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34-163-20614

Well Details

Well ID: 34-163-20614
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Country: United States
State: Ohio
County: Vinton
Municipality: Knox Township
Operator Name: HOCKING HILLS ENERGY AND WELL
Well Pad ID:
Farm/Lease Name: STOUT KENNETH
License Status: Final Restoration
License Date: 2009-10-13
Spud Date: 1981-06-22
Spud Drilling Contractor:
Final Drill Date: 1981-06-27
Well Total Depth: 1236.00 ft
Configuration: Vertical
Latitude: 39.230000
Longitude: -82.310000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-06-04 566 GRIM PAUL A GeoDate 6/4/81
Original Spud 1981-06-22
Completed 1981-06-27
Reached Total Depth 1981-06-27
Change of Owner 2001-11-21 Operator changed from 566, GRIM PAUL A to 5755, CHIEFTAIN ENERGY CORP.
APP 2009-10-13 Proposed Formations:BEREA, Issued Date:10/13/2009, Expired Date:10/13/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2010-09-29
Construction Permit Expires 2010-10-13
Record Last Modified 2014-07-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1076 1081 2
1076 1081 2
1076 1081 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1000 Bbl 11000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TANSKY J/TANSKY OIL PROD 0.00 350.00 0
1985 ISON PROD SERVICES INC 0.00 160.00 90
1987 GRIM PAUL A 0.00 485.00 365
1988 GRIM PAUL A 0.00 316.00 365
1989 GRIM PAUL A 0.00 77.00 365
1990 GRIM PAUL A 0.00 450.00 365
1991 GRIM PAUL A 0.00 225.00 365
1992 GRIM PAUL A 0.00 196.00 365
1993 GRIM PAUL A 0.00 145.00 365
1994 GRIM PAUL A 0.00 106.00 365
1995 GRIM PAUL A 0.00 56.00 365
1996 GRIM PAUL A 0.00 20.00 365
1997 GRIM PAUL A 0.00 0.00 365
1998 GRIM PAUL A 0.00 0.00 365
1999 GRIM PAUL A 0.00 0.00 365
2000 GRIM PAUL A 0.00 0.00 365
2001 GRIM PAUL A 0.00 0.00 365
2002 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2003 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2004 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2005 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2006 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2007 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2008 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2009 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0
2010 HOCKING HILLS ENERGY AND WELL 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TANSKY J/TANSKY OIL PROD Brine 0 0
1985 ISON PROD SERVICES INC Brine 1800 90
1987 GRIM PAUL A Brine 4555 365
1988 GRIM PAUL A Brine 3010 365
1989 GRIM PAUL A Brine 899 365
1990 GRIM PAUL A Brine 1428 365
1991 GRIM PAUL A Brine 2648 365
1992 GRIM PAUL A Brine 994 365
1993 GRIM PAUL A Brine 910 365
1994 GRIM PAUL A Brine 410 365
1995 GRIM PAUL A Brine 220 365
1996 GRIM PAUL A Brine 0 365
1997 GRIM PAUL A Brine 0 365
1998 GRIM PAUL A Brine 0 365
1999 GRIM PAUL A Brine 0 365
2000 GRIM PAUL A Brine 15 365
2001 GRIM PAUL A Brine 0 365
2002 HOCKING HILLS ENERGY AND WELL Brine 0 0
2003 HOCKING HILLS ENERGY AND WELL Brine 0 0
2004 HOCKING HILLS ENERGY AND WELL Brine 0 0
2005 HOCKING HILLS ENERGY AND WELL Brine 0 0
2006 HOCKING HILLS ENERGY AND WELL Brine 0 0
2007 HOCKING HILLS ENERGY AND WELL Brine 0 0
2008 HOCKING HILLS ENERGY AND WELL Brine 0 0
2009 HOCKING HILLS ENERGY AND WELL Brine 0 0
2010 HOCKING HILLS ENERGY AND WELL Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1045460274 2005-10-3 0:00: PW No Violations
-1123150468 2010-9-17 0:00: AM No Violations
-1141338772 2008-2-5 0:00:0 PW No Violations
-1212923258 2004-10-7 0:00: PW No Violations
-1410153597 2008-10-3 0:00: PW No Violations
-1575008394 2008-4-3 0:00:0 PW No Violations
-1721322875 2008-4-25 0:00: AM No Violations
-179469770 2008-2-19 0:00: PW No Violations
-1800544467 2006-1-11 0:00: PW No Violations
-2016051595 2008-5-1 0:00:0 PW No Violations
-2037966068 2010-10-1 0:00: PB No Violations
-2063555802 2004-5-26 0:00: PW No Violations
-2118123817 2004-9-28 0:00: PW No Violations
-428575114 2004-7-19 0:00: PW No Violations
-45526981 2008-4-28 0:00: PW No Violations
-52994372 2002-3-6 0:00:0 PW No Violations
-889160327 2005-8-15 0:00: PW No Violations
001269i845 2002-03-06 Production Wells Violations Noted An inspection of the well revealed there is No ID at the well or tank battery, oily soil around well head, oil and oily soil in dike of tank battery. Dike does not meet requirements, not large enough. Dike size is 30x40x1, will hold 195 bbls of fluid, dike has 3-100bbl, 1-200bbl tanks. NEED FULL ID AT THE WELL AND TANK BATTERY, CLEAN UP ALL OIL, AND OILY SOIL AT WELL AND DIKE OF TANK BATTERY. BUILD A DIKE TO HOLD AT LEAST 220BBLS OF FLUID.
