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34-157-24295

Well Details

Well ID: 34-157-24295
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Country: United States
State: Ohio
County: Tuscarawas
Municipality: Mill Township
Operator Name: DOVER ATWOOD CORP.
Well Pad ID:
Farm/Lease Name: RANDALL
License Status: Final Restoration
License Date: 2013-06-20
Spud Date: 1987-12-12
Spud Drilling Contractor: MID ATLANTC DRLG
Final Drill Date: 1987-12-19
Well Total Depth: 5295.00 ft
Configuration: Vertical
Latitude: 40.370000
Longitude: -81.330000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1985-07-08 1754 SUTTON ENTERPRISES INC GeoDate 7/8/85
Oil and Gas 1985-07-08 Issued Date 7/8/85 Expired Date 7/8/86 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1987-10-20 1754 SUTTON ENTERPRISES INC GeoDate 10/20/87
Oil and Gas 1987-10-20 Issued Date 10/20/87 Expired Date 10/19/88 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05295 Proposed Drill Depth 05295
Original Spud 1987-12-12 RI/ RL 10-24-87
Completed 1987-12-19 RI/ RL 10-24-87
Reached Total Depth 1987-12-19 RI/ RL 10-24-87
Completion Report Received 1988-01-13 RI/ RL 10-24-87
CO 1993-10-22 2172 NATLAND ENERGY CORP GeoDate 10/20/87
Change of Owner 1997-07-25 Operator changed from 2172, NATLAND ENERGY CORP to 182, BELDEN & BLAKE CO
Change of Owner 1999-04-23 Operator changed from 182, BELDEN & BLAKE CORPORATION to 6351, T & C OIL & GAS COMPANY
Change of Owner 1999-05-24 Operator changed from 6351, T & C OIL & GAS COMPANY to 5935, DOVER ATWOOD CORP.
APP 2013-06-20 Proposed Formations:CLINTON, Issued Date:6/20/2013, Expired Date:6/20/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-05-28 RI/ RL 10-24-87
Construction Permit Expires 2015-06-20 RI/ RL 10-24-87
Record Last Modified 2017-02-15 RI/ RL 10-24-87

