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Well ID: 34-157-23536 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Dover Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: REYNOLDS-STUCKY UNIT | |
License Status: Final Restoration | |
License Date: 2017-11-22 | |
Spud Date: 1980-09-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-09-17 | |
Well Total Depth: 4840.00 ft | |
Configuration: Vertical | |
Latitude: 40.490000 | |
Longitude: -81.560000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-08-14 | 168 RED HILL DEVELOPMENT GeoDate 8/14/80 |
Original Spud | 1980-09-13 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Completed | 1980-09-17 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Reached Total Depth | 1980-09-17 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
APP | 2017-11-22 | Proposed Formations:CLINTON, Issued Date:11/22/2017, Expired Date:11/22/2019 12:00:00 PM, Drilling unit acres:93.4, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-04-30 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Record Last Modified | 2018-12-20 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Construction Permit Expires | 2019-11-22 | UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4661 | 4743 | 6 |
4661 | 4743 | 6 | |
4661 | 4743 | 6 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 88300 Gal | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-697841113 | 2018-4-25 0:00: | PB | No Violations | 2.00 |
0090323688 | 2018-04-27 | Plug / Plug Back | No Violations | Upon arrival on location, I witnessed Redhill rig crew had ripped 4.5 inch diameter casing at 3500 feet and had it all pulled out of well. They had 1.5 inch diameter tubing ran back in well to the depth of 3200 feet. Petroset was on location preparing to set the second cement plug in well. Petroset established circulation, then set a 50 sack, Class A cement plug at 3200 feet. They displaced to 3000 feet with 7.5 barrels of fresh water. The rig crew pulled 1.5 inch diameter tubing to the depth of 1244 feet. Petroset established circulation, then pumped a 55 sack, Class A cement plug at 1244 feet. They displaced to 1044 feet with 2.6 barrels of fresh water. The rig crew pulled 1.5 inch diameter tubing to the depth of 200 feet. Petroset established circulation, then pumped a 55 sack, Class A cement plug from 200 feet to surface. The rig crew pulled the remaining tubing out of well. |
0171285991 | 2006-08-14 | Production Wells | No Violations | Arrived on location and found Sound energy has put well into production. Violation has been corrected. CASE CLOSED 08/14/06 |
0697841113 | 2018-04-25 | Plug / Plug Back | No Violations | Upon arrival on location I was accompanied by Inspector Jeff Adams. Please refer to his report. |
1395348094 | 2014-03-20 | Production Wells | No Violations | On the day of my inspection accompanied with ODNR Inspector Randy Akins, I witnessed that there was 1-100bbl tank, a horizontal separator and a 2 inch sales meter with a chart recorder. The well was equipped with 8.625 inch casing, 4.5 inch casing, 2.375 inch tubing and a plunger lift system logically controlled. Identification was present and production records are up to date. Updated GPS coordinates are 40.491074 -81.567825 and have been verified with handheld unit. |
1524241526 | 2018-04-20 | Plug / Plug Back | No Violations | Upon arrival at location, I witnessed the plugging rig was moved in on site. It was not rigged up over the hole at this time. There was also a tractor and trailer on site for hauling pipe off location. Nobody was on location at the time of inspection. |
1625997179 | 2018-11-13 | Final Restoration | No Violations | On the day of inspection, I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B). |
1697696457 | 2018-04-30 | Plug / Plug Back | No Violations | Upon arrival on location, I witnessed the top cement plug had a hard, smooth finish and had settled 18 inches below surface. |
171285991 | 2006-8-14 0:00: | PW | No Violations | |
1873232365 | 2018-04-25 | Plug / Plug Back | No Violations | Upon arrival at location, accompanied by ODNR Inspector Randy Akins, I witnessed Redhill rig crew had ran tubing to the depth of 4661 feet. Petroset cleared tubing, then set a 30 sack, Class A cement plug, then displaced with 11.5 barrel of fresh water. |
90323688 | 2018-4-27 0:00: | PB | No Violations | 4.70 |
For data sources see[9]