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34-163-20783

Well Details

Well ID: 34-163-20783
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Country: United States
State: Ohio
County: Vinton
Municipality: Madison Township
Operator Name: STOUT GENN DBA OHIO VALLEY DRI
Well Pad ID:
Farm/Lease Name: STOUT
License Status: Final Restoration
License Date: 2016-02-19
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 39.270000
Longitude: -82.380000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-09-15 1208 STOUT G dba/OH VALLEY DRL GeoDate 9/15/82
Oil and Gas 1982-09-15 Issued Date 9/15/82 Expired Date 3/15/83 Acres 0069610 Tool Type CT Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000
APP 2016-02-19 Proposed Formations:BEREA, Issued Date:2/19/2016, Expired Date:2/18/2018 12:00:00 PM, Drilling unit acres:1, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2017-11-16 An inspection of the well revealed well is idle and incapable of producing, according to owner of well, well has not been drilled to a producing formation, well depth is approx 600'ft, Mr. Stout thinks he may plug well. PERMIT EXPIRED.
Construction Permit Expires 2018-02-18 An inspection of the well revealed well is idle and incapable of producing, according to owner of well, well has not been drilled to a producing formation, well depth is approx 600'ft, Mr. Stout thinks he may plug well. PERMIT EXPIRED.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1051202333 2008-3-20 0:00: PW No Violations
-1083316135 2008-3-20 0:00: PW No Violations
-10833161358888 2008-3-20 0:00: DD No Violations
-108331613599 2008-3-20 0:00: PW No Violations
-1124996708 2008-4-2 0:00:0 AM No Violations
-1156828128 2007-5-31 0:00: PW No Violations
-1222598365 2008-3-20 0:00: PW No Violations
-1247674740 2009-9-2 0:00:0 AM No Violations
-126177177 2008-3-20 0:00: DD No Violations
-1430662791 2011-1-18 0:00: PW No Violations 0.50
-1708343501 2009-10-29 0:00 PW No Violations
-1850983228 2009-6-17 0:00: AM No Violations
-1946670781 2010-5-12 0:00: PW No Violations
-2016628021 2008-3-20 0:00: DD No Violations
-2121628697 2008-7-29 0:00: PW No Violations
-445120324 2011-12-30 0:00 PW No Violations 1.50
-533354409 2015-1-13 0:00: PW No Violations 1.00
-636440241 2009-9-1 0:00:0 AM No Violations
-810202560 2008-8-15 0:00: PW No Violations
-894426036 2008-3-20 0:00: DD No Violations
-91222332 2016-11-2 0:00: PW No Violations 3.00
0091222332 2016-11-02 Production Wells No Violations Chiefs order follow-up. The well consists of 8.62 casing. The well was drilled to approx. 600 and was never completed. I met with well owner Glenn Stout during my inspection. The rig has been moved off the hole and a road has been built to allow access to the well. New photographs were taken during my inspection.
0126177177 2008-03-20 Drill / Deepen / Reopen No Violations FOLLOW UP TO NOV # -10833161358888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout.
0224560292 2017-01-09 Final Restoration No Violations Final restoration inspection. The well was plug on affidavit by Keith Wright. Cemenco used 128 sacks of cement to plug the well from bottom to surface. The well was cut off 30 inches below grade and capped with a plate that had the API number welded on the plate. The area has been reclaimed. The well site meets minimum standards for final restoration.
0445120324 2011-12-30 Production Wells No Violations Status of well remains the same as last inspection. Fluid level about 2 seconds down. Left business card and note to call me on front door of Mr. Stouts house.
0533354409 2015-01-13 Production Wells No Violations Compliance follow-up. The well remains unplugged. The well was partially plugged by owner Glenn Stout. Mr. Stout has not taken any action to plug the well properly and bring the well into compliance.
0544208727 2009-02-17 Production Wells No Violations A follow-up inspection revealed non-compliance. No action has been taken to resolve violations. The status of this well has not changed since the last inspection.
0617239993 2005-09-07 Production Wells Violations Noted FOLLOW UP TO NOV # 1126530166 An inspection of the well revealed well is idle and incapable of producing, according to owner of well, well has not been drilled to a producing formation, well depth is approx 600ft, Mr. Stout thinks he may plug well.
0630148871 2009-03-31 Production Wells No Violations A follow-up inspection revealed non-compliance. The well status remains the same and no action has been taken by the company to comply with Chiefs Order.
