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34-167-24994

Well Details

Well ID: 34-167-24994
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Country: United States
State: Ohio
County: Washington
Municipality: Marietta Township
Operator Name: MELIUS DARYL
Well Pad ID:
Farm/Lease Name: MILLER ROBERT & HILL RICHARD
License Status: Domestic Well
License Date: 1979-09-19
Spud Date: 1979-11-02
Spud Drilling Contractor:
Final Drill Date: 1979-11-06
Well Total Depth: 2586.00 ft
Configuration: Vertical
Latitude: 39.400000
Longitude: -81.370000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-09-19 2070 HALWELL COMPANY GeoDate 9/19/79
Original Spud 1979-11-02 CHANGED STATUS FROM PR TO DM PER TRANSFER FROM STONEBRIDGE OPERATING CO. LLC #2070 TO OWNER ON 6/8/2017 CM.
Completed 1979-11-06 CHANGED STATUS FROM PR TO DM PER TRANSFER FROM STONEBRIDGE OPERATING CO. LLC #2070 TO OWNER ON 6/8/2017 CM.
Reached Total Depth 1979-11-06 CHANGED STATUS FROM PR TO DM PER TRANSFER FROM STONEBRIDGE OPERATING CO. LLC #2070 TO OWNER ON 6/8/2017 CM.
Change of Owner 2017-06-08 Operator changed from 2070, STONEBRIDGE OPERATING CO to 9713, BEARDSLEY RANDY M. - WELL #2-4944 INCORRECTLY TRANSFERRED ON 7/18/2016. CORRECTLY TRANSFERRED WELL 2-4994 ON 6/8/2017 CM.
Change of Owner 2017-08-24 Operator changed from 9713, BEARDSLEY RANDY M to 9970, MELIUS DARYL
Record Last Modified 2019-06-04 CHANGED STATUS FROM PR TO DM PER TRANSFER FROM STONEBRIDGE OPERATING CO. LLC #2070 TO OWNER ON 6/8/2017 CM.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2412 2436 25
2412 2436 25
2412 2436 25