001269i908 2002-03-26 Production Wells No Violations Follow-up, Non-Compliance, met with Doug Kitchen.
0040269577 2005-10-17 Production Wells No Violations Follow-up on NOV, Non-Compliance, no action to plug or produce.
0045526981 2008-04-28 Production Wells No Violations An inspection revealed non-compliance.
0052994372 2002-03-06 Production Wells Violations Noted FOLLOW UP TO NOV # 1269i845 An inspection of the well revealed there is No ID at the well or tank battery, oily soil around well head, oil and oily soil in dike of tank battery. Dike does not meet requirements, not large enough. Dike size is 30x40x1, wi
01269i1022 2002-05-06 Production Wells No Violations Follow-up on NOV, In-Compliance.
0179469770 2008-02-19 Production Wells No Violations A follow-up inspection revealed that the flow line has been repaired. C&P has been removed.
0192803336 2008-04-02 Production Wells Violations Noted A complaint was received alleging that oil has been released from a broken flowline. The owner, Chieftain Energy was contacted and informed of the complaint. An inspection revealed that the oil release was the result of a ruptured flowline. Contamination and pollution was not observed outside the dike. A valve had been closed on a frac tank. As a result, the plastic line ruptured due to pressure. Chieftain Energy had previously stated that this tank was not being utilized. The company was observed on-site performing cleanup. They were instructed to remove oily soil and evaluate 100bbl tank that may contain a small leak underneath and rebuild dike. (1) 100bbl tank was found to be only 40ft from the road. The company states that they will not be utilizing this tank. In addition, the area is limited due a right of way located behind the tank battery.
0428575114 2004-07-19 Production Wells No Violations Follow-up, Non-Compliance.
0578541966 2008-04-29 Production Wells No Violations Met with Chieftain Energy to discuss related cleanup at tank battery location.
0602946304 2010-09-29 Plug / Plug Back No Violations Witnessed plugging activity with Mr. Robert Stonerock, South Region Oil & Gas Supervisor.
0731034567 2011-10-24 Final Restoration No Violations FOLLOW UP TO NOV # 1319630113 An inspection of the final restoration revealed an electric pole with service boxes on it is present on site. Pole needs to be removed from site. Mr. Doug Kitchen from Chieftain energy was called on Tuesday 10/25/11 at 9:30 am and notified of the problem. Mr. Kitchen agreed to comply next week.
0752225641 2007-10-17 Production Wells Violations Noted A complaint was received by the Division of Mineral Resources Management alleging that this well was idle. An inspection revealed that the well does not appear to be producing and identification is incomplete. Production records indicate that the last year of production was 1996. Landowner has not received any monies for several years. No electric for the motor on the well. The well owner, Mr. Doug Kitchen, states that he has not been producing this well and to send him a NOV.
0889160327 2005-08-15 Production Wells Violations Noted An inspection of the well revealed the well has been producing since 1996. Landowner has not received any monies for several years. No electric for motor on well.
0939628894 2008-04-18 Production Wells No Violations A follow-up inspection revealed non-compliance. C&P has not been removed.
1045460274 2005-10-03 Production Wells No Violations Non-Compliance, well still idle.
1104942620 2005-01-05 Production Wells No Violations Follow-up on NOV, In-Compliance
1123150468 2010-09-17 Administrative Inspection No Violations Attempts made to speak with Mr. Doug Kithen by telephone regarding plugging requirements were unsuccessful. Therefore, Mr. Ron McBride with Chieftain Energy was advised of requirements at 9:30 a.m.
1141338772 2008-02-05 Production Wells No Violations A follow-up inspection revealed that the leak from the flow line has not been repaired. The impacted area from this leak is approximately a 10x 15 area. Quantab (high range) reading reached a maximum unit of 10, which greatly exceeds the US EPA Secondary Drinking Water Standard of 250 milligrams per liter. Doug Kitchen was instructed to remove this soil from the site.
