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Well ID: 34-167-23143 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Barlow Township | |
Operator Name: CONLEY ENERGY CO LLC | |
Well Pad ID: | |
Farm/Lease Name: ROM ROACH | |
License Status: Final Restoration | |
License Date: 2017-06-14 | |
Spud Date: 1967-12-14 | |
Spud Drilling Contractor: | |
Final Drill Date: 1967-12-29 | |
Well Total Depth: 1100.00 ft | |
Configuration: Vertical | |
Latitude: 39.420000 | |
Longitude: -81.690000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1967-12-14 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Completed | 1967-12-29 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Reached Total Depth | 1967-12-29 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Completion Report Received | 1968-01-11 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Change of Owner | 2008-08-14 | Operator changed from 3434, GONZOIL INC to 8404, CONLEY ENERGY CO LLC |
APP | 2017-06-14 | Proposed Formations:1ST, 2ND & 3RD SALT SANDS, Issued Date:6/14/2017, Expired Date:6/14/2019 12:00:00 PM, Drilling unit acres:168, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-06-21 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Record Last Modified | 2018-03-06 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
Construction Permit Expires | 2019-06-14 | GL=745.56. UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2000 | GONZOIL INC | 650.00 | 0.00 | 365 |
2001 | GONZOIL INC | 139.00 | 0.00 | 365 |
2002 | GONZOIL INC | 28.00 | 0.00 | 365 |
2003 | GONZOIL INC | 126.00 | 0.00 | 365 |
2004 | GONZOIL INC | 0.00 | 0.00 | 0 |
2005 | GONZOIL INC | 0.00 | 0.00 | 0 |
2006 | GONZOIL INC | 0.00 | 0.00 | 0 |
2007 | GONZOIL INC | 0.00 | 0.00 | 0 |
2008 | GONZOIL INC | 0.00 | 0.00 | 0 |
2012 | CONLEY ENERGY CO LLC | 0.00 | 0.00 | 363 |
2013 | CONLEY ENERGY CO LLC | 0.00 | 0.00 | 0 |
2014 | CONLEY ENERGY CO LLC | 0.00 | 0.00 | 0 |
2015 | CONLEY ENERGY CO LLC | 0.00 | 0.00 | 0 |
2016 | CONLEY ENERGY CO LLC | 0.00 | 0.00 | 0 |
2017 | CONLEY ENERGY CO LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2000 | GONZOIL INC | Brine | 0 | 365 |
2001 | GONZOIL INC | Brine | 0 | 365 |
2002 | GONZOIL INC | Brine | 0 | 365 |
2003 | GONZOIL INC | Brine | 0 | 365 |
2004 | GONZOIL INC | Brine | 0 | 0 |
2005 | GONZOIL INC | Brine | 0 | 0 |
2006 | GONZOIL INC | Brine | 0 | 0 |
2007 | GONZOIL INC | Brine | 0 | 0 |
2008 | GONZOIL INC | Brine | 0 | 0 |
2012 | CONLEY ENERGY CO LLC | Brine | 0 | 363 |
2013 | CONLEY ENERGY CO LLC | Brine | 0 | 0 |
2014 | CONLEY ENERGY CO LLC | Brine | 0 | 0 |
2015 | CONLEY ENERGY CO LLC | Brine | 0 | 0 |
2016 | CONLEY ENERGY CO LLC | Brine | 0 | 0 |
2017 | CONLEY ENERGY CO LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1302254414 | 2017-6-21 0:00: | PB | No Violations | 6.50 |
-1631887537 | 2017-6-21 0:00: | PB | No Violations | 8.00 |
-1771319369 | 2016-12-15 0:00 | PW | No Violations | 2.00 |
-528729923 | 2016-12-15 0:00 | AM | No Violations | 0.30 |
-903595715 | 2017-10-17 0:00 | PB | No Violations | |
0416486047 | 2017-06-19 | Production Wells | No Violations | Dave Kale currently has his rig on this well in order to plug the well. Dave had a permit expedited to DNR Columbus to plug this well a couple of weeks ago and I received an e-mail saying I should have it by 6/19/17. I received a call from Dave today asking me the status of the permit on this well and I informed him that we should have it done by the end of today. Dave is going to dig a pit and line the pit in the next few days to be ready to plug this well once the permit is received. |
0528729923 | 2016-12-15 | Administrative Inspection | No Violations | I called the listed number 304-481-1199 and left a message about this well. In the message I asked for a return call and left my cell number. |
0860010314 | 2017-10-17 | Plug / Plug Back | No Violations | This well has been plugged and the Washington County inspector Brian has asked me to close this compliance notice |
0884994452 | 2004-03-29 | Production Wells | No Violations | Inspection this day found no violations, well tied into line and producing with jack, no meter found, tank area clean, may not be used, good IDs, good dike |
0903595715 | 2017-10-17 | Plug / Plug Back | No Violations | This well was plugged on 6/21/17 to surface. The inspection this day revealed that this well has had the wellhead cut off and all production equipment removed. The well is now in compliance and has been plugged to surface. |
1302254414 | 2017-06-21 | Plug / Plug Back | No Violations | I was on location at this well with Inspector Bill Stolarik to plug this well. Dave Kale was on location with his rig to pull tubing as the well was plugged. Formation Cementing was on location to cement the well in. All cement was set in the hole using 2 3/8 inch diameter non upset tubing. Formation set a bottom hole plug from 1125 to 761 feet inside 6 3/4 inch diameter hole and 100 feet inside 8 5/8 inch diameter surface casing using 105 sacks of Class A cement with 1% NaCl and cotton seed hulls. We then pulled 24 joint of tubing and ran the rigs sinker rod into the hole to check height of cement top. We then set our surface plug from 400 feet to surface inside 8 5/8 inch diameter surface casing with 104 sacks of Class A cement with 2% NaCL and cotton seed hulls. |
1434036785 | 2018-02-27 | Final Restoration | No Violations | The inspection this day was for a final restoration check. All production equipment has been removed, vegetation has been established, the wellhead is buried, and roadways have been restored. This well has passed final restoration. |
1631887537 | 2017-06-21 | Plug / Plug Back | No Violations | -On site inspection to witness the well plugging process with a service rig on the hole owned by Dave Kale and Formation Cementing. The rig has pulled the 2 diameter 10 round tubing and ran the tubing back into the well bore to a depth of 1,125, the well is equipped with 8.625 diameter surface casing only set to 761 according to records. A 21.5 barrel bottom plug was set to cover the open hole below the 8.625 surface and 100 above the 8.625 shoe, the plug consisted of 105 sacks of class A cement with 1% calcium and 1% gel additives. The tubing was pulled up to 400 and the plug top tagged at 660 with the rigs wireline through the tubing. A surface plug was then set from 400 to surface. |
1771319369 | 2016-12-15 | Production Wells | Violations Noted | |
416486047 | 2017-6-19 0:00: | PW | No Violations | 1.00 |
860010314 | 2017-10-17 0:00 | PB | No Violations | 0.30 |
884994452 | 2004-3-29 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1771319369 | US-OH-117635 | 2017-10-23 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
1771319369 | US-OH-117636 | 2017-10-23 | NONE | Well shall be plugged |
For data sources see[7]