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1200 Bbl 50000
N2 0 105 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 STONEBRIDGE OPERATING CO LLC 1.00 0.00 130
1994 STONEBRIDGE OPERATING CO LLC 0.00 0.00 355
1995 STONEBRIDGE OPERATING CO LLC 48.00 0.00 259
1996 STONEBRIDGE OPERATING CO LLC 20.00 0.00 91
1997 STONEBRIDGE OPERATING CO LLC 0.00 0.00 91
1998 STONEBRIDGE OPERATING CO LLC 490.00 0.00 343
1999 STONEBRIDGE OPERATING CO LLC 9.00 0.00 294
2000 STONEBRIDGE OPERATING CO LLC 156.00 0.00 366
2001 STONEBRIDGE OPERATING CO LLC 133.00 0.00 364
2002 STONEBRIDGE OPERATING CO LLC 45.00 1.00 138
2003 STONEBRIDGE OPERATING CO LLC 74.00 0.00 317
2004 STONEBRIDGE OPERATING CO LLC 54.00 0.00 364
2005 STONEBRIDGE OPERATING CO LLC 49.00 0.00 364
2006 STONEBRIDGE OPERATING CO LLC 44.00 0.00 273
2007 STONEBRIDGE OPERATING CO LLC 27.00 0.00 175
2008 STONEBRIDGE OPERATING CO LLC 29.00 0.00 365
2009 STONEBRIDGE OPERATING CO LLC 208.00 0.00 364
2010 STONEBRIDGE OPERATING CO LLC 228.00 0.00 365
2011 STONEBRIDGE OPERATING CO LLC 114.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 245.00 0.00 364
2013 STONEBRIDGE OPERATING CO LLC 160.00 0.00 161
2015 STONEBRIDGE OPERATING CO LLC 221.00 0.00 308
2016 STONEBRIDGE OPERATING CO LLC 170.00 0.00 21
2017 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 STONEBRIDGE OPERATING CO LLC Brine 0 130
1994 STONEBRIDGE OPERATING CO LLC Brine 0 355
1995 STONEBRIDGE OPERATING CO LLC Brine 0 259
1996 STONEBRIDGE OPERATING CO LLC Brine 0 91
1997 STONEBRIDGE OPERATING CO LLC Brine 0 91
1998 STONEBRIDGE OPERATING CO LLC Brine 0 343
1999 STONEBRIDGE OPERATING CO LLC Brine 0 294
2000 STONEBRIDGE OPERATING CO LLC Brine 0 366
2001 STONEBRIDGE OPERATING CO LLC Brine 0 364
2002 STONEBRIDGE OPERATING CO LLC Brine 0 138
2003 STONEBRIDGE OPERATING CO LLC Brine 0 317
2004 STONEBRIDGE OPERATING CO LLC Brine 0 364
2005 STONEBRIDGE OPERATING CO LLC Brine 0 364
2006 STONEBRIDGE OPERATING CO LLC Brine 0 273
2007 STONEBRIDGE OPERATING CO LLC Brine 60 175
2008 STONEBRIDGE OPERATING CO LLC Brine 0 365
2009 STONEBRIDGE OPERATING CO LLC Brine 0 364
2010 STONEBRIDGE OPERATING CO LLC Brine 0 365
2011 STONEBRIDGE OPERATING CO LLC Brine 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 364
2013 STONEBRIDGE OPERATING CO LLC Brine 0 161
2015 STONEBRIDGE OPERATING CO LLC Brine 0 308
2016 STONEBRIDGE OPERATING CO LLC Brine 0 21
2017 STONEBRIDGE OPERATING CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-253148478 2014-8-20 0:00: PW No Violations 1.00
-258283341 2014-7-3 0:00:0 PW No Violations 1.50
-914679293 2014-6-26 0:00: PW No Violations 5.00
0056773704 2014-07-02 Production Wells No Violations Upon inspection, it was observed that cleanup activities are still going on at this location. Roust crew was not present upon my arrival, however, it was evident that work had been done there this day. Oil absorbent pads are still in place in containment ditches and pit that was dug to flush free product into. Will continue to monitor this location until cleanup is complete.
0253148478 2014-08-20 Production Wells No Violations Performed final check on this location to ensure that vegetation was established over the remediated spill area. There is grass growing over the entirety of the remediated area. No oil has shown up at the surface, indicating that all of the contaminated soil was removed. New IDs are posted at the well and on the new plumbing setup. Well is in compliance.
0258283341 2014-07-03 Production Wells No Violations Stopped in to check on status of cleanup at the tank battery for this well. Stonebridge Operating Co. roust crew was on location and was tearing down the mechanical separators and drip tanks for removal. New domestic and sales lines will be run in the next few days so the well can be put back in line. All of the contaminated soil has been excavated and loaded into a dump truck to be hauled away to Athens/Hocking Sanitary Landfill in Nelsonville. Soil on the location will be monitored for another week or so to ensure no more oil surfaces. Reclamation will be done on entire site.
0914679293 2014-06-26 Production Wells Violations Noted Stonebridge Well Tender Mr. Randy Cisler reported a spill at this well at 10:04 p.m. on 6/25/2014. Between 4-5 bbl of oil was released from a 100 bbl production tank that was very corroded and developed a significant leak. Stonebridges roust crew was on location and had contained all but approximately 0.5 bbl of oil that escaped into the drainage ditch during last nights heavy rain event. Oil absorbent booms were in place in spots along the drainage ditch and a tributary creek to the Little Muskingum River. The oil covered an area approximately 10 wide by 60 long. There was no dike around the tank battery to hold back a spill. No oil is believed to have made it into waters of the state. I witnessed Stonebridges water truck pumping down the (2) 100 bbl tanks to empty. OEPA Environmental Specialist Mr. Trevor Irwin was on location when I arrived. I discussed a cleanup strategy with Mr. Jeremy Cassidy of Stonebridge Operating and he stated they will flush all of the free product into one area using a sump pump and hose, and then will use the water truck to pump off all of the free product on the surface. Mr. Cassidy will also bring in a skid-steer to scrape off all of the contaminated soil and it will be hauled off to an EPA approved landfill. Mr. Cassidy stated that they plan to have 90% of the cleanup effort completed today, and they will have it finished this weekend. The tank battery will be eliminated, as the wells using them are swab wells only and the tank battery is unnecessary. The wells that used these tanks will now be swabbed into portable poly tanks.
1404160736 2014-06-30 Production Wells No Violations Upon inspection, Stonebridge Operating Cos roust crew was on location and working on cleaning up the oil spill which occurred on 6/26/2014. Most of the free product had been flushed into a containment pit and pumped out by a water truck. Some free product is still surfacing around the affected area, and oil absorbent pads are being used to continually gather it. Both 100 bbl tanks have been removed from the location, and the mechanical separators and drip will be removed this week. A track hoe is on location and is being used to scrape off contaminated soil. Oil absorbent booms are still being used in the drainage ditch to catch any oil that may migrate off location. The clean up is expected to be finished by the end of this week.
1467721508 2016-07-05 Production Wells No Violations During my inspection today the well was equipped with 8.635 inch surface casing, 4.5 inch production, and opened valves. Located at 39.40834 -81.37186 is a master meter, a drip, a regulator, and lines labeled house gas. Valves within the meter run were in the closed position at the time of my inspection. Identification was posted at the meter run. No violations noted and there is not any open compliance notices with this given well.
1500380592 2017-07-18 Exempt Well Pre Transfer No Violations The inspection this day revealed that this well is equipped with a 4 1/2 inch diameter production casing and 2 inch diameter production lines. The valves on the wellhead are closed at the time of inspection. There is a master meter at 39.40834, -81.37186 as well as a drip and a separator. I called John Schneider from Stonebridge to make sure I was at the correct wellhead that day. I also asked him about the closed valves on the wellhead when I spoke to him. John sent me a picture he had of the well to compare to mine and they were indeed the same well. He told me that his pumper had closed the valves on the wellhead when the well was sold to the landowner but before that they were open. There are no issues at the time of inspection and the well is capable for house gas at the time of inspection.
2063869610 2014-07-09 Production Wells No Violations Upon inspection, it was observed that cleanup efforts at this location are complete. All old equipment that sat in the former tank battery has been removed, and new lines have been plumbed in with a domestic meter and new sales line. All contaminated soil has been excavated and hauled off to Athens-Hocking Reclamation Landfill. I have been provided with landfill load documentation by Mr. John Schneider of Stonebridge Operating. The location has been brought back to grade and seeded/mulched in an attempt to grow a new vegetative cover. This satisfies the requirements of the compliance notice.
56773704 2014-7-2 0:00:0 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0914679293 US-OH-130454 2014-10-28 Equipment pressure rated below operating pressure

For data sources see[9]

References