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Well ID: 34-157-22345 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Goshen Township | |
Operator Name: AIM ENERGY LLC | |
Well Pad ID: | |
Farm/Lease Name: LEGGETT GEORGE RAY | |
License Status: Producing | |
License Date: 1990-07-24 | |
Spud Date: 1974-08-14 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-08-20 | |
Well Total Depth: 5045.00 ft | |
Configuration: Vertical | |
Latitude: 40.490000 | |
Longitude: -81.410000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1974-06-26 | 18 MUTUAL OIL & GAS CO GeoDate 6/26/74 |
Original Spud | 1974-08-14 | |
Completed | 1974-08-20 | |
Reached Total Depth | 1974-08-20 | |
CO | 1990-07-24 | 18 MUTUAL OIL & GAS CO GeoDate 7/24/90 |
Unknown | 1990-07-24 | Issued Date 7/24/90 Expired Date 7/24/91 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1991-07-24 | |
CO | 1993-08-06 | 4468 DIETZ OIL FIELD SUPPLY GeoDate 7/24/90 |
Change of Owner | 1997-09-09 | Operator changed from 4468, DIETZ OIL FIELD SUPPLY to 2543, TIPKA ENERGY DEVLOP CO |
Change of Owner | 2016-03-02 | Operator changed from 2543, TIPKA ENERGY DEVLOP CO to 8175, AIM ENERGY LLC |
Record Last Modified | 2016-03-02 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4869 | 4896 | 15 |
4869 | 4896 | 15 | |
4869 | 4896 | 15 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 114750 | 0 | N2 SCF | ||
H2O | 0 | 1350 Bbl | 42500 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MUTUAL OIL & GAS CO | 9596.00 | 6690.00 | 0 |
1985 | MUTUAL OIL & GAS CO | 8668.00 | 61.00 | 0 |
1986 | MUTUAL OIL & GAS CO | 7603.00 | 59.00 | 365 |
1987 | MUTUAL OIL & GAS CO | 6900.00 | 54.00 | 365 |
1988 | MUTUAL OIL & GAS CO | 4403.00 | 47.00 | 365 |
1989 | MUTUAL OIL & GAS CO | 2991.00 | 0.00 | 365 |
1990 | MUTUAL OIL & GAS CO | 3288.00 | 61.00 | 365 |
1991 | MUTUAL OIL & GAS CO | 2973.00 | 0.00 | 365 |
1992 | MUTUAL OIL & GAS CO | 2694.00 | 53.00 | 365 |
1993 | MUTUAL OIL & GAS CO | 1176.00 | 0.00 | 365 |
1995 | DIETZ OIL FIELD SUPPLY | 2319.00 | 61.00 | 365 |
1996 | DIETZ OIL FIELD SUPPLY | 1930.00 | 33.00 | 365 |
1997 | TIPKA ENERGY DEVLOPMENT COMPAN | 117.00 | 0.00 | 0 |
1998 | TIPKA ENERGY DEVLOPMENT COMPAN | 1696.00 | 0.00 | 0 |
1999 | TIPKA ENERGY DEVLOPMENT COMPAN | 803.00 | 44.00 | 0 |
2000 | TIPKA ENERGY DEVLOPMENT COMPAN | 755.00 | 37.00 | 0 |
2001 | TIPKA ENERGY DEVLOPMENT COMPAN | 926.00 | 0.00 | 365 |
2002 | TIPKA ENERGY DEVLOPMENT COMPAN | 1141.00 | 0.00 | 365 |
2003 | TIPKA ENERGY DEVLOPMENT COMPAN | 1490.00 | 0.00 | 365 |
2004 | TIPKA ENERGY DEVLOPMENT COMPAN | 1650.00 | 62.00 | 366 |
2005 | TIPKA ENERGY DEVLOPMENT COMPAN | 1662.00 | 0.00 | 365 |
2006 | TIPKA ENERGY DEVLOPMENT COMPAN | 906.00 | 0.00 | 365 |
2007 | TIPKA ENERGY DEVLOPMENT COMPAN | 1227.00 | 0.00 | 365 |
2008 | TIPKA ENERGY DEVLOPMENT COMPAN | 1703.00 | 12.00 | 366 |
2009 | TIPKA ENERGY DEVLOPMENT COMPAN | 2031.00 | 0.00 | 365 |
2010 | TIPKA ENERGY DEVLOPMENT COMPAN | 1585.00 | 51.00 | 365 |
2011 | TIPKA ENERGY DEVLOPMENT COMPAN | 1278.00 | 0.00 | 0 |
2012 | TIPKA ENERGY DEVLOPMENT COMPAN | 1241.00 | 0.00 | 366 |
