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34-167-22978

Well Details

Well ID: 34-167-22978
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Country: United States
State: Ohio
County: Washington
Municipality: Watertown Township
Operator Name: ANDERSON BOBBY B
Well Pad ID:
Farm/Lease Name: KELLER RAYMOND & RUDY
License Status: Producing
License Date: 1965-10-15
Spud Date: 1965-11-01
Spud Drilling Contractor:
Final Drill Date: 1965-12-01
Well Total Depth:
Configuration: Vertical
Latitude: 39.460000
Longitude: -81.640000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1965-11-01 INSPECTED BY CINDY VAN DYKE ON MAY 7, 2004. INSPECTION FOUND THAT OIL HAD SPILLED FROM A STORAGE TANK AT ROAD, LOST APPROX. 40-65 BARRELS AS THE VALVE AT BOTTOM OF TANK LET GO. OIL RAN APPROX. 2 MILES DOWNSTREAM IN WOLF CREEK; BOOMS WERE SET AND APPROX. 25-30 BARRRELS WERE RECOVERED. WELL IS PRODUCING WITH JACK, NEEDS AN ID AND A DIKE. OWNER IS JOHN MURPHY OF LANCASTER, OH.
Completed 1965-12-01 INSPECTED BY CINDY VAN DYKE ON MAY 7, 2004. INSPECTION FOUND THAT OIL HAD SPILLED FROM A STORAGE TANK AT ROAD, LOST APPROX. 40-65 BARRELS AS THE VALVE AT BOTTOM OF TANK LET GO. OIL RAN APPROX. 2 MILES DOWNSTREAM IN WOLF CREEK; BOOMS WERE SET AND APPROX. 25-30 BARRRELS WERE RECOVERED. WELL IS PRODUCING WITH JACK, NEEDS AN ID AND A DIKE. OWNER IS JOHN MURPHY OF LANCASTER, OH.
Reached Total Depth 1965-12-01 INSPECTED BY CINDY VAN DYKE ON MAY 7, 2004. INSPECTION FOUND THAT OIL HAD SPILLED FROM A STORAGE TANK AT ROAD, LOST APPROX. 40-65 BARRELS AS THE VALVE AT BOTTOM OF TANK LET GO. OIL RAN APPROX. 2 MILES DOWNSTREAM IN WOLF CREEK; BOOMS WERE SET AND APPROX. 25-30 BARRRELS WERE RECOVERED. WELL IS PRODUCING WITH JACK, NEEDS AN ID AND A DIKE. OWNER IS JOHN MURPHY OF LANCASTER, OH.
Change of Owner 2010-12-16 Operator changed from 516, MURPHY OIL CO to 422, ANDERSON BOBBY B
Record Last Modified 2013-10-03 INSPECTED BY CINDY VAN DYKE ON MAY 7, 2004. INSPECTION FOUND THAT OIL HAD SPILLED FROM A STORAGE TANK AT ROAD, LOST APPROX. 40-65 BARRELS AS THE VALVE AT BOTTOM OF TANK LET GO. OIL RAN APPROX. 2 MILES DOWNSTREAM IN WOLF CREEK; BOOMS WERE SET AND APPROX. 25-30 BARRRELS WERE RECOVERED. WELL IS PRODUCING WITH JACK, NEEDS AN ID AND A DIKE. OWNER IS JOHN MURPHY OF LANCASTER, OH.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 579 610 0
579 610 0
579 610 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 190 Lbs 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2016 ANDERSON BOBBY B 0.00 0.00 365
2017 ANDERSON BOBBY B 0.00 0.00 365
2018 ANDERSON BOBBY B 0.00 4.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2016 ANDERSON BOBBY B Brine 0 365
2017 ANDERSON BOBBY B Brine 0 365
2018 ANDERSON BOBBY B Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1101998319 2004-11-16 Production Wells No Violations Inspection this day found well with jack capable of producing, owner is Murphy Oil, ship tank at highway, stock tank?, needs IDs when get permit no. Will send to Mike
1101998319176063 2004-11-16 0:00 PW No Violations
1617655339 2004-05-07 Production Wells No Violations Inspection this day found oil had spilled from storage tank at road, tank was full and ready to sell, lost approx. 40-65 bbl - valve at bottom of tank let go. Well is in production with jack, tank needs IDs, now a dike, oil ran approx 2 miles downstream in Wolf Creek. Booms have been set and approx. 25-30 bbl. have been recovered. John Murphy is operator, told him needs to get IDs on tank, build dike, clean up spill. Will give him time to comply.

For data sources see[9]

References