0636440241 2009-09-01 Administrative Inspection No Violations Received voice mail message from Mr. Glenn Stout at 7:42 am stating that he attempted to plug a well back a little bit and plugged it clear back. Further states that he will give me a call another time. Returned Mr. Stouts call at 5:51 pm. No answer. Left message stating that a permit is required and to return my call. I would like to know more details about material, and total depth.
0787323897 2013-11-21 Production Wells No Violations Compliance notice follow up, Nothing has been done to properly plug the well. The compliance notice cannot be satisfied.
0810202560 2008-08-15 Production Wells No Violations A follow-up inspection was conducted with Dan Goins. The well status has not changed since the last inspection. Attempts to speak with Mr. Stout directly have not been successful.
0894426036 2008-03-20 Drill / Deepen / Reopen No Violations FOLLOW UP TO NOV # -10833161358888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout.
0923191188 2010-08-09 Production Wells No Violations A follow-up inspection revealed non-compliance. The status of this well has not changed since the last inspection. No action or communication has been received from Mr. Glenn Stout. To date. Mr. Stout has also failed to file permit application with the Division. A note was left for Mr. Stout stating that the Division will pursue further enforcement action, if unwilling to cooperate.
0931601315 2009-12-22 Production Wells No Violations A follow-up inspection to Chiefs order revealed non-compliance. No action has been taken by Mr. Glenn Stout to resolve violations. The status of the well remains unchanged. A dozer that had been observed on the well site has now been moved off location. At conclusion of inspection, I spoke Mr. Stout whom, was in the process of leaving for work. I asked Mr. Stout how much time he will need to achieve compliance, another month? He states that attempts to find a contractor have not been successful. The individual he had in mind who drills water wells does not appear to be interested. I reminded Mr. Stout that a permit has not been received. Mr. Stout states that he could obtain a permit in a month and is thinking work could be performed after winter. Management will informed of status.
1008438783 2008-03-20 Drill / Deepen / Reopen No Violations FOLLOW UP TO NOV # -1083316135888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not vali
1051202333 2008-03-20 Production Wells No Violations FOLLOW UP TO NOV # -108331613599 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout.
1055022477 2008-11-04 Administrative Inspection No Violations An attempt to meet with Mr. Glenn Stout was not successful.
1083316135 2008-03-20 Production Wells Violations Noted An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout. A previous inspections conducted on 9/7/2005, showed that this well was never drilled to a producing formation. At the time of the inspection, the well was idle and not capable of production. According to the report, the depth at the time of the inspect
1124996708 2008-04-02 Administrative Inspection No Violations Hand delivered NOV to Mr. Glenn Stout.
1126530166 2005-09-07 Production Wells Violations Noted An inspection of the well revealed well is idle and incapable of producing, according to owner of well, well has not been drilled to a producing formation, well depth is approx 600ft, Mr. Stout thinks he may plug well.
1156828128 2007-05-31 Production Wells No Violations An inspection revealed that the well does not appear to have been plugged. No plugging report observed in RBDMS. Cable Tool Rig observed on-site. The owner, Mr. Glenn Stout, will be contacted. The current telephone number in RBDMS is not valid. Once the owner is contacted a new NOV will be issued.
1168746483 2009-05-01 Production Wells No Violations A follow-up inspection conducted with Oil & Gas Supervisor, Mr. Robert Stonerock revealed non-compliance. It was noted that the status of this well has not changed. No action has been taken by the well owner to achieve compliance.
1222598365 2008-03-20 Production Wells No Violations FOLLOW UP TO NOV # -1051202333 FOLLOW UP TO NOV # -108331613599 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout.
1247674740 2009-09-02 Administrative Inspection No Violations At 8:00 am, I called Mr. Glenn Stout. My last call on 9/1/09 at 5:51 pm was never returned. No answer and left message stating for him to return my call.
1254159679 2009-09-28 Administrative Inspection No Violations Met with Mr. Glenn Stout today at the Jackson Office today. Mr. Stout confirmed that the total depth of this well was 600. Mr. Stout states that the casing inside the well bore consists only of 10 of 8 and is open hole. He believes there is cave in around #2 Coal. Mr. Stout states that he plugged the well back in August with crushed lime dust. He was informed that this material is not approved and must be clay from an approved source. Contact information from approved list was provided to Mr. Stout. Contacted Mr. Robert Stonerock, Oil & Gas South Region Supervior, by telephone at 12:59 pm while, Mr. Stout was in attendence. After speaking with Mr. Stonerock Mr. Stout states that he will be cleaning out the well. I informed Mr. Stout that he would need to reach 600. Mr. Stout was also advised that a pit with a liner would be required.