1202308848 2008-01-28 Production Wells Violations Noted A follow-up inspection revealed non-compliance. The well is still idle and no identification was observed. Mr. Doug Kitchen states that the well has been pumping, but had to repair the production line. The broken line was located approximately 150 feet behind the tank battery. At the time of the inspection, the production line (black plastic) was found to be leaking. The leak is a slow constant drip. Mr. Kitchen was informed by telephone to repair this line immediately and remove contamination and pollution.
1212923258 2004-10-07 Production Wells No Violations Follow-up on NOV, non-compliance, violations not corrected, well still idle, spoke with Doug Kitchen on the phone, he is hoping Paul Grim will take over well.
1247957173 2014-04-10 Final Restoration No Violations This is a follow-up/ final restoration for a piece of equipment left at the well site. During my inspection I was unable to find anything. The violation was from 2011. The well is in-compliance and the final restoration meets 1509.072.
1269i1022 2002-5-6 0:00:0 PW No Violations
1269i845 2002-3-6 0:00:0 PW No Violations
1269i908 2002-3-26 0:00: PW No Violations
1319630113 2011-10-24 Final Restoration Violations Noted An inspection of the final restoration revealed an electric pole with service boxes on it is present on site. Pole needs to be removed from site. Mr. Doug Kitchen from Chieftain energy was called on Tuesday 10/25/11 at 9:30 am and notified of the problem. Mr. Kitchen agreed to comply next week.
1410153597 2008-10-03 Production Wells No Violations An inspection revealed that valves are open at the well. Tanks empty at time of inspection.
1575008394 2008-04-03 Production Wells No Violations Met with complainant to discuss issues with associated well. A follow-up inspection revealed non-compliance at the tank battery. Chieftain Energy had been instructed to remove C&P. It was noted that C&P has been buried. The company was contacted by telephone and informed of inspection results.
1721322875 2008-04-25 Administrative Inspection No Violations Informed Doug Kitchen to remove oily soil inside dike. Mr. Kitchen was also instructed that once the cleanup has been performed, the 100bbl tank will need to be evaluated for leaks.
1800544467 2006-01-11 Production Wells No Violations Follow-up on NOV, IN-COMPLIANCE.
192803336 2008-4-2 0:00:0 PW No Violations
2016051595 2008-05-01 Production Wells No Violations An inspection revealed that cleanup has been performed. Met with the landowner to discuss inspection results and concerns.
2026373130 2008-03-18 Production Wells No Violations A follow-up inspection was conducted, in response to landowner complaint alleging that a flow line is leaking. During the inspection, it was noted that a black plastic flow line had separated inside the dike. Small amount of C&P was observed. The line appeared to be routed to the top of a 100 bbl tank. Chieftain Energy was contacted by telephone and stated that the line was not being utilized, but would perform repair and cleanup.
2037966068 2010-10-01 Plug / Plug Back No Violations An inspection revealed that cement remains at the surface inside 4.5 casing. The casing has been cut below grade with no ID plate at time of inspection. Oil remains in the pit containing a liner and will be pumped by Chieftain Energy.
2063555802 2004-05-26 Production Wells Violations Noted An inspection of the well revealed the well is idle and has not been producing for several years. According to production records well has not produced since 1998.
2118123817 2004-09-28 Production Wells No Violations Met with Doug Kitchen and Joe Hoerst, Doug said work was not done, at this time have no plans to plug or produce well.
40269577 2005-10-17 0:00 PW No Violations
578541966 2008-4-29 0:00: PW No Violations
602946304 2010-9-29 0:00: PB No Violations
731034567 2011-10-24 0:00 FR No Violations 1.00
752225641 2007-10-17 0:00 PW No Violations
939628894 2008-4-18 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
001269i845 US-OH-107474 2002-03-06 Well operation causing pollution and contamination
001269i845 US-OH-107475 2002-03-06 Failure to legibly identify well
001269i845 US-OH-107476 2002-03-06 No SPCC dike/or failure to keep dike free of water or oil
0052994372 US-OH-125789 2002-03-06 Well operation causing pollution and contamination
0052994372 US-OH-125790 2002-03-06 Failure to legibly identify well
0052994372 US-OH-125791 2002-03-06 No SPCC dike/or failure to keep dike free of water or oil
0192803336 US-OH-119412 2008-04-07 Well operation causing pollution and contamination
0752225641 US-OH-128550 2007-10-26 Failure to legibly identify well
0752225641 US-OH-128551 2007-10-26 Well shall be plugged
0889160327 US-OH-130158 2005-08-15 Well shall be plugged
0889160327 US-OH-130159 2005-08-15 Urban - failure to meet tank battery setbacks from mandatory pooled property
1202308848 US-OH-105302 2008-02-06 Inadequate pipeline strength
1319630113 US-OH-109112 2014-04-23 Failure to remove production equip. within 6 mos. REPLACE
2063555802 US-OH-121031 2004-05-28 Well shall be plugged

For data sources see[9]

References