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34-163-20947

Well Details

Well ID: 34-163-20947
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Country: United States
State: Ohio
County: Vinton
Municipality: Knox Township
Operator Name: BANCEQUITY PETROLEUM CORPORATI
Well Pad ID:
Farm/Lease Name: AKERS K ET AL
License Status: Producing
License Date: 2012-02-15
Spud Date: 2012-02-20
Spud Drilling Contractor: BOWMAN DRILLING
Final Drill Date: 2012-02-22
Well Total Depth: 1225.00 ft
Configuration: Vertical
Latitude: 39.240000
Longitude: -82.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-07-11 Proposed Formations:BEREA, Issued Date:7/11/2008, Expired Date:7/11/2009 6:00:00 AM, Drilling unit acres:11, Proposed Well Type:OG, Proposed Well Class:POOL
APP 2012-01-05 Proposed Formations:BEREA, Issued Date:1/5/2012, Expired Date:1/4/2014 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Correction to Well 2012-01-11 CORRECTION TO CASING PROGRAM, ADDED CODE 54.
APP 2012-02-15 Proposed Formations:BEREA, Issued Date:2/15/2012, Expired Date:2/14/2014 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2012-02-22
Completion Report Received 2012-03-27
Construction Permit Expires 2014-02-14
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2012-04-12 1024 1040 17
1024 1040 17
1024 1040 17

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-03-05 H2O 15 34681 Gal 17000 Producers Service Corporation
2012-03-05 H2O 15 34681 Gal 17000 Producers Service Corporation Witnessed first hour of job. Accompanied by inspector Kip Thompson. Average treatment rate was 3 barrels per minute.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 0
2012 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 312
2013 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365
2014 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365
2015 BANCEQUITY PETROLEUM CORPORATI 0.00 51.00 365
2016 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365
2017 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365
2018 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 BANCEQUITY PETROLEUM CORPORATI Brine 0
2012 BANCEQUITY PETROLEUM CORPORATI Brine 651 312
2013 BANCEQUITY PETROLEUM CORPORATI Brine 1375 365
2014 BANCEQUITY PETROLEUM CORPORATI Brine 10255 365
2015 BANCEQUITY PETROLEUM CORPORATI Brine 2495 365
2016 BANCEQUITY PETROLEUM CORPORATI Brine 1354 365
2017 BANCEQUITY PETROLEUM CORPORATI Brine 1357 365
2018 BANCEQUITY PETROLEUM CORPORATI Brine 921 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1287647759 2012-2-21 0:00: DD No Violations 1.50
-1580242960 2012-3-8 0:00:0 DD No Violations 2.00
-1591907510 2012-2-22 0:00: DD No Violations 4.00
-807176186 2012-3-5 0:00:0 DD No Violations 3.00
0807176186 2012-03-05 Drill / Deepen / Reopen No Violations Witnessed beginning stages of frac job.
1287647759 2012-02-21 Drill / Deepen / Reopen No Violations Checked on rig status. Total depth was at 796 feet. Surface casing would be cemented later that evening.
1331144981 2012-02-28 Drill / Deepen / Reopen No Violations Checked status of pit closure. Pits had been emptied of fluid.
1580242960 2012-03-08 Drill / Deepen / Reopen No Violations Met with Mr. Mike McPeak to pick up frac ticket.
1591907510 2012-02-22 Drill / Deepen / Reopen No Violations Witnessed running and cementing of the production string. Good circulation was achieved. Accompanied by Inspector Kip Thompson.
1687164155 2012-08-02 Production Wells No Violations No violations were noted at the time of inspection. Accompanied by inspector Morgan Button.
1786901377 2012-06-14 Preliminary Restoration No Violations Site has been graded, seeded and strawed. Well was pumping at the time of inspection.
1788135389 2012-04-18 Preliminary Restoration No Violations Preliminary restoration not yet completed. Grading needs to be done on the site. Well has been completed and was pumping at the time of inspection. Talked to Mr. Mike McPeak about it and he plans on working on it this week.
1897810311 2012-02-21 Drill / Deepen / Reopen No Violations Witnessed cementing of surface casing. Good circulation was achieved and good returns were witnessed. Cement fell back after the job was finished. It was topped off, and it stayed up after that.

For data sources see[9]

References