2013 | TIPKA ENERGY DEVLOPMENT COMPAN | 946.00 | 13.00 | 365 |
2014 | TIPKA ENERGY DEVLOPMENT COMPAN | 390.00 | 0.00 | 273 |
2015 | AIM ENERGY LLC | 1286.00 | 0.00 | 365 |
2016 | AIM ENERGY LLC | 1869.00 | 0.00 | 365 |
2017 | AIM ENERGY LLC | 1771.00 | 0.00 | 365 |
2018 | AIM ENERGY LLC | 1328.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2125154627 | 2014-5-5 0:00:0 | PW | No Violations | 1.50 |
-806704651 | 2013-4-13 0:00: | PW | No Violations | 3.00 |
0000000286 | 2002-08-10 | Production Wells | No Violations | no violations |
001252i286 | 2002-08-10 | Production Wells | No Violations | no violations |
0806704651 | 2013-04-13 | Production Wells | Violations Noted | I arrived on location and found crew working on clean-up. Oil soaked absorbent pads from dike area are being collected and placed into plastic trash bags to be sent to landfill. Dams are working well and oil was sucked off with vaccum truck. The oil in lease road ditch has been removed and there is no oil to be found in Beaver dam creek at this time. |
1252i286 | 2002-8-10 0:00: | PW | No Violations | |
1366122052 | 2013-04-12 | Production Wells | No Violations | I received a call from OEPA Michael Sherron advising of a oil spill that occurred between 04/10/13 and 04/11/13, A hole rusted through bottom of tank letting approximately 30 barrels of fluid escape. The fluid soaked through the bottom of the dike and into a ditch that runs beside the lease rd it then went through a rd culvert and into Beaver dam creek. OEPA advised and helped set plywood dams in ditch to collect oil to be sucked out with a vaccum truck. Absorbent pads being placed on top of oil in ditch and inside dike. I advised company to keep clean-up on going until done. |
1385559876 | 2013-04-16 | Production Wells | No Violations | I arrived on location and found all oil has been removed and violation has been corrected. This case can be closed, 04/16/13 |
1398265871 | 2014-04-22 | Production Wells | No Violations | On the day of my inspection I found the well to be producing with a plunger lift system. I found 1-100 bbl. tank in an earthen dike. The tank was not properly identified. I call Tipka Energy and advised them to properly identify their tank. |
2125154627 | 2014-05-05 | Production Wells | No Violations | On the day of my inspection following up on NOV-806704651, I witnessed that the well was capable of production and equipped with 2.875 inch casing, 1.5 inch tubing and a plunger lift system with valves open on the tubing. Production equipment included a 100bbl tank which is shared with the Legett #3 34157224710000, a vertical separator, a drip, a 2 inch sales meter with a 1 inch orifice and a chart recorder. Identification was present and production records are current. Compliance issue has been resolved. |
286 | 2002-8-10 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0806704651 | US-OH-129165 | 2013-04-16 | No SPCC dike/or failure to keep dike free of water or oil | |
0806704651 | US-OH-129166 | 2013-04-16 | Dike or pit not able to prevent escape of brine or other wastes |
For data sources see[9]