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Well ID: 34-157-23717 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Washington Township | |
Operator Name: AM-TEK OIL INC | |
Well Pad ID: | |
Farm/Lease Name: FULLER R | |
License Status: Producing | |
License Date: 1982-04-12 | |
Spud Date: 1982-05-20 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1982-05-27 | |
Well Total Depth: 5710.00 ft | |
Configuration: Vertical | |
Latitude: 40.210000 | |
Longitude: -81.340000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-04-12 | 2559 WNT OPERATING INC GeoDate 4/12/82 |
Oil and Gas | 1982-04-12 | Issued Date 4/13/82 Expired Date 10/10/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05710 Proposed Drill Depth 05710 |
Original Spud | 1982-05-20 | |
Completed | 1982-05-27 | |
Reached Total Depth | 1982-05-27 | |
Construction Permit Expires | 1982-10-10 | |
Completion Report Received | 1983-02-04 | |
Change of Owner | 2001-09-05 | Operator changed from 2559, WNT OPERATING INC to 2543, TIPKA ENERGY DEVLOP CO |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5505 | 5583 | 22 |
5505 | 5583 | 22 | |
5505 | 5583 | 22 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1700 Bbl | 50000 | FRAC: 1700 BBL H2O, 50M SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TIPKA WILLIAM N | 11481.00 | 262.00 | 365 |
1985 | TIPKA WILLIAM N | 6358.00 | 154.00 | 0 |
1986 | WNT OPERATING INC | 4037.00 | 62.00 | 365 |
1987 | WNT OPERATING INC | 5065.00 | 155.00 | 365 |
1988 | WNT OPERATING INC | 4672.00 | 132.00 | 365 |
1989 | WNT OPERATING INC | 4322.00 | 67.00 | 365 |
1990 | WNT OPERATING INC | 3412.00 | 0.00 | 365 |
1991 | WNT OPERATING INC | 3180.00 | 67.00 | 365 |
1992 | WNT OPERATING INC | 1910.00 | 67.00 | 365 |
1993 | WNT OPERATING INC | 2058.00 | 55.00 | 365 |
1994 | WNT OPERATING INC | 1792.00 | 0.00 | 365 |
1995 | WNT OPERATING INC | 1359.00 | 68.00 | 365 |
1996 | WNT OPERATING INC | 1200.00 | 64.00 | 366 |
1997 | WNT OPERATING INC | 1319.00 | 0.00 | 365 |
1999 | WNT OPERATING INC | 955.00 | 0.00 | 365 |
2000 | WNT OPERATING INC | 1013.00 | 48.00 | 366 |
2001 | TIPKA ENERGY DEVLOPMENT COMPAN | 922.00 | 0.00 | 365 |
2002 | TIPKA ENERGY DEVLOPMENT COMPAN | 373.00 | 0.00 | 365 |
2003 | TIPKA ENERGY DEVLOPMENT COMPAN | 492.00 | 53.00 | 365 |
2004 | TIPKA ENERGY DEVLOPMENT COMPAN | 563.00 | 0.00 | 366 |
2005 | TIPKA ENERGY DEVLOPMENT COMPAN | 379.00 | 24.00 | 365 |
2006 | TIPKA ENERGY DEVLOPMENT COMPAN | 720.00 | 0.00 | 365 |
2007 | TIPKA ENERGY DEVLOPMENT COMPAN | 699.00 | 0.00 | 365 |
2008 | TIPKA ENERGY DEVLOPMENT COMPAN | 316.00 | 0.00 | 366 |
2009 | TIPKA ENERGY DEVLOPMENT COMPAN | 307.00 | 0.00 | 365 |
2010 | TIPKA ENERGY DEVLOPMENT COMPAN | 285.00 | 51.00 | 365 |
2011 | TIPKA ENERGY DEVLOPMENT COMPAN | 516.00 | 4.00 | 0 |
2012 | TIPKA ENERGY DEVLOPMENT COMPAN | 724.00 | 44.00 | 366 |
2013 | TIPKA ENERGY DEVLOPMENT COMPAN | 974.00 | 67.00 | 365 |
2014 | TIPKA ENERGY DEVLOPMENT COMPAN | 1236.00 | 30.00 | 365 |
2015 | TIPKA ENERGY DEVLOPMENT COMPAN | 1003.00 | 25.00 | 365 |
2016 | TIPKA ENERGY DEVLOPMENT COMPAN | 991.00 | 27.00 | 366 |
2017 | TIPKA ENERGY DEVLOPMENT COMPAN | 1404.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1222636709 | 2015-3-6 0:00:0 | PW | No Violations | 1.50 |
-1406446600 | 2014-2-27 0:00: | PW | No Violations | |
-348139636 | 2016-2-26 0:00: | PW | No Violations | 1.50 |
-945308030 | 2015-4-14 0:00: | PW | No Violations | 1.00 |
0000PL3110 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
001252i350 | 2002-08-27 | Production Wells | No Violations | no violations |
