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Well ID: 34-157-22948 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: York Township | |
Operator Name: BOWER OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: MUTCHLER | |
License Status: Producing | |
License Date: 2012-05-15 | |
Spud Date: 1977-08-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-10-07 | |
Well Total Depth: 4878.00 ft | |
Configuration: Vertical | |
Latitude: 40.470000 | |
Longitude: -81.540000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1977-08-20 | |
Completed | 1977-10-07 | |
Reached Total Depth | 1977-10-07 | |
APP | 2012-05-15 | Proposed Formations:, Issued Date:5/15/2012, Expired Date:5/15/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2014-05-15 | |
Record Last Modified | 2019-06-14 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4660 | 4732 | 1 |
4660 | 4732 | 1 | |
4660 | 4732 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2150 Bbl | 70000 |
For data sources see[4]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1987 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1988 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1989 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1990 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 365 |
1991 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 365 |
1992 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 365 |
1993 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1994 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1995 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
1996 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2010 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 240 | 0 |
2011 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2012 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2013 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2014 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2015 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2016 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2017 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
2018 | HI SNYDER/SNYDER OIL & GAS INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1782606499 | 2020-5-4 0:00:0 | PW | No Violations | 1.50 |
-21484453 | 2019-4-11 0:00: | PW | No Violations | 0.50 |
-819903956 | 2018-9-13 0:00: | PW | No Violations | 1.00 |
-931530685 | 2014-5-13 0:00: | PW | No Violations | 2.50 |
0021484453 | 2019-04-11 | Production Wells | No Violations | This inspection was a follow up to a compliance notice number 133172770, issued on 3/13/12 by ODNR Inspector Barry Grimm. Upon arrival on location, I witnessed the well was still shut in. The well was equipped with 4.5 inch diameter casing swaged down to a 2 inch diameter valve. The valve was closed, and this is a swab well. The production equipment included a steel 210 tank and a horizonal separator. The tank was inside an earthen dike. The location, the inside of the earthen dike, and around the well was all grown up with vegetation. Production report is up to date, but the well has not produced since 1986. The well needs to be plugged. Placed a phone call to Ann Walkins, the secretary of the company. She would have someone get back with me on this issue. |
0578922078 | 2016-05-06 | Production Wells | No Violations | On the day of my inspection I followed up on NOV- |
0819903956 | 2018-09-13 | Production Wells | No Violations | This inspection was a follow up to a compliance notice number 133172770, issued on 3/13/12 by ODNR Inspector Barry Grimm. Upon arrival on location, I witnessed the well was still shut in. The well was equipped with 4.5 inch diameter casing swaged down to a 2 inch diameter valve. The valve was closed, and this is a swab well. The production equipment included a steel 210 tank and a horizonal separator. The tank was inside an earthen dike. The location, the inside of the earthen dike, and around the well was all grown up with vegetation. Production report is up to date, but the well has not produced since 1986. The well needs to be plugged. |
0931530685 | 2014-05-13 | Production Wells | No Violations | On the day of my inspection following up on NOV-133172970, I witnessed that the well was equipped with 8.625 inch casing, 4.5 inch casing reduced to 2 inches with all valves closed at the well. Production equipment included a 210bbl tank and a 100bbl tank. I made call to Operator of the well and advised that I needed an update on their plans for the well. |
1208647540 | 2020-8-10 0:00: | PW | No Violations | 1.00 |
1331729770 | 2012-03-13 | Production Wells | Violations Noted | arrived on location and found well idle , no production has been reported since 1986 this well needs to be plugged. This well is not economically feasible to operate. Within 30 days apply for a plug permit and plug well. |
1620812369 | 2017-08-09 | Production Wells | No Violations | On the day of my inspection I followed up on NOV- |
578922078 | 2016-5-6 0:00:0 | PW | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1331729770 | US-OH-109518 | 2012-03-14 | Well shall be plugged |
For data sources see[9]