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| Well ID: 34-167-27193 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Washington | |
| Municipality: Palmer Township | |
| Operator Name: CARPER WELL SERVICE INC. | |
| Well Pad ID: | |
| Farm/Lease Name: KELLER RAYMOND & RUDY | |
| License Status: Producing | |
| License Date: 1982-05-19 | |
| Spud Date: 1982-05-25 | |
| Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]] | |
| Final Drill Date: 1982-06-07 | |
| Well Total Depth: 5703.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.450000 | |
| Longitude: -81.680000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1982-05-19 | Issued Date 5/25/82 Expired Date 11/15/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05703 Proposed Drill Depth 05703 |
| Original Spud | 1982-06-02 | |
| Completed | 1982-06-07 | |
| Reached Total Depth | 1982-06-07 | |
| CO | 1982-06-29 | 182 BELDEN & BLAKE CO GeoDate 5/19/82 |
| Completion Report Received | 1982-07-28 | |
| Construction Permit Expires | 1982-11-15 | |
| Change of Owner | 2002-08-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
| Change of Owner | 2003-01-21 | Operator changed from 1966, PETROX INC to 3621, MILL JAMES & KATHY |
| Change of Owner | 2017-04-13 | Operator changed from 3621, INDIAN HILLS RESOURCES LLC to 7007, CARPER WELL SERVICE |
| Record Last Modified | 2017-04-13 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2006-09-11 | 5498 | 5504 | 6 |
| 5430 | 5510 | 0 | |
| 2006-09-11 | 5474 | 5478 | 6 |
| 5474 | 5478 | 6 | |
| 5430 | 5510 | 0 | |
| 1997-06-29 | 5430 | 5510 | 0 |
| 2006-09-11 | 5566 | 5578 | 12 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| N2 | 0 | 18000 Mscf | 70000 | CLINTON | ||
| N2 | 0 | 140 Mscf | 50000 | FRAC: 58MG H2O, 50M SAND, 140M N2, HCL | ||
| ACID | 15 | 750 Gal | 0 | CLINTON | ||
| ACID | 15 | 500 Gal | 0 | CL. | ||
| H2O | 0 | 69950 Gal | 0 |
For data sources see[4]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1110954776 | 2004-10-13 0:00 | PW | No Violations | |
| -1826385538 | 2019-10-30 0:00 | PW | No Violations | 0.90 |
| -723096722 | 2018-8-8 0:00:0 | PW | No Violations | 1.00 |
| 0000PL1957 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0723096722 | 2018-08-08 | Production Wells | Violations Noted | I was on location today to do a field inspection on this well. When I arrived on location I heard a gas leak coming from the wellhead. I located the leak on the back side of the well coming below the stuffing box. The 2 inch diameter tubing appears to be leaking. I contacted the company to let them know about the situation and they will be sending someone out. They will contact me back once they have something lined up. I spoke with Mason Carper about it. |
| 1110954776 | 2004-10-13 | Production Wells | No Violations | Inspection this day found well producing, current chart in meter, 2 100 bbl tanks, 2 smaller water, good IDs, fair dike, sloping downhill so wont do much good with a spill. |
| 1256862179 | 2020-3-10 0:00: | PW | No Violations | 0.30 |
| 1542309157 | 2018-11-15 | Production Wells | No Violations | On this day, I am conducting a compliance notice follow-up inspection. The gas leak is still present at the wellhead, and no work appears to have been conducted to remediate the issue. I spoke with Ryan Carper on 11/15/2018, and he indicated that he hasnt been to the well to check on the leak, but will be out on Monday 11/19/2018 to assess the issue. He will be calling back with a plan to fix the leak. |
| 1576851604 | 2019-12-20 0:00 | PW | No Violations | 2.00 |
| 1671972094 | 2019-04-12 | Production Wells | No Violations | On this day, I am conducting a compliance notice follow-up inspection. No progress has been made to gain compliance. The gas leak is still present at the wellhead. On 4/12/19 I contacted Carpers Well Service and spoke with Tiffany, requesting that Mr. Carper return my call to discuss the intentions of resolving the issue. I spoke with Ryan Carper on 4/12/19, and he stated that they attempted to fix the issue, but were unsuccessful. He will be working on the well the week of 4/15/19, and update me with the progress. |
| 1783072508 | 2015-04-24 | Production Wells | No Violations | Upon inspection, it was observed that this well is currently in production. The well consists of a pumping unit standing over 8.625 surface casing, 4.5 intermediate casing, and 2 production tubing. The well is producing sales on the 4.5 casing and is closed on the 2 tubing. The tank battery consinsts of a 100 bbl production tank, mechanical separator, drip, meter run, and containment dike. Legible and correct ID information is posted on the tank. No violations were observed. |
| PL1957 | PL | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0723096722 | US-OH-128220 | 2018-08-29 | 9-10-04 | Inadequate pipeline strength |
For data sources see[9]