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Well ID: 34-167-27018 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Dunham Township | |
Operator Name: DECKER WELL SERVICE LLC | |
Well Pad ID: | |
Farm/Lease Name: HART KENNETH | |
License Status: Final Restoration | |
License Date: 2015-04-13 | |
Spud Date: 1981-12-30 | |
Spud Drilling Contractor: | |
Final Drill Date: 1982-01-15 | |
Well Total Depth: 2366.00 ft | |
Configuration: Vertical | |
Latitude: 39.340000 | |
Longitude: -81.670000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-12-10 | 2202 DECKER WELL SERVICE GeoDate 12/10/81 |
Original Spud | 1981-12-30 | |
Completed | 1982-01-15 | |
Reached Total Depth | 1982-01-15 | |
APP | 2015-04-13 | Proposed Formations:BEREA, Issued Date:4/13/2015, Expired Date:4/12/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-08-12 | |
Record Last Modified | 2017-02-10 | |
Construction Permit Expires | 2017-04-12 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2148 | 2154 | 4 |
2148 | 2154 | 4 | |
2148 | 2154 | 4 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 50000 Gal | 50000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0689246005 | 2015-08-12 | Plug / Plug Back | No Violations | On location to witness plugging operations for this well and to train newly hired Inspector Brian Sefcik. Knox Energy was the plugging contractor for the well. After running in tools to total depth, it was observed the well was dry down to 100 off bottom. The decision was made to bullhead the bottom plug through the 4.5 casing. Cemenco pumped a 400 bottom plug from 2150-1750 using 30 sks class A cement and 28.2 bbls of freshwater displacement. Knox Energy then ran in with ripping tools and was able to rip the 4.5 casing at 625. Cemenco tried to establish a pumping rate at that depth, but was unsuccessful due to red rock cave in on the annulus of the 4.5 casing. The casing was pulled to a depth of 500 and 300 plug was set from 500-200 using 75 sks 2% gel cement and 3.2 bbls of freshwater displacement. Casing was then pulled to 150 and a plug was circulated to surface using 40 sks 2% gel cement. The cement did not drop below 30 down. |
1439317694 | 2015-08-11 | Administrative Inspection | No Violations | Received call from Bill Mitten of Knox Energy stating they are moving a service rig onto this well to commence plugging operations. 1.5 tubing will be pulled from the well today. The bottom plug will be set tomorrrow. |
1465322000 | 2016-06-07 | Final Restoration | No Violations | The purpose of my inspection today is a status check on a final restoration. During my inspection I witnessed no evidence of an oil and gas well and the site has been restored. Location has met 1509.072 B requirements. |
689246005 | 2015-8-12 0:00: | PB | No Violations | 8.00 |
For data sources see[9]