0048859547 | 2014-09-18 | Production Wells | No Violations | We began our investigation at the location of a 30bbl tank and sales line along Atkinson Creek Rd. SE, Perry Township, Tuscarawas County, Ohio. The purpose of the investigation was to respond to a complaint received from Mr. Mike Pivonka which referenced his property and that of his brother-in-law Mr. Clyde Fuller. Mr. Pivonka had claimed to smell gas on his property, particularly H2S. Our investigation included determining whether H2S or any other gases were present near the locations of Mr. Clyde Fullers properties or that of his brother-in-law Mr. Mike Pivonka. A complaint was taken from Mr. Fuller in the past referring to the odor of H2S on his property and the case was closed due to a lack of evidence. Personnel on site were ODNR Inspector Randy Akins, SE District Supervisor Brent Bear, and ODNR Inspector Brandon Trigg. Our beginning coordinates were 40.22027 N/-81.33530 W. We used Honeywell PhD6 gas handheld gas monitoring devices around the tank, sales line, and motor valve. We did not detect H2S around the equipment. We checked any pipeline road crossing vents for gas throughout our route.
-81.33841 W. We monitored around the home and property adjacent to the home as well as the exhaust unit that came out from the house on the west side and where a gas line had previously been connected near the same location. We did not detect H2S around the home, adjacent property, or along the roadway from our starting point. -81.342274. We monitored gas levels around the perimeter of his rental home, barn, and the low lying areas near the stream to the south of the road. We did not detect any gas at this location. We continued west to the location of the R. Fuller #1 well, separator, and tan |
0075321618 | 2015-05-12 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
0136763879 | 2016-10-13 | Production Wells | No Violations | On the day of my inspection I found an 8 5/8 X 4 1/2 inch wellhead and a 4 1/2 X 1 1/2 wellhead operated by a plunger lift system. The valves are in the open position. The tank battery is made up of one 100 bbl. tank, one 50 bbl. tank, and a horizontal separator, and a recording gauge, in and earthen dike. The production reporting is up to date, the tank is properly identified, the production reporting is up to date, and there are no violations at this time. There are no indications of any H2S at this time. |
0302240366 | 2015-03-19 | Production Wells | No Violations | |
0348139636 | 2016-02-26 | Production Wells | No Violations | |
0945308030 | 2015-04-14 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1222636709 | 2015-03-06 | Production Wells | No Violations | On the date of inspection I am following up on complaint #4911. I inspected the well head, separator, tank, and from Guthrie Road along Atkinson Creek Road to Deer Horn Road. I was unable to detect any gas leaking at the well site or along the road either by odor or my personal protective gas meter. |
1240962354 | 2010-06-18 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1252i350 | 2002-8-27 0:00: | PW | No Violations | |
136763879 | 2016-10-13 0:00 | PW | No Violations | 1.00 |
1406446600 | 2014-02-27 | Production Wells | No Violations | I arrived on location with Oil and Gas well inspector Mark Moreland, to conduct an inspection of oil and gas wells located within 1/2 mile radius of H2S complaint no. 3701. Inspector Moreland monitored the well site with a calibrated Sperian PHD6 gas meter for this inspection and showed no detection of H2S. |
1420465978 | 2014-01-05 | Production Wells | No Violations | On the day of my inspection I found a 4 X 1.5 wellhead and the system was operated by a plunger lift. A horizontal separator, a 50 bbl, and a 100 bbl tank, all in an earthen dike. The tank is properly identified. The production reports are up to date. I had a report of some gas leakage at this location. I called Tipka and they responded to the location and found no gas leakage. On Sunday Freeport fire department was call to the location for an odor of gas. I talked with Gary with the fire department and he stated there was no gas odor. I have not found any gas leakage at this time. I met with the pumper with Tipka and Vito Amian at the location, again no gas leakage was found. The well and the separator have been temporally shut in. |
