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Well ID: 34-157-23826 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Goshen Township | |
Operator Name: A BERRY ENTERPRISES LLC | |
Well Pad ID: | |
Farm/Lease Name: TUSC COUNTY COMMISSIONERS | |
License Status: Producing | |
License Date: 1983-03-03 | |
Spud Date: 1983-05-11 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1983-05-14 | |
Well Total Depth: 5230.00 ft | |
Configuration: Vertical | |
Latitude: 40.480000 | |
Longitude: -81.400000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-03-03 | Issued Date 3/3/83 Expired Date 8/30/83 Acres 0067000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05230 Proposed Drill Depth 05230 |
Original Spud | 1983-05-10 | |
Completed | 1983-05-14 | |
Reached Total Depth | 1983-05-14 | |
CO | 1983-05-23 | 84 EVERFLOW EASTERN PTNS L P GeoDate 3/3/83 |
Completion Report Received | 1983-06-03 | |
Construction Permit Expires | 1983-08-30 | |
Change of Owner | 2018-02-28 | Operator changed from 84, EVERFLOW EASTERN PTNS L P to 5567, BERRY ENTERPRISES INC |
Change of Owner | 2018-07-25 | Operator changed from 5567, BERRY ENTERPRISES INC to 10068, A BERRY ENTERPRISES LLC |
Record Last Modified | 2018-07-25 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5028 | 5130 | 0 |
5028 | 5130 | 0 | |
2006-09-11 | 5035 | 5074 | 14 |
5035 | 5074 | 14 | |
5028 | 5130 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 96000 Gal | 60000 | FRAC: 96MG H2O, 60M SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL3017 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1401043391 | 2018-05-22 | Production Wells | No Violations | Upon arrival on location, I witnessed the well was equipped 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, and a plunger lift system. The well was shut in at the time of the inspection. Production equipment included a plastic 50 barrel tank and a horizonal separator within an earthen dike. The production report was up to date. The identification needs to be updated, made a phone call to new owner. |
1595596994 | 2020-7-24 0:00: | PW | No Violations | 0.30 |
PL3017 | PL | No Violations |
For data sources see[9]