If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-157-24253 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.22,"lon":-81.34,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Perry Township | |
Operator Name: AM-TEK OIL INC | |
Well Pad ID: | |
Farm/Lease Name: FULLER | |
License Status: Producing | |
License Date: 1985-04-10 | |
Spud Date: 1985-09-05 | |
Spud Drilling Contractor: BULLDOG DRLG | |
Final Drill Date: 1985-09-12 | |
Well Total Depth: 5923.00 ft | |
Configuration: Vertical | |
Latitude: 40.220000 | |
Longitude: -81.340000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-04-10 | 2559 WNT OPERATING INC GeoDate 4/10/85 |
Oil and Gas | 1985-04-10 | Issued Date 4/10/85 Expired Date 10/7/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05923 Proposed Drill Depth 05923 |
Original Spud | 1985-09-05 | |
Completed | 1985-09-12 | |
Reached Total Depth | 1985-09-12 | |
Construction Permit Expires | 1985-10-07 | |
Completion Report Received | 1985-11-19 | |
Change of Owner | 2001-09-05 | Operator changed from 2559, WNT OPERATING INC to 2543, TIPKA ENERGY DEVLOP CO |
Last Compliance Report | 2016-05-06 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5528 | 5662 | 0 |
5528 | 5662 | 0 | |
2006-09-11 | 5557 | 5600 | 19 |
5557 | 5600 | 19 | |
5528 | 5662 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1550 Bbl | 40000 | FRAC;H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | WNT OPERATING INC | 6140.00 | 66.00 | 365 |
1987 | WNT OPERATING INC | 6734.00 | 66.00 | 365 |
1988 | WNT OPERATING INC | 2410.00 | 0.00 | 365 |
1989 | WNT OPERATING INC | 2175.00 | 0.00 | 365 |
1990 | WNT OPERATING INC | 3164.00 | 0.00 | 365 |
1991 | WNT OPERATING INC | 2801.00 | 0.00 | 365 |
1992 | WNT OPERATING INC | 2397.00 | 0.00 | 365 |
1993 | WNT OPERATING INC | 1913.00 | 99.00 | 365 |
1994 | WNT OPERATING INC | 1811.00 | 0.00 | 365 |
1995 | WNT OPERATING INC | 1828.00 | 0.00 | 365 |
1996 | WNT OPERATING INC | 1851.00 | 0.00 | 366 |
1997 | WNT OPERATING INC | 1226.00 | 0.00 | 365 |
1999 | WNT OPERATING INC | 687.00 | 0.00 | 365 |
2000 | WNT OPERATING INC | 736.00 | 40.00 | 366 |
2001 | TIPKA ENERGY DEVLOPMENT COMPAN | 551.00 | 0.00 | 365 |
2002 | TIPKA ENERGY DEVLOPMENT COMPAN | 822.00 | 0.00 | 365 |
2003 | TIPKA ENERGY DEVLOPMENT COMPAN | 593.00 | 0.00 | 365 |
2004 | TIPKA ENERGY DEVLOPMENT COMPAN | 278.00 | 0.00 | 366 |
2005 | TIPKA ENERGY DEVLOPMENT COMPAN | 242.00 | 0.00 | 365 |
2006 | TIPKA ENERGY DEVLOPMENT COMPAN | 691.00 | 0.00 | 365 |
2007 | TIPKA ENERGY DEVLOPMENT COMPAN | 537.00 | 0.00 | 365 |
2008 | TIPKA ENERGY DEVLOPMENT COMPAN | 442.00 | 0.00 | 366 |
2009 | TIPKA ENERGY DEVLOPMENT COMPAN | 302.00 | 0.00 | 365 |
2010 | TIPKA ENERGY DEVLOPMENT COMPAN | 128.00 | 0.00 | 365 |
2011 | TIPKA ENERGY DEVLOPMENT COMPAN | 167.00 | 0.00 | 0 |
2012 | TIPKA ENERGY DEVLOPMENT COMPAN | 472.00 | 0.00 | 366 |
2013 | TIPKA ENERGY DEVLOPMENT COMPAN | 588.00 | 0.00 | 365 |
2014 | TIPKA ENERGY DEVLOPMENT COMPAN | 559.00 | 30.00 | 365 |
2015 | TIPKA ENERGY DEVLOPMENT COMPAN | 852.00 | 0.00 | 365 |
2016 | TIPKA ENERGY DEVLOPMENT COMPAN | 676.00 | 19.00 | 366 |
2017 | TIPKA ENERGY DEVLOPMENT COMPAN | 473.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1382910292 | 2015-8-17 0:00: | PW | No Violations | 1.00 |
-1431306957 | 2014-2-27 0:00: | PW | No Violations | |
-1923491940 | 2016-10-13 0:00 | PW | No Violations | 1.00 |
0000PL2685 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
001252i349 | 2002-08-27 | Production Wells | No Violations | no violations |
0172878787 | 2016-01-29 | Temporary Abandoned Annular Disposal | No Violations | |
1252i349 | 2002-8-27 0:00: | PW | No Violations | |
1381675315 | 2015-01-05 | Production Wells | No Violations | On the day of my inspection I found a 4 X 1.5 inch wellhead. The system is operated by a plunger lift. A horizontal separator , a 50 bbl tank, and two 100 bbl tanks are in an earthen dike. The production records are up to date. |
1382910292 | 2015-08-17 | Production Wells | No Violations | On the day of my inspection I found a 4 X 1.5 inch wellhead operated by a plunger lift system. The valves are in the open position. The tank battery is made up of two 100 bbl. tanks, one 50 bbl. tank, and a horizontal separator, all in an earthen dike. The tanks are properly identified. The production reporting is up to date, and there are no violations at this time. |
1390335780 | 2012-04-04 | Production Wells | No Violations | I arrived on location and made an inspection at the tank battery and wellsite I found well to be in production, all valves are open and a new chart has been placed in meter box. No violations this date. |
1408029143 | 2014-08-13 | Production Wells | Violations Noted | On the day of my inspection I was accompanied by Mark Morland and Brent Bear due to being a known H2S area. I had received a call from John Tipka of Tipka Energy that a pipeline leak was called to them form the fire department. Upon arriving at the Fuller farm I was met By Mr. Fuller. He was upset with our department, and how useless our department is and that it was our fault the he was unable to live in his home. I then met Brian Tipka and was taken to the leak site. No H2s was detected. The pipeline was exposed and a repair clamp was installed. |
1431306957 | 2014-02-27 | Production Wells | No Violations | I arrived on location with Oil and Gas well inspector Mark Moreland, to conduct an inspection of oil and gas wells located within 1/2 mile radius of H2S complaint no. 3701. Inspector Moreland monitored the well site with a calibrated Sperian PHD6 gas meter for this inspection and showed no detection of H2S. |
172878787 | 2016-1-29 0:00: | TD | No Violations | 0.50 |
1923491940 | 2016-10-13 | Production Wells | No Violations | On the day of my inspection I found an 8 5/8 X 4 1/2 inch wellhead and a 4 1/2 X 1 1/2 wellhead operated by a plunger lift system. The valves are in the open position. The tank battery is made up of two 100 bbl. tank, a horizontal separator, and one 50 bbl. brine tank, all in an earthen dike. The production reporting is up to date, the tank is properly identified, and there are no violations at this time. |
PL2685 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1408029143 | US-OH-112017 | 2014-11-05 | Inadequate pipeline strength |
For data sources see[9]