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Well ID: 34-163-20155 | Loading map...
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Country: United States | |
State: Ohio | |
County: Vinton | |
Municipality: Harrison Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: GEARING BH | |
License Status: Storage Well | |
License Date: 1958-08-15 | |
Spud Date: 1958-08-15 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 1958-09-05 | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.260000 | |
Longitude: -82.650000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1958-08-15 | GL=642.6, STORAGE |
Completed | 1958-09-05 | GL=642.6, STORAGE |
Reached Total Depth | 1958-09-05 | GL=642.6, STORAGE |
Record Last Modified | 2014-02-24 | GL=642.6, STORAGE |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1019131854 | 2019-2-21 0:00: | SO | No Violations | 0.30 |
-59374092 | 2020-10-27 0:00 | SO | No Violations | 0.30 |
-819382974 | 2013-10-17 0:00 | SO | No Violations | 0.20 |
-978786528 | 2016-3-17 0:00: | SO | No Violations | 0.20 |
0306017616 | 2018-09-05 | Storage Well | No Violations | My Columbia Gas storage well inspection revealed the well had a legible identification. The lease road was in stable condition without substantial erosion. |
0629187847 | 2014-10-29 | Storage Well | No Violations | Storage well inspection. The well has a legible identification. No violations noted. |
0819382974 | 2013-10-17 | Storage Well | No Violations | No noted violations. |
0978786528 | 2016-03-17 | Storage Well | No Violations | Storage well inspection. The well has a legible identification. No violations noted. |
1019131854 | 2019-02-21 | Storage Well | No Violations | This Columbia Gas storage well is connected to the Columbia gas storage well system. Legible identification was posted. |
1268698804 | 2015-07-01 | Storage Well | No Violations | Storage well inspection. Legible well identification found at well. No violations found on date of inspection. |
1485178755 | 2017-01-09 | Storage Well | No Violations | Storage well inspection. The well has a legible identification. No violations noted. GPS was used to identify location of Storage Well. |
1773745350 | 2011-03-28 | Storage Well | No Violations | Upon arrival at the well head, leaking could be heard. It was coming from a flange that was at ground level. Notified Steve Hampshire and he promptly came to the location. He put a gauge on it and it read about 100 psi. He then told me that he has plugs in this well and there was only top end pressure. He then bled the pressure off and there was no storage gas smell. The well is scheduled for rework. |
306017616 | 2018-9-5 0:00:0 | SO | No Violations | 0.10 |
629187847 | 2014-10-29 0:00 | SO | No Violations | 0.50 |
For data sources see[4]