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Well ID: 34-157-23245 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Sugar Creek Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: MILLER NELSON | |
License Status: Final Restoration | |
License Date: 2014-06-10 | |
Spud Date: 1978-11-12 | |
Spud Drilling Contractor: | |
Final Drill Date: 1978-11-18 | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.500000 | |
Longitude: -81.600000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1978-11-09 | 168 RED HILL DEVELOPMENT GeoDate 11/9/78 |
Original Spud | 1978-11-12 | |
Completed | 1978-11-18 | |
Reached Total Depth | 1978-11-18 | |
APP | 2014-06-10 | Proposed Formations:CLINTON, Issued Date:6/10/2014, Expired Date:6/9/2016 12:00:00 PM, Drilling unit acres:64.2, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-11-25 | |
Construction Permit Expires | 2016-06-09 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4408 | 4490 | 7 |
4408 | 4490 | 7 | |
4408 | 4490 | 7 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 143000 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RHDK OIL & GAS LLC/DBA RED HIL | 4892.00 | 0.00 | 0 |
1985 | RHDK OIL & GAS LLC/DBA RED HIL | 3841.00 | 0.00 | 365 |
1986 | RHDK OIL & GAS LLC/DBA RED HIL | 1813.00 | 0.00 | 365 |
1987 | RHDK OIL & GAS LLC/DBA RED HIL | 1989.00 | 0.00 | 365 |
1988 | RHDK OIL & GAS LLC/DBA RED HIL | 1348.00 | 0.00 | 365 |
1989 | RHDK OIL & GAS LLC/DBA RED HIL | 797.00 | 0.00 | 365 |
1990 | RHDK OIL & GAS LLC/DBA RED HIL | 890.00 | 0.00 | 365 |
1991 | RHDK OIL & GAS LLC/DBA RED HIL | 624.00 | 0.00 | 365 |
1992 | RHDK OIL & GAS LLC/DBA RED HIL | 799.00 | 0.00 | 365 |
1993 | RHDK OIL & GAS LLC/DBA RED HIL | 1127.00 | 0.00 | 365 |
1994 | RHDK OIL & GAS LLC/DBA RED HIL | 710.00 | 0.00 | 365 |
1995 | RHDK OIL & GAS LLC/DBA RED HIL | 507.00 | 0.00 | 365 |
1996 | RHDK OIL & GAS LLC/DBA RED HIL | 512.00 | 0.00 | 365 |
1997 | RHDK OIL & GAS LLC/DBA RED HIL | 159.00 | 40.00 | 365 |
2010 | RHDK OIL & GAS LLC/DBA RED HIL | 171.00 | 0.00 | 365 |
2011 | RHDK OIL & GAS LLC/DBA RED HIL | 1874.00 | 0.00 | 365 |
2014 | RHDK OIL & GAS LLC/DBA RED HIL | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 0 |
1985 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1986 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1987 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1988 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1989 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1990 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1991 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1992 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1993 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1994 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1995 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1996 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
1997 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
2010 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
2011 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 365 |
2014 | RHDK OIL & GAS LLC/DBA RED HIL | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-848207436 | 2015-10-19 0:00 | FR | No Violations | 1.00 |
0848207436 | 2015-10-19 | Final Restoration | No Violations | On the day of my inspection I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B). |
1416249451 | 2014-11-17 | Plug / Plug Back | No Violations | On the day of my inspection I found Nicks Well Plugging preparing to plug and abandon the well. 2 3/8 inch tubing is being run to the perfs and will be ready to start setting plugs tomorrow. |
1416315449 | 2014-11-18 | Plug / Plug Back | No Violations | on the day of my inspection I found Nicks Well Plugging ready to set the bottom plug at 4408 feet with 30 sacks of cement. Established circulation and set plug. In an attenpt to pull strech in the 4 1/2 casing the 8 inch casing started to come with the 4 1/2 inch casing both strings of casing appear to be parted around 50 feet. |
1416409496 | 2014-11-19 | Plug / Plug Back | No Violations | On the day of my inspection I found Nicks Well Plugging running at tapered mill to the depth of 50 feet. Unable to go any deeper with this tool. The wellhead was secured so it would not slip down the wellbore, and the wellhead was removed. A 27 foot piece of 4 1/2 inch casing was removed from the wellbore. It was full of holes and was corroded in to. A piece of 7 inch casing with a guide shoe was fabricated to run in the wellbore to center up the 4 1/2 inch casing the wellbore. |
1416488508 | 2014-11-20 | Plug / Plug Back | No Violations | On the day of my inspection I found that Nicks Well Plugging has installed the 7 inch casing and are prepairing to run the wellbore with a tapered mill to clean up the top of the 4 1/2 inch casing. |
1416574896 | 2014-11-21 | Plug / Plug Back | No Violations | On the day of my inspection I found Nicks Well Plugging was rigging up a power swivel to was tubing the are starting at 64 feet, and made it down to 115 feet. |
1417003773 | 2014-11-25 | Plug / Plug Back | No Violations | On arrival of location I found the Nicks Well Plugging had completed plugging the well and was grading the location. They were able to reenter the wellbore with 2 inch tubing and the big lime plug, the plug at the bottom of the 8 5/8 inch casing and the last 200 feet to the surface. About 20 feet of the 8 5/8 inch casing was remover do to the casing being parted. |
For data sources see[9]