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Well ID: 34-157-24593 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Rush Township | |
Operator Name: S & S ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: JONES | |
License Status: Final Restoration | |
License Date: 2015-06-18 | |
Spud Date: 1987-12-11 | |
Spud Drilling Contractor: ADVENT DRLG | |
Final Drill Date: 1987-12-17 | |
Well Total Depth: 5912.00 ft | |
Configuration: Vertical | |
Latitude: 40.320000 | |
Longitude: -81.280000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-10-09 | 1218 LANGASCO ENERGY CORP GeoDate 10/9/87 |
Oil and Gas | 1987-10-09 | Issued Date 10/9/87 Expired Date 10/8/88 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1987-11-23 | 182 BELDEN & BLAKE CO GeoDate 11/23/87 |
Oil and Gas | 1987-11-23 | Issued Date 10/9/87 Expired Date 10/8/88 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05912 Proposed Drill Depth 05912 |
Original Spud | 1987-12-11 | RL. 11-28-87 |
Completed | 1987-12-17 | RL. 11-28-87 |
Reached Total Depth | 1987-12-17 | RL. 11-28-87 |
Completion Report Received | 1988-03-07 | RL. 11-28-87 |
Change of Owner | 2002-08-12 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2005-07-08 | Operator changed from 1966, PETROX, INC to 5660, S & S ENERGY CORPORATION |
APP | 2015-06-18 | Proposed Formations:CLINTON, Issued Date:6/18/2015, Expired Date:6/17/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-11-25 | RL. 11-28-87 |
Construction Permit Expires | 2017-06-17 | RL. 11-28-87 |
Record Last Modified | 2018-06-23 | RL. 11-28-87 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5710 | 5797 | 32 |
5710 | 5797 | 32 | |
5710 | 5797 | 32 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 90000 Gal | 80000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | RESOURCE AMERICA INC | 0.00 | 0.00 | 365 |
1990 | BELDEN & BLAKE CORPORATION | 3756.00 | 0.00 | 181 |
1991 | BELDEN & BLAKE CORPORATION | 10.00 | 0.00 | 365 |
1992 | BELDEN & BLAKE CORPORATION | 5202.00 | 56.00 | 333 |
1993 | BELDEN & BLAKE CORPORATION | 5835.00 | 0.00 | 361 |
1994 | BELDEN & BLAKE CORPORATION | 4343.00 | 0.00 | 355 |
1995 | BELDEN & BLAKE CORPORATION | 3803.00 | 0.00 | 361 |
1996 | BELDEN & BLAKE CORPORATION | 3231.00 | 0.00 | 359 |
1997 | BELDEN & BLAKE CORPORATION | 3049.00 | 0.00 | 357 |
1998 | BELDEN & BLAKE CORPORATION | 2416.00 | 91.00 | 331 |
1999 | BELDEN & BLAKE CORPORATION | 2649.00 | 0.00 | 323 |
2000 | BELDEN & BLAKE CORPORATION | 2124.00 | 0.00 | 351 |
2001 | BELDEN & BLAKE CORPORATION | 1910.00 | 25.00 | 351 |
2002 | BELDEN & BLAKE CORPORATION | 1074.00 | 8.00 | 155 |
2003 | PETROX, INC | 1900.00 | 7.00 | 365 |
2004 | PETROX, INC | 1609.00 | 0.00 | 365 |
2005 | PETROX, INC | 1211.00 | 0.00 | 180 |
2006 | S & S ENERGY CORP | 1059.00 | 0.00 | 365 |
2007 | S & S ENERGY CORP | 1392.00 | 0.00 | 365 |
2008 | S & S ENERGY CORP | 1273.00 | 48.00 | 365 |
2009 | S & S ENERGY CORP | 1522.00 | 65.00 | 365 |
2010 | S & S ENERGY CORP | 1263.00 | 17.00 | 365 |
2011 | S & S ENERGY CORP | 1120.00 | 0.00 | 365 |
2012 | S & S ENERGY CORP | 1339.00 | 28.00 | 366 |
2013 | S & S ENERGY CORP | 997.00 | 0.00 | 365 |
2014 | S & S ENERGY CORP | 177.00 | 0.00 | 365 |
2015 | S & S ENERGY CORP | 19.00 | 0.00 | 30 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | RESOURCE AMERICA INC | Brine | 0 | 365 |
1990 | BELDEN & BLAKE CORPORATION | Brine | 0 | 181 |
1991 | BELDEN & BLAKE CORPORATION | Brine | 127 | 365 |
1992 | BELDEN & BLAKE CORPORATION | Brine | 58 | 333 |
1993 | BELDEN & BLAKE CORPORATION | Brine | 72 | 361 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 81 | 355 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 34 | 361 |
1996 | BELDEN & BLAKE CORPORATION | Brine | 43 | 359 |
1997 | BELDEN & BLAKE CORPORATION | Brine | 18 | 357 |
1998 | BELDEN & BLAKE CORPORATION | Brine | 43 | 331 |
1999 | BELDEN & BLAKE CORPORATION | Brine | 0 | 323 |
2000 | BELDEN & BLAKE CORPORATION | Brine | 33 | 351 |
2001 | BELDEN & BLAKE CORPORATION | Brine | 28 | 351 |
2002 | PETROX, INC | Brine | 18 | 56 |
2003 | PETROX, INC | Brine | 0 | 365 |
2004 | PETROX, INC | Brine | 0 | 365 |
2005 | PETROX, INC | Brine | 0 | 180 |
2006 | S & S ENERGY CORP | Brine | 0 | 365 |
2007 | S & S ENERGY CORP | Brine | 23 | 365 |
