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Well ID: 34-157-23450 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Warren Township | |
Operator Name: EDWARDS MARY IRENE | |
Well Pad ID: | |
Farm/Lease Name: EDWARDS | |
License Status: Final Restoration | |
License Date: 2005-07-15 | |
Spud Date: 1980-01-28 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-03-04 | |
Well Total Depth: 5300.00 ft | |
Configuration: Vertical | |
Latitude: 40.500000 | |
Longitude: -81.320000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-12-10 | 3523 EDWARDS MARY IRENE GeoDate 12/10/79 |
Original Spud | 1980-01-28 | |
Completed | 1980-03-04 | |
Reached Total Depth | 1980-03-04 | |
CO | 1989-07-14 | 3523 EDWARDS MARY IRENE GeoDate 7/14/89 |
Unknown | 1989-07-14 | Issued Date 7/14/89 Expired Date 7/14/90 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
APP | 2005-07-15 | Proposed Formations:CLINTON, Issued Date:7/15/2005, Expired Date:7/15/2006 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2006-03-08 | |
Construction Permit Expires | 2006-07-15 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5102 | 5168 | 30 |
5102 | 5168 | 30 | |
5102 | 5168 | 30 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2750 Bbl | 25000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MUTUAL OIL & GAS CO | 10946.00 | 0.00 | 0 |
1985 | MUTUAL OIL & GAS CO | 8437.00 | 0.00 | 0 |
1986 | MUTUAL OIL & GAS CO | 2252.00 | 183.00 | 365 |
1987 | MUTUAL OIL & GAS CO | 2487.00 | 276.00 | 0 |
1989 | MUTUAL OIL & GAS CO | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MUTUAL OIL & GAS CO | Brine | 0 | 0 |
1985 | MUTUAL OIL & GAS CO | Brine | 85 | 0 |
1986 | MUTUAL OIL & GAS CO | Brine | 101 | 365 |
1987 | MUTUAL OIL & GAS CO | Brine | 41 | 0 |
1989 | MUTUAL OIL & GAS CO | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-571010133 | 2019-11-5 0:00: | FR | No Violations | 0.20 |
0096109692 | 2006-03-07 | Preliminary Restoration | No Violations | restoration ok |
0632486513 | 2018-06-21 | Final Restoration | No Violations | |
0698732687 | 2006-03-15 | Plug / Plug Back | No Violations | check plug , plug did not slip |
1204859341 | 2006-03-08 | Plug / Plug Back | No Violations | on site for plug job, plug pit ok |
1454430397 | 2016-02-02 | Plug / Plug Back | No Violations | On the day of my inspection I was accompanied by Inspector Joe Zollars. We found that the well has been plugged and the site has been restored. The 8 inch casing has not been cut off below ground. All other items of the restoration have been completed. The site has not passed final restoration. |
1454613379 | 2016-02-04 | Administrative Inspection | No Violations | I contacted Terry Edwards about the surface casing still sticking up above ground. Terry will cut if off and let me know when completed and I will re- inspect for the final restoration. |
1479319481 | 2016-11-16 | Final Restoration | No Violations | On the day of my inspection I was unable to pass the final restoration due the fact that the 8 5/8 inch has not been cut off. I was not able to locate Terry Edwards |
1540304723 | 2018-10-23 | Final Restoration | No Violations | Upon my arrival on location, I witnessed that the 8.625 inch casing had not been cut off yet. I talked to Terry Edwards about this issue in July. I tracked down the owner of the property off of the Tuscarawas Auditor site. I spoke with Mr. Patterson (the property owners farther) about this issue. He also lives on this property. He would have his sons dig up around the 8.625 inch diameter casing, cut the casing off 30 inches below the surface, and install a permit plate on top of the plugged well. Then he would backfill the hole and put grass seed on it. He said he would give me a call, so I can witness the job being completed. |
1683864855 | 2019-12-19 0:00 | FR | No Violations | 0.70 |
632486513 | 2018-6-21 0:00: | FR | No Violations | 0.50 |
698732687 | 2006-3-15 0:00: | PB | No Violations | |
96109692 | 2006-3-7 0:00:0 | PL | No Violations |
For data sources see[9]