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5136 5228 0
5136 5228 0
2006-09-11 5170 5182 9
5170 5182 9
5136 5228 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1280 Bbl 60000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 SUTTON ENTERPRISES INC 13910.00 252.00 303
1989 SUTTON ENTERPRISES INC 9330.00 81.00 365
1990 SUTTON ENTERPRISES INC 7036.00 0.00 365
1991 SUTTON ENTERPRISES INC 4993.00 60.00 365
1992 SUTTON ENTERPRISES INC 4383.00 42.00 365
1993 SUTTON ENTERPRISES INC 3710.00 42.00 365
1994 SUTTON ENTERPRISES INC 4037.00 0.00 365
1995 SUTTON ENTERPRISES INC 3165.00 0.00 365
1996 SUTTON ENTERPRISES INC 2129.00 100.00 365
1999 DOVER ATWOOD CORP. 0.00 0.00 0
2000 DOVER ATWOOD CORP. 0.00 0.00 365
2001 DOVER ATWOOD CORP. 0.00 0.00 365
2002 DOVER ATWOOD CORP. 0.00 0.00 365
2003 DOVER ATWOOD CORP. 0.00 0.00 365
2004 DOVER ATWOOD CORP. 0.00 0.00 365
2005 DOVER ATWOOD CORP. 0.00 0.00 365
2006 DOVER ATWOOD CORP. 0.00 0.00 365
2007 DOVER ATWOOD CORP. 0.00 0.00 365
2008 DOVER ATWOOD CORP. 0.00 0.00 365
2009 DOVER ATWOOD CORP. 0.00 0.00 365
2010 DOVER ATWOOD CORP. 0.00 0.00 365
2011 DOVER ATWOOD CORP. 0.00 0.00 0
2013 DOVER ATWOOD CORP. 0.00 0.00 0
2014 DOVER ATWOOD CORP. 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 SUTTON ENTERPRISES INC Brine 344 303
1989 SUTTON ENTERPRISES INC Brine 31 365
1990 SUTTON ENTERPRISES INC Brine 1312 365
1991 SUTTON ENTERPRISES INC Brine 31 365
1992 SUTTON ENTERPRISES INC Brine 23 365
1993 SUTTON ENTERPRISES INC Brine 0 365
1994 SUTTON ENTERPRISES INC Brine 0 365
1995 SUTTON ENTERPRISES INC Brine 0 365
1996 SUTTON ENTERPRISES INC Brine 0 365
1999 DOVER ATWOOD CORP. Brine 0 0
2000 DOVER ATWOOD CORP. Brine 0 365
2001 DOVER ATWOOD CORP. Brine 0 365
2002 DOVER ATWOOD CORP. Brine 0 365
2003 DOVER ATWOOD CORP. Brine 0 365
2004 DOVER ATWOOD CORP. Brine 0 365
2005 DOVER ATWOOD CORP. Brine 0 365
2006 DOVER ATWOOD CORP. Brine 0 365
2007 DOVER ATWOOD CORP. Brine 0 365
2008 DOVER ATWOOD CORP. Brine 0 365
2009 DOVER ATWOOD CORP. Brine 0 365
2010 DOVER ATWOOD CORP. Brine 0 365
2011 DOVER ATWOOD CORP. Brine 0
2013 DOVER ATWOOD CORP. Brine 0 0
2014 DOVER ATWOOD CORP. Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-486872457 2014-4-17 0:00: PW No Violations 2.00
0000PL2654 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0084269947 2015-10-15 Final Restoration No Violations On the day of my inspection I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B).
0303397646 2015-05-27 Plug / Plug Back No Violations On the date of inspection I am on site to witness the fourth attempt for a bottom plug in the well. Hagan Well Service set 1.5 inch tubing to a depth of 1,767 feet. Universal Well Service pumped 132sk of 50/50 POZ cement, 14.4ppg, 1.27 yield, 2% gel, and 10% salt. Circulation was established during cement pumping. Universal displaced cement with 2.5bbl of water. H2S alarms set for 10ppm were not triggered during cementing. The rig will tag the cement plug the following day.
0486872457 2014-04-17 Production Wells No Violations On the day of my inspection I was accompanied by Inspector Mark Moreland. The well was idle and showed signs of H2S. No gas was encountered at this time. Well has 1 1/2 tubing and 8 inch casing. There is severe corrosion. Well is to be plugged By Dover Atwood.
0967507631 2015-05-26 Plug / Plug Back No Violations Upon arrival on location I found that Hagen well service had run an impression block, and it was determined that the 4.5 inch casing has parted. It was discussed and the crew would move 1.5 tubing into location and see if they could reenter the 4.5 inch casing.
1227030131 2010-05-19 Production Wells Violations Noted arrived on site and found well idle, well has h2s leaking from wellhead. Called company and talked with john levengood he advised he is putting well on plug list and will plug this summer.
1274358391 2010-08-02 Production Wells No Violations I arrived on location and found well is in production, no h2s is leaking from wellhead this date. . Case closed on 08/02/2010.
1432657169 2015-05-23 Plug / Plug Back No Violations Upon arrival I found Hagen well service preparing to plug the well. A 30 sack plug was pumped, and when running the wireline in to shoot the pipe off. It was determined that the well was on vacuum. Waited for a half hour and pumped another 30 sack plug. We shut down for 2 hours and checked fluid level to shoot pipe off. The fluid had dropped and a 3rd plug wise pumped. It was decided to shut down over night,
1432658982 2015-05-22 Plug / Plug Back No Violations Upon arrival on location I found that 1800 feet tubing was pulled out of the well. It was decided that 2 3/8 tubing was going to brought to location and fish for the remainder of the tubing.
1432729222 2015-05-27 Plug / Plug Back No Violations Upon arrival on location I found the crew prepairing to run 1.5 inch tubing in the wellbore. Ran the tubing to a depth of 1769 feet. Waiting on cementers.
1432816112 2015-05-28 Plug / Plug Back No Violations Upon arrival on location I found that the rig crew had tagged the top of the cement at 1210 feet. The 4.5 inch casing was ripped at 1106 feet, and a cement plug was set there to 906 feet. The casing was pulled up to a depth of 206 feet and a cement plug was set from there to the surface.
1934009473 2013-12-20 Production Wells No Violations 12/23/2013 12:32 pm, I called Brian Levengood of Dover Atwood Corp to get update for the Randell # 2 well. I was advised by Brian that this well would be plugged with-in four months or before crops are planted. Plug permit for this well was issued on 06/20/2013.
303397646 2015-5-27 0:00: PB No Violations 2.00
84269947 2015-10-15 0:00 FR No Violations 1.00
967507631 2015-5-26 0:00: PB No Violations
PL2654 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1227030131 US-OH-106099 2014-04-23 Well shall be plugged

For data sources see[9]

References