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34-167-23757

Well Details

Well ID: 34-167-23757
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Country: United States
State: Ohio
County: Washington
Municipality: Waterford Township
Operator Name: LAKESIDE INC
Well Pad ID:
Farm/Lease Name: ULLMAN H W
License Status: Final Restoration
License Date: 2014-09-19
Spud Date: 1978-04-15
Spud Drilling Contractor:
Final Drill Date: 1978-05-15
Well Total Depth: 5620.00 ft
Configuration: Vertical
Latitude: 39.550000
Longitude: -81.600000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-03-16 122 TIGER OIL INC GeoDate 3/16/78
Oil and Gas 1978-03-16 Issued Date 3/16/78 Expired Date 3/16/79 Acres 0000000 Tool Type RTAF Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1978-04-15
Completed 1978-05-15
Reached Total Depth 1978-05-15
Change of Owner 1998-12-30 Operator changed from 122, TIGER OIL INC to 56, BUCKEYE OIL PRODUCING CO
Change of Owner 2001-02-27 Operator changed from 56, BUCKEYE OIL PRODUCING CO to 3569, LANG LARRY D
Change of Owner 2007-05-04 Operator changed from 3569, LANG LARRY D to 8200, LAKESIDE INC
APP 2014-09-19 Proposed Formations:MEDINA, Issued Date:9/19/2014, Expired Date:9/18/2016 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-06-11
Construction Permit Expires 2016-09-18
Record Last Modified 2017-02-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5405 5542 16
5405 5542 16
5405 5542 16

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1200 Bbl 27000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TIGER OIL INC 543.00 0.00 0
1985 TIGER OIL INC 1146.00 0.00 365
1986 TIGER OIL INC 1517.00 0.00 365
1987 TIGER OIL INC 1185.00 58.00 365
1989 TIGER OIL INC 730.00 0.00 365
1990 TIGER OIL INC 778.00 0.00 365
1991 TIGER OIL INC 451.00 0.00 365
1993 TIGER OIL INC 363.00 0.00 360
1994 TIGER OIL INC 75.00 0.00 365
1995 ENERGY CONTRACTORS INC 0.00 0.00 365
1996 ENERGY CONTRACTORS INC 126.00 0.00 365
1997 ENERGY CONTRACTORS INC 0.00 0.00 365
1998 BUCKEYE OIL PRODUCING CO 0.00 0.00 141
2001 BUCKEYE OIL PRODUCING CO 0.00 0.00 365
2004 LANG LARRY D 0.00 0.00 0
2005 LANG LARRY D 0.00 0.00 0
2009 LAKESIDE INC 0.00 0.00 0
2010 LAKESIDE INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TIGER OIL INC Brine 0 0
1985 TIGER OIL INC Brine 0 365
1986 TIGER OIL INC Brine 0 365
1987 TIGER OIL INC Brine 0 365
1989 TIGER OIL INC Brine 0 365
1990 TIGER OIL INC Brine 0 365
1991 TIGER OIL INC Brine 0 365
1993 TIGER OIL INC Brine 0 360
1994 TIGER OIL INC Brine 0 365
1995 ENERGY CONTRACTORS INC Brine 0 365
1996 ENERGY CONTRACTORS INC Brine 0 365
1997 ENERGY CONTRACTORS INC Brine 0 365
1998 ENERGY CONTRACTORS INC Brine 0 365
2001 BUCKEYE OIL PRODUCING CO Brine 0 365
2004 LANG LARRY D Brine 0 0
2005 LANG LARRY D Brine 0 0
2009 LAKESIDE INC Brine 0 0
2010 LAKESIDE INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1511509293 2014-8-28 0:00: PW No Violations 1.00
-1785437845 2015-6-10 0:00: PB No Violations 8.00
0084298007 2014-07-30 Field Inspected, Well Not Found No Violations Attempted to perform an inspection on this well in response to a request from PDC Energy. After searching for 1 hour using the RBDMS coordinates, I was unable to locate the well. The area has been timbered recently, making the area difficult to search in. I will contact Lakeside, Inc and request assistance in finding the well next week.
1264430634 2016-10-17 Final Restoration No Violations The purpose of my inspection is a status check on the final restoration of the plugged well site. During my inspection today no evidence of an oil and gas well has been left behind. Location has met 1509.072 B requirements.
1434399875 2015-06-11 Plug / Plug Back No Violations On location to witness plugging activities for this well. Altier Bros. service crew set the 4.5 casing at 2587. Formation Cementing set a 500, 2 stage rip isolation plug from 2587-2087 using 135 sks of 1% gel cement. Stage 1 was set from 2587-2287 using 81 sks 1% gel cement with 3% CaCl, 30 lbs LCM, and 37 bbls freshwater displacement. Stage 2 was set from 2287-2087 using 54 sks 1% gel cement with 2% CaCl, 30 lbs LCM, and 34 bbls freshwater displacement. The 4.5 casing was then pulled to 1699 and a 200 Berea/Bottom of Surface plug was set from 1699-1499 using 53 sks 2% gel cement, 2%CaCl, 30 lbs LCM, and 24 bbls freshwater displacement. Casing was then pulled to 200 and cement was circulated to surface. The remaining 4.5 casing was then pulled and the cement was topped-off to surface and did not drop below 30 below grade. Good circulation was achieved on all plugs. I was accompanied on this job by ODNR DOGRM Emergency Operations Manager Trisha Cartmell.
1511509293 2014-08-28 Production Wells No Violations Upon inspection, it was observed that this well is not capable of production. The well is currently shut in and flow lines are no longer attached. The well consists of 7 surface casing, 4.5 intermediate casing, and 2 production tubing with a rabbit catcher. The tank battery consists of a 100 bbl tank, a mechanical separator, and a drip. According to Mr. Chuck Ungurean of Lakeside, Inc, this well will be plugged this fall. Lakeside is currently in the process of filing for a plugging permit. GPS was not functioning properly, so no location data was gathered.
1785437845 2015-06-10 Plug / Plug Back No Violations On location to witness plugging activities for this well. Altier Bros. service rig is standing over the well. While pulling the 1.5 tubing from the well, the tubing parted at 3190. Jet Wireline Services attempted to run a tool past the top of the parted tubing but was unsuccessful. It was then decided to shoot 8 holes in the 4.5 casing at 3190 to set a plug in an attempt to isolate the Big Lime and squeeze cement into the annulus of the 4.5 casing. Formation Cementing pumped 30 sks of class A cement and displaced the entirety of the plug to 3190 in an attempt to squeeze as much cement as possible through the perforations. The plug was then locked in for a period of 1.5 hrs to ensure it did not travel back up the 4.5 casing. Jet Wireline Services then shot the 4.5 casing off at 2625 and 1 joint of casing was pulled out of the well. Plugging activities will resume on 6/11/2015.
84298007 2014-7-30 0:00: NF No Violations 1.50

For data sources see[9]

References