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| Well ID: 34-157-23076 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Tuscarawas | |
| Municipality: Perry Township | |
| Operator Name: ENERVEST OPERATING LLC | |
| Well Pad ID: | |
| Farm/Lease Name: DUNLAP LEASE | |
| License Status: Final Restoration | |
| License Date: 2012-09-17 | |
| Spud Date: 1978-04-13 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1978-05-25 | |
| Well Total Depth: 5878.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.260000 | |
| Longitude: -81.380000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1978-03-28 | 311 STOCKER & SITLER INC GeoDate 3/28/78 |
| Original Spud | 1978-04-13 | |
| Completed | 1978-05-25 | |
| Reached Total Depth | 1978-05-25 | |
| Change of Owner | 1999-05-03 | Operator changed from 311, STOCKER & SITLER INC to 1388, NORTH COAST ENERGY INC |
| Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
| APP | 2012-09-17 | Proposed Formations:CLINTON, Issued Date:9/17/2012, Expired Date:9/17/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2013-10-15 | |
| Record Last Modified | 2014-07-10 | |
| Construction Permit Expires | 2014-09-17 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 5622 | 5700 | 15 |
| 5622 | 5700 | 15 | |
| 5622 | 5700 | 15 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 2100 Bbl | 70000 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1984 | STOCKER & SITLER INC | 11368.00 | 94.00 | 365 |
| 1985 | STOCKER & SITLER INC | 11231.00 | 0.00 | 0 |
| 1986 | STOCKER & SITLER INC | 9936.00 | 327.00 | 365 |
| 1987 | STOCKER & SITLER INC | 6954.00 | 88.00 | 365 |
| 1988 | STOCKER & SITLER INC | 21106.00 | 161.00 | 0 |
| 1989 | STOCKER & SITLER INC | 13625.00 | 141.00 | 365 |
| 1990 | STOCKER & SITLER INC | 23983.00 | 141.00 | 365 |
| 1991 | CARLESS RESOURCES INC | 5988.00 | 0.00 | 365 |
| 1992 | CARLESS RESOURCES INC | 5425.00 | 0.00 | 365 |
| 1993 | STOCKER & SITLER INC | 5001.00 | 0.00 | 365 |
| 1994 | STOCKER & SITLER INC | 4669.00 | 0.00 | 0 |
| 1995 | STOCKER & SITLER INC | 3358.00 | 0.00 | 0 |
| 1996 | STOCKER & SITLER INC | 1855.00 | 0.00 | 0 |
| 1997 | STOCKER & SITLER INC | 0.00 | 0.00 | 365 |
| 1998 | STOCKER & SITLER INC | 0.00 | 0.00 | 365 |
| 1999 | EXCO - NORTH COAST ENERGY INC | 7332.00 | 0.00 | 365 |
| 2000 | EXCO - NORTH COAST ENERGY INC | 4326.00 | 0.00 | 365 |
| 2001 | EXCO - NORTH COAST ENERGY INC | 2824.00 | 0.00 | 365 |
| 2002 | EXCO - NORTH COAST ENERGY INC | 1774.00 | 0.00 | 365 |
| 2003 | EXCO - NORTH COAST ENERGY INC | 2649.00 | 0.00 | 365 |
| 2004 | EXCO - NORTH COAST ENERGY INC | 444.00 | 0.00 | 365 |
| 2005 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 365 |
| 2006 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 365 |
| 2007 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
| 2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 35.00 | 366 |
| 2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
| 2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| 2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
| 2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1597259961 | 2014-4-9 0:00:0 | FR | No Violations | 1.50 |
| -1963290300 | 2013-10-9 0:00: | PB | No Violations | 1.50 |
| -566521383 | 2013-10-22 0:00 | FR | No Violations | |
| 0566521383 | 2013-10-22 | Final Restoration | No Violations | I arrived on location with landowner ( Gary Kimble ) to check final restoration. Company has final graded and seeded wellsite and tank battery and closed plugging pit. Final restoration is approved. Well was plugged on 10/11/2013. |
| 0661313856 | 2013-04-11 | Preliminary Restoration | No Violations | I arrived on location and found violation has not been corrected as of this date. A plug permit was issued on 09/17/2012. |
| 1344265451 | 2012-08-01 | Production Wells | Violations Noted | I arrived on location and found well idle. Checked production reports which showed no production since 2006 . Equipment has been removed so well cannot produce. H2s is leaking from wellhead. Because well has been idle for so long no temporary inactive status will be permitted. |
| 1348249339 | 2012-08-01 | Production Wells | No Violations | Well is idle leaking h2s. |
| 1381934907 | 2013-10-10 | Plug / Plug Back | No Violations | Arrived on location and found crew pulling 2 tubing and trying to rip 41/2. Plug pit lined . |
| 1597259961 | 2014-04-09 | Final Restoration | No Violations | On the day of my inspection following up on NOV-1344265451, I was accompanied by landowner and Enervest well tender to verify the well location with the coordinates being 40.262723 -81.379896. Also with the plugging of well prior complaint and compliance issues have been resolved. |
| 1822582624 | 2013-10-11 | Plug / Plug Back | No Violations | Arrived on location and found crew ripping 41/2 having trouble. Well has H2S and crew is killing well with brine. |
| 1915147704 | 2013-10-07 | Plug / Plug Back | No Violations | Arrived on location and met with landowner Mr Kimble who advised he had concerns about plugging a well on his farm which has h2s leaking from well-head. I went over the plugging program with him. |
| 1963290300 | 2013-10-09 | Plug / Plug Back | No Violations | Met with Chip of Chipco well service and showed him where well were located. Company is going to plug well which has h2s leaking from well-head. |
| 661313856 | 2013-4-11 0:00: | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 1344265451 | US-OH-109955 | 2012-12-04 | Well shall be plugged | |
| 1344265451 | US-OH-109956 | 2012-12-04 | Defective casing, leaking well |
For data sources see[9]