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34-167-23905

Well Details

Well ID: 34-167-23905
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Country: United States
State: Ohio
County: Washington
Municipality: Barlow Township
Operator Name: TRI-CITY DRILLING JOINT VENTUR
Well Pad ID:
Farm/Lease Name: CARVER NORVAL
License Status: Producing
License Date: 1982-12-28
Spud Date: 1977-09-25
Spud Drilling Contractor:
Final Drill Date: 1977-10-20
Well Total Depth: 1287.00 ft
Configuration: Vertical
Latitude: 39.380000
Longitude: -81.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1977-09-25
Completed 1977-10-20
Reached Total Depth 1977-10-20
CO 1982-12-28 1331 TRI-CITY DRILL JOINT VENT GeoDate 12/28/82
Record Last Modified 2013-10-03

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2018 TRI-CITY DRILLING JOINT VENTUR 278.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2018 TRI-CITY DRILLING JOINT VENTUR Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-49939242 2019-7-16 0:00: PW No Violations 1.20
-996162826 2018-9-26 0:00: PW No Violations 0.50
0858515313 2006-08-16 Production Wells No Violations Inspection this day found well producing with jack, tank has good IDs, needs more dike.
0905130921 2018-08-17 Production Wells Violations Noted On this day, I am conducting an inspection in reference to Complaint #5927. Landowner, Connie and Randall Reid expressed concerns of safety with an exposed 1 inch diameter plastic flowline along their drive. They requested that the flowline be buried. I found approximately 125 feet of exposed 1 inch plastic line along the drive. The well is equipped with 4.5 inch diameter casing and 2.375 inch diameter tubing with the production valves open. The well appears to show signs of recent activity. There are (2) 100 barrel steel tanks, but only 1 within an earthen dike. It will be noted that there is a vertical separator near the wellhead, within less than 20 feet, which does not meet the spacing requirements of 50 feet minimum spacing from the wellhead. The identification at the tank is faded and needs updated, and annual production has never been reported. Multiple pictures were taken. An attempt to contact Tri-City Drilling was made on 8/21/2018, and spoke with Greg Nuzum, to inform him of the issues and time frame for remediation. To bring the well within compliance, the following will need to be conducted. 1) Bury the gas line approximately 24 inches 2) Move the separator within 50 feet minimum of the wellhead 3) Properly identify the wellhead and/or tanks.
0996162826 2018-09-26 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection in regard to Complaint #5927. There has been no progress made to remediate the issues and get the well back within compliance. The section of pipeline that was requested to be buried is above ground, the identification is not updated, and the separator has not been adjusted to the minimum 50 setback from the wellhead. Updated pictures were taken. An attempt to contact Greg at Tri-City Drilling was made on 9/26/18, with no answer, and a voicemail left requesting a callback.
1543419519 2018-11-28 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection in regard to Complaint #5927. No progress has been conducted to regain compliance. On 11/28/2018, I spoke with Greg Nuzum of Tri-City Drilling, and he indicated that he has made contact with his contractor, but the contractor has been unavailable due to engagements with other activities. I reiterated that progress needs to be made, and he will need to attempt to commence work to address the issues.
1573844778 2019-11-15 0:00 PW No Violations 3.60
1919256692 2018-08-20 Production Wells No Violations On this day, I am conducting a follow-up inspection from 08/17/2018 to gather additional information regarding the footage spacing of the separator.
1962306577 2019-04-12 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection in regard to Complaint #5927. No progress has been made to gain compliance. On 4/12/19, I spoke with Greg Nuzum of Tri-City Drilling, and he stated that the weather and health issues had prohibited the work to be conducted throughout the winter months. I explained that progress needs to be made, and he is attempting to contact a contractor. Updated pictures were taken.
858515313 2006-8-16 0:00: PW No Violations
905130921 2018-8-17 0:00: PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0905130921 US-OH-130330 2018-08-30 9-10-05 Failure to properly bury pipeline
0905130921 US-OH-130331 2018-08-30 9-9-02 General Safety
0905130921 US-OH-130332 2018-08-30 9-9-05(A)10 Failure to legibly identify well
0905130921 US-OH-130333 2018-08-30 9-9-05(A)5 Violation of separator spacing requirements

For data sources see[7]

References