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Well ID: 34-167-25095 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Fairfield Township | |
Operator Name: GENESIS RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: DUNBAR DAVID D | |
License Status: Producing | |
License Date: 1979-10-24 | |
Spud Date: 1979-10-28 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-11-12 | |
Well Total Depth: 2630.00 ft | |
Configuration: Vertical | |
Latitude: 39.350000 | |
Longitude: -81.740000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1979-10-28 | |
Completed | 1979-11-12 | |
Reached Total Depth | 1979-11-12 | |
Change of Owner | 2018-03-23 | Operator changed from 2, BLAUSER ENERGY CORPORATION to 9086, GENESIS RESOURCES LLC |
Record Last Modified | 2018-03-23 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1778 | 1783 | 8 |
2006-09-11 | 2045 | 2056 | 1 |
1778 | 1783 | 8 | |
1778 | 1783 | 8 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1500 Bbl | 95000 | 1ST STAGE, 2ND STAGE 47M# SD. |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1581923702 | 2015-05-14 | Production Wells | No Violations | Upon inspection, it was observed that this well is capable of production but is currently shut in. The well consists of 7 surface casing, 4.5 intermediate casing with a 4-2 swedge and vall valve. The tank battery consists of a 100 bbl production tank, mechanical separator, and drip. The IDs are faded but are still present. The landowner, Mr. Bill Hoover, stated that this well has not produced in many years and he would like to see it plugged. I will contact Blauser Well Service and inquire about plans to service/produce or plug/abandon the well. |
For data sources see[9]