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34-167-26672

Well Details

Well ID: 34-167-26672
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Country: United States
State: Ohio
County: Washington
Municipality: Decatur Township
Operator Name: BLAUSER ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: W A MCKIBBEN
License Status: Final Restoration
License Date: 2017-08-23
Spud Date: 1981-08-15
Spud Drilling Contractor:
Final Drill Date: 1981-08-18
Well Total Depth: 1960.00 ft
Configuration: Vertical
Latitude: 39.280000
Longitude: -81.810000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-06-23 2 BLAUSER WELL SERVICE INC GeoDate 6/23/81
Original Spud 1981-08-15
Completed 1981-08-18
Reached Total Depth 1981-08-18
APP 2017-08-23 Proposed Formations:BEREA, Issued Date:8/23/2017, Expired Date:8/23/2019 12:00:00 PM, Drilling unit acres:49.9, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-08-29
Record Last Modified 2018-05-19
Construction Permit Expires 2019-08-23

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1875 1885 8
1875 1885 8
1875 1885 8

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 600 Bbl 46000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BLAUSER ENERGY CORPORATION 4990.00 0.00 0
1985 BLAUSER ENERGY CORPORATION 3688.00 0.00 365
1986 BLAUSER ENERGY CORPORATION 5347.00 0.00 365
1987 BLAUSER ENERGY CORPORATION 4521.00 0.00 365
1988 BLAUSER ENERGY CORPORATION 4295.00 0.00 365
1989 BLAUSER ENERGY CORPORATION 3674.00 0.00 365
1990 BLAUSER ENERGY CORPORATION 3629.00 0.00 365
1991 BLAUSER ENERGY CORPORATION 3312.00 0.00 365
1992 BLAUSER ENERGY CORPORATION 4126.00 0.00 365
1993 BLAUSER ENERGY CORPORATION 3556.00 0.00 365
1994 BLAUSER ENERGY CORPORATION 3368.00 0.00 365
1995 BLAUSER ENERGY CORPORATION 3360.00 0.00 365
1996 BLAUSER ENERGY CORPORATION 3030.00 0.00 365
1997 BLAUSER ENERGY CORPORATION 3003.00 0.00 365
1998 BLAUSER ENERGY CORPORATION 2810.00 0.00 365
1999 BLAUSER ENERGY CORPORATION 2724.00 0.00 365
2000 BLAUSER ENERGY CORPORATION 2367.00 68.00 365
2001 BLAUSER ENERGY CORPORATION 1746.00 0.00 365
2002 BLAUSER ENERGY CORPORATION 2104.00 0.00 365
2003 BLAUSER ENERGY CORPORATION 665.00 0.00 365
2004 BLAUSER ENERGY CORPORATION 909.00 0.00 365
2005 BLAUSER ENERGY CORPORATION 717.00 0.00 365
2006 BLAUSER ENERGY CORPORATION 259.00 0.00 365
2007 BLAUSER ENERGY CORPORATION 253.00 0.00 365
2008 BLAUSER ENERGY CORPORATION 40.00 0.00 365
2009 BLAUSER ENERGY CORPORATION 0.00 0.00 365
2010 BLAUSER ENERGY CORPORATION 0.00 0.00 365
2011 BLAUSER ENERGY CORPORATION 258.00 23.00 365
2012 BLAUSER ENERGY CORPORATION 0.00 0.00 366
2013 BLAUSER ENERGY CORPORATION 0.00 0.00 365
2014 BLAUSER ENERGY CORPORATION 0.00 0.00 365
2015 BLAUSER ENERGY CORPORATION 0.00 0.00 365
2016 BLAUSER ENERGY CORPORATION 0.00 0.00 365
2017 BLAUSER ENERGY CORPORATION 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BLAUSER ENERGY CORPORATION Brine 0 0
1985 BLAUSER ENERGY CORPORATION Brine 0 365
1986 BLAUSER ENERGY CORPORATION Brine 0 365
1987 BLAUSER ENERGY CORPORATION Brine 0 365
1988 BLAUSER ENERGY CORPORATION Brine 0 365
1989 BLAUSER ENERGY CORPORATION Brine 0 365
1990 BLAUSER ENERGY CORPORATION Brine 0 365
1991 BLAUSER ENERGY CORPORATION Brine 0 365
1992 BLAUSER ENERGY CORPORATION Brine 0 365
1993 BLAUSER ENERGY CORPORATION Brine 0 365
1994 BLAUSER ENERGY CORPORATION Brine 0 365
1995 BLAUSER ENERGY CORPORATION Brine 0 365
1996 BLAUSER ENERGY CORPORATION Brine 0 365
1997 BLAUSER ENERGY CORPORATION Brine 0 365
1998 BLAUSER ENERGY CORPORATION Brine 0 365
1999 BLAUSER ENERGY CORPORATION Brine 0 365
2000 BLAUSER ENERGY CORPORATION Brine 365
2001 BLAUSER ENERGY CORPORATION Brine 0 365
2002 BLAUSER ENERGY CORPORATION Brine 0 365
2003 BLAUSER ENERGY CORPORATION Brine 0 365
2004 BLAUSER ENERGY CORPORATION Brine 365
2005 BLAUSER ENERGY CORPORATION Brine 0 365
2006 BLAUSER ENERGY CORPORATION Brine 0 365
2007 BLAUSER ENERGY CORPORATION Brine 0 365
2008 BLAUSER ENERGY CORPORATION Brine 0 365
2009 BLAUSER ENERGY CORPORATION Brine 0 365
2010 BLAUSER ENERGY CORPORATION Brine 0 365
2011 BLAUSER ENERGY CORPORATION Brine 0 365
2012 BLAUSER ENERGY CORPORATION Brine 0 366
2013 BLAUSER ENERGY CORPORATION Brine 0 365