1421075353 | 2015-01-12 | Production Wells | No Violations | On the day of my inspection I did not find any gas leaking, and no H2S. The well is still shut in and there was no odors. I have surveyed the bottom area along Atkinson road and I have not found any gas odors. I also inspected the pipeline drip area, and did not find any gas odor. |
1421852120 | 2015-01-21 | Production Wells | No Violations | On the day of my inspection I found the well has been place back into production. I did not find any odors around the well or the tanks and separator. In surveying the area I did not find any odor. The weather conditions were right to find any gas odor. Lite snow, fog, and lite rain. I did not encounter any gas odors. This is a follow up to complaint ID 4911. |
1423231612 | 2015-02-06 | Production Wells | No Violations | On the day of my inspection, I surveyed the area along Atkinson Road and the well and tank battery. I found no gas leakage. This is a follow up to complaint ID #4911. |
1424182483 | 2015-02-17 | Production Wells | No Violations | On the day of my inspection, I surveyed the area along Atkinson Road and the well and tank battery. I found no gas leakage. This is a follow up to complaint ID #4911. |
1424967536 | 2015-02-26 | Production Wells | No Violations | On the day of my inspection I did not find any signs of gas leakage or H2S around the well or in the area along Atkinson Road. The well looks like it has been temporally shut in. |
1426079008 | 2015-03-11 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1426683157 | 2015-03-18 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1427374108 | 2015-03-26 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1427982959 | 2015-04-02 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1432745668 | 2015-05-27 | Plug / Plug Back | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1439821623 | 2015-08-17 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1443098359 | 2015-09-24 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
1568891297 | 2019-9-18 0:00: | PW | No Violations | 1.00 |
1982340325 | 2015-04-28 | Production Wells | No Violations | On the day of my inspection I found that the well was in production and there was no gas odors or signs of H2S. I surveyed the area along Atkinson Road and found no gas odors. This is a follow up to complaint # 4911. |
2137425745 | 2016-08-03 | Production Wells | No Violations | I arrived on site today after encountering a concerned citizen who I met conducting an inspection on another well bore. The person wished to stay anonymous and informed me that he had noticed some odd orders coming from the well bore well he was hunting last year. He asked if I would just perform an inspection on the well for him. When I arrived on location I witnessed the permitted well bore is utilizing a plunger-lift system for means of production. The casing program for the well consists of 8.625 inch diameter surface casing, 4.5 inch diameter production casing and 1.5 inch diameter production tubing. The plunger is being operated by a motor valve and a control box. All valves were in the open position. Production equipment consists of a horizontal separator, a 2 inch diameter meter run, a 50 barrel brine tank and a 100 barrel production tank. All production equipment is placed inside an earthen dike that measures approximately 20 feet by 25 feet at an average height of 1.5 foot. RBDMS records indicate that the well is in producing order and no issues could be noted at the time of my inspection. I did not noticed any odors or detect any gases with my meters. I stated to him I would perform a follow up inspection on the well. |
302240366 | 2015-3-19 0:00: | PW | No Violations | 1.00 |
48859547 | 2014-9-18 0:00: | PW | No Violations | 4.00 |
75321618 | 2015-5-12 0:00: | PW | No Violations | 1.50 |
PL3110 | PL | No Violations |
For data sources see[9]