1345215070 2012-08-14 Administrative Inspection No Violations Spoke with Mr. Glen Stout in person and discussed why he hasnt plugged his well yet. He claimed that he couldnt get anyone to do it and that clay was not available. I mentioned that a nearby company had a cable tool rig that he may be able to hire to drill it out and he stated that he would make a phone call to them. Accompanied by inspector Morgan Button.
1430662791 2011-01-18 Production Wells No Violations An inspection revealed well status remains unchanged. No recent communication have been received from the well owner, Mr. Glenn Stout. Mr. Stout has also failed to file for a plugging permit. New photographs were obtained from this inspection. Made an attempt to visit with Mr. Stout but no answer at his residence. Left business card with note requesting a call to discuss well status.
1430751077 2015-05-04 Production Wells No Violations Compliance notice follow-up. The condition of the well has not changed. The 8 casing is above grade and open. There is a old service rig set next to the well. Pictures were taken in preparation of issuing a chiefs order.
1473276761 2016-09-07 Production Wells No Violations Compliance notice follow-up. The well consists of a 8.62 casing that is open to the atmosphere. No other casing are present. The well was drilled to approx. 600 but never completed. No attempt has been made to bring the well into compliance. I attempted to contact the well owner Mr. Glenn Stout concerning his lack of action in regards to plugging the well. New photographs were taken and sent to Regional Supervisor Dan Goins.
1483030871 2016-12-29 Plug / Plug Back No Violations I received a call from rig owner Keith Smith. Keith stated he had moved his rig on site on 12-28-2016 and would drill out the limestone dust that was in the wellbore. Smith Drilling ran a 6.5 inch diameter bit on drill string to 492 feet where they encountered sold rock. No limestone dust was found in the well bore. Well owner Glen Stout was present and stated he had used approx. 1 ton of limestone dust to partially plug the well. The coal seam may have taken the limestone dust as none were encountered when the wellbore was cleaned out. Cement contractor Cemenco is due to plug the well on 1-2-2017.
1486045025 2010-08-11 Administrative Inspection No Violations Mr. Glenn Stout called today at 7:39 a.m. in response to the note left from 8/9/2010 inspection. Mr. Stout states he has not had this work at the top of his priority list. Further stating that he was helping an old judge move and sell his home. He still needs to mow the grass too. Mr. Stout was informed of SB 165 and to cooperate to avoid further enforcement action. Mr. Stout responded by stating why have things not been done on other wells around the area? Mr. Stout was informed that this conversation is about his well: plugging without a permit, and plugging with unapproved material. Asked about a timeframe needed to achieve compliance, Mr. Stout was unable to provide me with a date. Mr. Stout states that he cant find a spudder rig therefore, he was given a list of names to call. Informed Mr. Stout to begin by applying for a permit.
1507521900 2009-09-15 Production Wells No Violations A follow-up inspection with Mr. Robert Stonerock, Oil & Gas South Region Supervisor, revealed non-compliance. The well status remains the same as last inspection.
1521407924 2008-03-20 Drill / Deepen / Reopen No Violations FOLLOW UP TO NOV # -126177177 FOLLOW UP TO NOV # -10833161358888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout.
1531036968 2008-03-20 Production Wells No Violations FOLLOW UP TO NOV # -1083316135 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not valid. It is believed that the owner, Mr. Glenn Stout, lives near the well site. A business card was left at this residence stating that a prior NOV had been issued in 2005 to plug or produce this well. Previous inspection in 2005 states that this well was never drilled to a producing formation and depth was 600 feet. A new NOV will be hand delivered to Mr. Stout. A previous inspections conducted on 9/7/2005, showed that this well was never drilled to a producing formation. At the time of the inspection, the well was idle and not capable of production. According to the report, the depth at the time of the inspect
1560028388 2009-09-03 Production Wells No Violations At 7:55 am, I called Mr. Glenn Stout. No answer. Left message stating for him to return my call. An inspection was also conducted today. No observed activity. The status remains the same as noted on 8/31/09. Solid obstruction down approx 1 second.
1576418267 2011-02-08 Production Wells No Violations A follow-up inspection conducted with Mr. Andy Thomas revealed non-compliance.