2014 BLAUSER ENERGY CORPORATION Brine 0 365
2015 BLAUSER ENERGY CORPORATION Brine 0 365
2016 BLAUSER ENERGY CORPORATION Brine 0 365
2017 BLAUSER ENERGY CORPORATION Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1143226613 2017-5-30 0:00: PW No Violations 1.00
-1409808598 2006-1-26 0:00: PW No Violations
-1569409786 2018-2-22 0:00: PW No Violations
-79463581 2018-5-10 0:00: FR No Violations
-933581171 2017-8-4 0:00:0 PW No Violations 1.50
0079463581 2018-05-10 Final Restoration No Violations The inspection this day was a final restoration status check. The inspection this day revealed that vegetation has been established, the production equipment has been removed, and the wellhead has been cut off and been buried. Final restoration has been passed for this well.
0933581171 2017-08-04 Production Wells No Violations The inspection this day revealed that this well is equipped with a 4 1/2 to 2 inch diameter swage. The valve on the well is closed at the time of inspection. The tank battery for this well is equipped with a 100 barrel steel tank, a meter with an unmarked chart, and a vertical separator. The valve leading to the meter box is closed and there has been zero production reported on this well since 2011. Blauser Energy has a rig on the well at the time of inspection. No one was on site and I am unsure as to whos rig it is. The rig is set in place but it appears nothing has been pulled from the well at the time of inspection. There are no changes to this well and the well is idle at the time of inspection.
1143226613 2017-05-30 Production Wells Violations Noted The inspection this day revealed that this well is equipped with a 4 1/2 to 2 inch diameter swage. The valve on the well is closed at the time of inspection. The tank battery for this well is equipped with a 100 barrel steel tank, a meter with an unmarked chart, and a vertical separator. The valve leading to the meter box is closed and there has been zero production reported on this well since 2011. I called the company and spoke with Aaron Huck the Vice President and Treasurer of Blauser Energy. Aaron informed me that the company believes that this well may have a hole in the casing and they wanted to check to see if it can be repaired and put back in production or if it needed to be plugged. I then informed him I was going to issue a violation on this well for defective casing. Aaron then told me he would have Dean Decker of Decker Well Services, a third party contractor, look at this well as soon as he could get him out to the well. ORC 1509.12(A) states that upon discovery that the well casing is defective, the owner of the well shall notify the chief of the division within 24 hours, and the owner shall immediately repair the casing, correct the inadequacies, or plug and abandon the well.

Update 6/7/17 Spoke with Aaron Huck and informed him that the well needs to be plugged or repaired immediately. He told me he would do that as soon as he could get a service rig. Aaron mentioned possibly meeting him and Dean Decker at the office in Marietta one day to discuss this well. He also mentioned that he will speak with Dean and see what he advises him to do and may even apply for the permit to plug the well before getting a rig on the well that way if the well cannot be repaired they could just plug it right away. Aaron told me he would contact me as soon as he knew more details on the time frame for the well. They believe there is a hole in the casing due to pressure drop.

1409808598 2006-01-26 Production Wells No Violations Inspection this day found well producing thru casing, good IDs on tank, current chart in meter, needs a dike.
1569409786 2018-02-22 Production Wells No Violations This well was issued a compliance notice by Inspector Brian Sefcik for defective casing, leaking well on 5/30/17. This well was plugged on 8/29/17 and an affidavit was filed in RBDMS for the plugs. This well is now plugged and the compliance notice for this well has been resolved. This well is now plugged and abandoned.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1143226613 US-OH-103648 2017-08-25 NONE18 Defective casing, leaking well

For data sources see[9]

References