2008 | S & S ENERGY CORP | Brine | 157 | 365 |
2009 | S & S ENERGY CORP | Brine | 22 | 365 |
2010 | S & S ENERGY CORP | Brine | 66 | 365 |
2011 | S & S ENERGY CORP | Brine | 0 | 365 |
2012 | S & S ENERGY CORP | Brine | 78 | 366 |
2013 | S & S ENERGY CORP | Brine | 0 | 365 |
2014 | S & S ENERGY CORP | Brine | 0 | 365 |
2015 | S & S ENERGY CORP | Brine | 0 | 30 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-100228330 | 2015-11-20 0:00 | PB | No Violations | 6.00 |
-1709603060 | 2015-11-20 0:00 | PB | No Violations | 6.00 |
0000PL2430 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0100228330 | 2015-11-20 | Plug / Plug Back | No Violations | I was accompanied to the location by inspector Joe Zollars, please refer to his inspection report for details. |
0751885591 | 2015-11-19 | Plug / Plug Back | No Violations | I am on site accompanied by inspector Randy Akins to witness the plugging of this well. The bottom plug was set on 11/18/2015 from a depth of 4000-4300 feet. Today Ditty Well Service planed on having Formation Cementing setting the remainder of the plugs through the 4 1/2 inch diameter production casing. Ditty Well Service encountered problems when attempting to rip the 4 1/2 inch diameter casing. Ditty ripped at a depth of 4706. After the rip, Ditty pulled the pipe approximately 2 feet and the pipe started gaining weight. Shortly after gaining the weight the rig could not pull the string up hole any further. Ditty tried ripping the casing multiple times after this, however the casing remained seized in the hole. S&S decided to contact a wireline truck and scheduled to run a Bond log the following day to access the down hole complications. Plugging operations where then put on standby until the complications where resolved. |
1447859459 | 2015-11-18 | Plug / Plug Back | No Violations | On arrival on location I was accompanied by Inspector Joe Zollars. The plugging is being done by Ditty Well Service. The rig crew has ran the 1 1/2 inch tubing back into the wellbore. We will be setting the bottom plug at 5680 feet. |
1448044937 | 2015-11-19 | Plug / Plug Back | No Violations | I was accompanied to the location by inspector Joe Zollars, please refer to his inspection report for details. |
1448386204 | 2015-11-24 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig crew running 1 1/2 tubing into the wellbore to set the big lime plug at a depth of 4050 feet. Established circulation and pumped cement. Pulled tubing out of wellbore |
1448468526 | 2015-11-25 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig crew had perforated the 4 1/2 casing at 1450 to 1460 feet with 10 shots. Established circulation and set a 200 foot plug from 1470 feet to 1270 feet. Shot off the 4 1/2 inch casing at 1348 feet. Set a 100 foot rip plug. Pulled the 4 1/2 inch casing up to 252 feet and cemented to surface. |
1448625103 | 2015-11-25 | Plug / Plug Back | No Violations | Timco Wire Line Services perforated 10 shots (1 spf) from 1460 - 1450. The rig ran 1-1/2 tubing to 1480. Formation Cementing was on location to spot a plug over the perforations. The inspector that I was covering for arrived and I departed. |
1709603060 | 2015-11-20 | Plug / Plug Back | No Violations | Due to previous complications (explained in previous report), Timco Energy is on site to conduct a Bond log on the well bore. The Bond log indicated that the hole was collapsed at approximately 1460 feet. I contacted Inspector Todd Miller, to gather a plan of what should be done to properly plug this well. Todd insisted that Ditty Well Service try to rip the 4 1/2 inch diameter casing at different depths in hope of gaining the ability to pull the casing out of the hole. Then if casing could not be pulled tubing would be ran in to a depth of 4700 to set the lime plug, after that plug was set Ditty would then rip the casing at approximately 1450 enabling them to set the Berea and surface plug. |
2145485994 | 2018-04-24 | Final Restoration | No Violations | On the day of inspection, I found that the final restoration inspection has been completed. The site passed final restoration according to ORC 1509.072 (B). |
751885591 | 2015-11-19 0:00 | PB | No Violations | 9.00 |
PL2430 | PL | No Violations |
For data sources see[9]