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Well ID: 34-167-24153 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Barlow Township | |
Operator Name: COLLINS-MCGREGOR OPERATING CO | |
Well Pad ID: | |
Farm/Lease Name: CARPENTER JOHN R | |
License Status: Producing | |
License Date: 1978-11-08 | |
Spud Date: 1978-05-23 | |
Spud Drilling Contractor: | |
Final Drill Date: 1978-06-30 | |
Well Total Depth: 2026.00 ft | |
Configuration: Vertical | |
Latitude: 39.400000 | |
Longitude: -81.640000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1978-05-23 | QUADRANGLE=( WATERFORD ) |
Completed | 1978-06-30 | QUADRANGLE=( WATERFORD ) |
Reached Total Depth | 1978-06-30 | QUADRANGLE=( WATERFORD ) |
CO | 1978-11-08 | 42 COLLINS-MCGREGOR OPER CO GeoDate 11/8/78 |
Record Last Modified | 2013-10-03 | QUADRANGLE=( WATERFORD ) |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1974 | 1980 | 14 |
1974 | 1980 | 14 | |
1974 | 1980 | 14 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 62000 Gal | 42000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-807864037 | 2016-4-21 0:00: | PW | No Violations | 1.50 |
-919858208 | 2008-3-5 0:00:0 | PW | No Violations | |
0807864037 | 2016-04-21 | Production Wells | Violations Noted | Performed an inspection of this well location with DOGRM Emergency Operations Coordinator Nathan Lane in response to a complaint of a brine release from the landowners property manager Marilyn McNabb. Upon inspection, it was observed that the well is in production and was in operation at the time of inspection. The well consists of a pumping unit standing over 4.5 production casing and 1.5 production tubing. The valves are in the open position on both strings. The tank battery consists of a 100 bbl production tank. The tank has leaked brine around a 1 valve at the bottom of the it. There is a brine scald area surrounding the tank and extending downhill of it encompassing an area 45 long by 20 wide. There is no containment dike around the tank. The tank is currently 27 away from the well, which violates DOGRM tank spacing requirements. Collins-McGregor Operating Co. will have 30 days upon the issue date of this notice to have the following completed: 1.) Pump down and move the 100 bbl production tank, excavate contaminated topsoil and dispose of it at an OEPA approved landfill; 2.) Replace contaminated soil with clean and apply lime/fertilizer and seed/mulch to the affected area to encourage regrowth of vegetation; 3.) Set a new production tank at least 50 from the well head and construct a containment dike around it to meet SPCC guidelines. |
0919858208 | 2008-03-05 | Production Wells | No Violations | Inspection this day found well producing with jack, tank has good IDs, no dike. |
1659789088 | 2016-05-16 | Production Wells | No Violations | Upon inspection, it was observed that remediation work has been performed on this location. Brine contaminated soil has been excavated, the location has been re-graded, limed/fertilized, and seeded/mulched. The production tank has been moved to meet DOGRM spacing requirements and has been set within an earthen containment dike which meets SPCC guidelines. This satisfies the requirements of the compliance notice dated 4/25/16. Photos taken. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0807864037 | US-OH-129184 | 2016-05-09 | Well operation causing pollution and contamination | |
0807864037 | US-OH-129185 | 2016-05-09 | Violation of tank spacing requirements | |
0807864037 | US-OH-129186 | 2016-05-09 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[9]