Administrative Inspection No Violations I phone John Davis and advised him that his letter of 12/29/2015 was not approved, and that he need to re-submit a timeline that completed the plugging by the 180 day period, ending on 06/09/2016
1466000979 2016-06-15 Plug / Plug Back No Violations Upon arrival on location I found that Thompson well service has moved in on location and are preparing to plug the well. They are pulling the rods getting ready to set the bottom plug.
1466082086 2016-06-16 Plug / Plug Back No Violations Upon arrival on location I found the rig crew ready to set the bottom plug from 5207 to 4800 feet with 30 sacks of class A with 2 % Gel. The 2 3/8 inch tubing is being removed from the wellbore.
1466101067 2016-06-16 Plug / Plug Back No Violations Arrive on site today with Inspector Akins and Scheiner to begin plugging this well. Thompson Well Service has 2 3/8 inch diameter tubing at 5240 ft. to set the bottom plug. Petroset Cementing Service set the first plug at 5240 ft. to 5040 ft. with 30 sacks of class A cement at 14.8 lb. and a yield of 1.26 After setting the bottom plug Thompson Well Service will pull all of the tubing out of the well. They will go back inside the 4 1/2 inch diameter casing and try to rip beginning at 4900 ft. and look for a telegraph. They plan to have the tubing out and the casing ripped so they can be ready to continue plugging at 7:30 AM Friday morning.
1466184967 2016-06-17 Plug / Plug Back No Violations
1466433268 2016-06-20 Plug / Plug Back No Violations On the day of my inspection I found the rig crew has reclaimed the location. The 8 5/8 inch casing has been cut off and the pit has been filled in. The location is ready for seeding and mulching. The NOV has been completed and ready to close.
1479316779 2016-11-16 Final Restoration No Violations On the day of my inspection, I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B).
44802321 2016-1-15 0:00: AM No Violations 0.50
890398584 2015-12-10 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0890398584 US-OH-130168 2016-11-25 General Safety
0890398584 US-OH-130169 2016-11-25 Well shall be plugged

For data sources see[9]

References