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Well ID: 34-167-25569 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Lawrence Township | |
Operator Name: STONEBRIDGE OPERATING CO LLC | |
Well Pad ID: | |
Farm/Lease Name: OTTMIRE DUFF | |
License Status: Final Restoration | |
License Date: 2012-06-20 | |
Spud Date: 1980-05-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-05-16 | |
Well Total Depth: 2254.00 ft | |
Configuration: Vertical | |
Latitude: 39.480000 | |
Longitude: -81.290000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-05-12 | 3033 HUBBARD OIL CO GeoDate 5/12/80 |
Original Spud | 1980-05-13 | |
Completed | 1980-05-16 | |
Reached Total Depth | 1980-05-16 | |
CO | 1995-01-18 | 2070 HALWELL COMPANY GeoDate 5/12/80 |
APP | 2012-06-20 | Proposed Formations:DEVONIAN-GORDON, Issued Date:6/20/2012, Expired Date:6/20/2014 12:00:00 PM, Drilling unit acres:65, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-11-06 | |
Record Last Modified | 2013-03-14 | |
Construction Permit Expires | 2014-06-20 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2092 | 2110 | 12 |
2092 | 2110 | 12 | |
2092 | 2110 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1065 Bbl | 48000 | |||
N2 | 0 | 120 Mscf | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1399125 | 2008-3-18 0:00: | PW | No Violations | |
-1442693216 | 2004-9-14 0:00: | PW | No Violations | |
-1703848095 | 2020-6-25 0:00: | FR | No Violations | 0.80 |
-1977459939 | 2010-12-3 0:00: | PW | No Violations | |
-1979991876 | 2009-10-13 0:00 | PW | No Violations | |
-239408284 | 2010-12-8 0:00: | PW | No Violations | 1.00 |
-530449215 | 2010-12-20 0:00 | PW | No Violations | 1.00 |
-690450143 | 2010-12-2 0:00: | PW | No Violations | 1.00 |
0001399125 | 2008-03-18 | Production Wells | No Violations | Inspection this day found no change. I had talked to John Schneider about getting this well in production, but he said this well a tough one - well is in slip and needs dug out with trac-hoe to either produce the well or plug it - cant get tubing in or out without doing this as casing is bent. This had been a landowner complaint since mid 2003 - I finally wrote it up in 5/06. No meter, tank is overgrown but has good IDs and dike, electric meter has been removed. In late 2005 or early 2006, they came in and put a flow-meter on it but it is not registering any gas - valve to sales line is cracked, but well is not producing, they admitted to me. Records show it made 37 mcf last year in 2006 - not sure how they are measuring that small amount. Well is not capable of producing at this time. |
0224153286 | 2008-10-27 | Production Wells | No Violations | No change in well status - only change is that brush around tank now cleared. Valves are open on well, no meter other than a small flow-meter, typical of many of Stonebridges wells. Landowner has complained about well since 2003 - finally wrote NOV in 2006 and now time for C. O.s. Stonebridge has admitted the well is not producing, needs worked on and is in a slip which will be expensive to fix, thus they have not done it. |
0239408284 | 2010-12-08 | Production Wells | No Violations
- asked them if they were going to connect and the crew said no gas there - even after swabbing and shutting in for the weekend. Cannot resolve NOV. | |
0530449215 | 2010-12-20 | Production Wells | No Violations | Inspection this day found casing well producing into sales line. Float gauge on well, reading gas, good IDs. Resolved. |
0538100549 | 2001-05-21 | Production Wells | No Violations | appears to be used for domestic I/D ok |
0690450143 | 2010-12-02 | Production Wells | No Violations | Inspection this day found crew on location with backhoe, having dug out large hole around/above the well that had been bent in slippage of ground. Crew said just digging well out and releaving the pressure had straighted the casing up but also found main bend in casing about 10 down. The crew was calling the office to get orders on how to pull back up so that well could again be swabbed. Well had pressure on it this day, when they opened valve for me, and told them they needed to do all that they could to increase production for the well. Landowners have complained about this well for over 7 years, wanting it plugged. Good IDs. Service rig should be on well tomorrow. |
0763102843 | 2012-11-16 | Administrative Inspection | No Violations | Well now plugged, reclamation complete. RESOLVED |
1088245495 | 2006-05-18 | Production Wells | Violations Noted | This well not producing, landowner wants something done. No change from last time well was inspected, but valves are open, going out into a line but not connected to tank, no separator. No one has been to tank in long time as completely overgrown with brush, IDs very faded, no meter -- putting a flowmeter on well was not enough to remedy. He agreed and would try and get on it. 10/27/2008 -- swabbing well - will have back in production soon. 12/20/10 - Well tied into sales line with meter, good IDs. |
1239041718 | 2009-04-06 | Production Wells | No Violations | Inspection this day found well still is not making anything - valves open but no chart, not commercial production. Good IDs on tank, needs more dike. Landowner had complained about this well - very old NOV (2006). Hillside has slipped and they need to come in with backhoe and straighten up casing before they can produce or plug. |
1329859811 | 2012-02-21 | Production Wells | Violations Noted | My inspection this day due to request from landowner to see if well is producing. I found a casing well with the valves shut, not capable of producing. The only meter on the well is a small flowmeter that has a tiny ball to register gas pressure and the ball is showing no indication of gas this day. The identification is posted on a sign and has all the required information. Annual production for 2010 reports 59 mcf. 100 bbl tank and separator have been removed in the last 6 months. The well needs put in Temporary Inactive status, plugged or put into production. |
1354652973 | 2012-12-04 | Final Restoration | No Violations | My inspection this day found location has been reclaimed, grass growing with these nice warm days. No debris left. |
1442693216 | 2004-09-14 | Production Wells | No Violations | Re-Inspection this day - well not in production, all valves shut, they report well has slipped - not the reason well is not producing, tank overgrown, good IDs, fair dike. Will call before giving NOV |
1763622231 | 2003-09-25 | Production Wells | No Violations | Inspection this day well hooked into line but does not appear to be producing - valve closed, tank area had not been visited recently, no IDs - will call operator. |
1977459939 | 2010-12-03 | Production Wells | No Violations | Inspection this day found company service rig on location, swabbing well - not much fluid in it - |
1979991876 | 2009-10-13 | Production Wells | No Violations | Inspection this day found no change, well still idle, has small flow meter/gauge on it but they have admitted not producing commercially, IDs faded, fair dike. Supervisor Stonerock will ask for Consent Agreement with this well included. |
2145154093 | 2007-10-26 | Production Wells | No Violations
- landowner wants it plugged. I am not going to resolve NOV this day, even tho well is capable. I have discussed this well with John Schneider and he knows they have to do something with it. | |
224153286 | 2008-10-27 0:00 | PW | No Violations | |
538100549 | 2001-5-21 0:00: | PW | No Violations | |
763102843 | 2012-11-16 0:00 | AM | No Violations | 0.20 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1088245495 | US-OH-102031 | 2006-05-18 | Well shall be plugged | |
1329859811 | US-OH-109437 | 2012-02-23 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]