1663292086 2008-03-20 Production Wells No Violations FOLLOW UP TO NOV # -108331613599 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not vali
1690729618 2008-03-20 Drill / Deepen / Reopen No Violations FOLLOW UP TO NOV # 1008438783 FOLLOW UP TO NOV # -1083316135888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not vali
1708343501 2009-10-29 Production Wells No Violations A follow-up inspection revealed non-compliance. The well status remains unchanged from last inspection. To date, no plugging permit has been received.
1778808835 2008-04-24 Production Wells No Violations Made attempt to visit with Mr. Stout. A left business card was left at residence.
1850983228 2009-06-17 Administrative Inspection No Violations On 6/17/2009, an attempt to contact Mr. Glenn Stout by telephone at 11:23 AM was not successful. A voice mail message therefore, was left stating that this well is not in-compliance and would not be considered a water well per inspection with Oil and Gas South Region District Supervisor, Mr. Robert Stonerock. Mr. Stout was instructed to contact me immediately.
1859805610 2008-03-20 Production Wells No Violations FOLLOW UP TO NOV # 1663292086 FOLLOW UP TO NOV # -108331613599 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not vali
1946670781 2010-05-12 Production Wells No Violations A follow-up inspection revealed non-compliance. The well status remains unchanged and no permit to date has been received. An attempt to visit with Mr. Stout at his residence revealed no answer.
2006529054 2009-10-09 Production Wells No Violations A follow-up inspection revealed non-compliance. No activity and well status remains the same as noted in last inspection.
2016628021 2008-03-20 Drill / Deepen / Reopen Violations Noted FOLLOW UP TO NOV # 2085237387 FOLLOW UP TO NOV # -10833161358888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not vali
2085237387 2008-03-20 Drill / Deepen / Reopen No Violations FOLLOW UP TO NOV # -10833161358888 An inspection revealed that no action has been taken to plug or produce this well. The drilling permit has expired. A Cable Tool Rig was observed on-site. Fluid is down approximately 2 seconds. Contact information for the owner, in RBDMS, is not vali
2100967837 2009-08-31 Plug / Plug Back Violations Noted A follow-up inspection revealed well owner plugging with no permit, failure to notify and utilizing unapproved material. The total depth has not been verified as no well completion report exists for this well. A white plastic bucket with hole in bottom has been placed over top of casing. Material observed, in bucket, around outside top of casing. A pile of this material also observed on ground surface. Solid obstruction down approx 1 second. A dozer was observed at the location. The well site location has now been graded. Old service rig still remains on site. The associated tools for this rig that had been observed on the ground surface have been picked up. After inspection, an attempt to visit with Mr. Stout at his house was not successful. Therefore, a note was left for Mr. Stout stating permit required, activity must be witnessed, material must be approved and question asked about the total depth.
2121628697 2008-07-29 Production Wells No Violations A follow-up inspection revealed non-compliance.
224560292 2017-1-9 0:00:0 FR No Violations 5.00
544208727 2009-2-17 0:00: PW No Violations
617239993 2005-9-7 0:00:0 PW No Violations
630148871 2009-3-31 0:00: PW No Violations
787323897 2013-11-21 0:00 PW No Violations 4.00
923191188 2010-8-9 0:00:0 PW No Violations
931601315 2009-12-22 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0617239993 US-OH-126970 2005-09-12 Well shall be plugged
0617239993 US-OH-126971 2005-09-12 Urban - failure to meet tank battery setbacks from mandatory pooled property
1083316135 US-OH-101887 2008-03-27 Failure to drill in accordance with plans
1083316135 US-OH-101888 2008-03-21 Well shall be plugged
1083316135 US-OH-101889 2008-03-27 Illegal/Unauthorized annular disposal of brine
1126530166 US-OH-103191 2005-09-12 Well shall be plugged
1126530166 US-OH-103192 2005-09-12 Urban - failure to meet tank battery setbacks from mandatory pooled property
2016628021 US-OH-120484 2018-03-23 Well shall be plugged
2100967837 US-OH-121468 2009-09-03 Failure to notify inspector
2100967837 US-OH-121469 2009-09-03 Plugging with unapproved materials
2100967837 US-OH-121470 2009-09-25 Failure to place clay plugs at designated intervals
2100967837 US-OH-121471 2009-09-03 Plugging without a permit
2100967837 US-OH-121472 2009-09-25 Failure to file plug report in 30 days

For data sources see[3]

References