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Well ID: 34-167-27715 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Watertown Township | |
Operator Name: SUNNY SHORES OF OHIO INC | |
Well Pad ID: | |
Farm/Lease Name: MCDOUGLE S | |
License Status: Producing | |
License Date: 1987-02-02 | |
Spud Date: 1984-05-18 | |
Spud Drilling Contractor: MID ATLANTC DRLG | |
Final Drill Date: 1987-04-23 | |
Well Total Depth: 5662.00 ft | |
Configuration: Vertical | |
Latitude: 39.460000 | |
Longitude: -81.670000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-04-02 | 143 DERBY OIL & GAS CORP GeoDate 4/2/84 |
Oil and Gas | 1984-04-02 | Issued Date 4/2/84 Expired Date 9/29/84 Acres 0080000 Tool Type RTA Proposed Formation BLACK RIVER Proposed Depth 05662 Proposed Drill Depth 05662 |
Original Spud | 1984-05-18 | |
Completion Report Received | 1984-07-02 | |
CO | 1987-02-02 | 3045 SUNNY SHORES OF OHIO INC GeoDate 2/2/87 |
Oil and Gas | 1987-02-02 | Issued Date 2/2/87 Expired Date 2/2/88 Acres 0080000 Tool Type RTA Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Plugged Back | 1987-02-07 | |
Completed | 1987-04-23 | |
Reached Total Depth | 1987-04-23 | |
Construction Permit Expires | 1988-02-02 | |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 0 | 0 | |
0 | 0 | ||
2006-09-11 | 5570 | 5579 | 18 |
5570 | 5579 | 18 | |
0 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
FOAM | 0 | 762 Bbl | 45000 | FRAC;H2O,SAND,N2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DERBY OIL & GAS CORP | 2457.00 | 0.00 | 0 |
1985 | DERBY OIL & GAS CORP | 2294.00 | 0.00 | 319 |
1986 | DERBY OIL & GAS CORP | 1320.00 | 0.00 | 341 |
1987 | CHRISTA OIL CO | 713.00 | 0.00 | 116 |
1993 | SUNNY SHORES OF OHIO INC | 680.00 | 0.00 | 365 |
1995 | SUNNY SHORES OF OHIO INC | 487.00 | 0.00 | 305 |
1996 | SUNNY SHORES OF OHIO INC | 1171.00 | 0.00 | 365 |
1997 | SUNNY SHORES OF OHIO INC | 586.00 | 0.00 | 365 |
1998 | SUNNY SHORES OF OHIO INC | 512.00 | 0.00 | 365 |
1999 | SUNNY SHORES OF OHIO INC | 600.00 | 0.00 | 365 |
2000 | SUNNY SHORES OF OHIO INC | 492.00 | 0.00 | 365 |
2001 | SUNNY SHORES OF OHIO INC | 681.00 | 0.00 | 365 |
2002 | SUNNY SHORES OF OHIO INC | 703.00 | 0.00 | 365 |
2003 | ANDERSON BOBBY B | 826.00 | 0.00 | 365 |
2004 | SUNNY SHORES OF OHIO INC | 965.00 | 0.00 | 365 |
2005 | SUNNY SHORES OF OHIO INC | 675.00 | 0.00 | 365 |
2006 | SUNNY SHORES OF OHIO INC | 465.00 | 0.00 | 365 |
2007 | SUNNY SHORES OF OHIO INC | 678.00 | 0.00 | 365 |
2008 | SUNNY SHORES OF OHIO INC | 529.00 | 0.00 | 310 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DERBY OIL & GAS CORP | Brine | 0 | 0 |
1985 | DERBY OIL & GAS CORP | Brine | 91 | 319 |
1986 | DERBY OIL & GAS CORP | Brine | 1 | 341 |
1987 | CHRISTA OIL CO | Brine | 0 | 116 |
1993 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
1995 | SUNNY SHORES OF OHIO INC | Brine | 0 | 305 |
1996 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
1997 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
1998 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
1999 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2000 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2001 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2002 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2003 | ANDERSON BOBBY B | Brine | 0 | 365 |
2004 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2005 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2006 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2007 | SUNNY SHORES OF OHIO INC | Brine | 0 | 365 |
2008 | SUNNY SHORES OF OHIO INC | Brine | 0 | 310 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1080438753 | 2020-4-21 0:00: | PW | No Violations | 0.20 |
-1663107879 | 2014-3-4 0:00:0 | PW | No Violations | 1.00 |
-714286620 | 2018-1-10 0:00: | PW | No Violations | |
-725135632 | 2019-12-20 0:00 | PW | No Violations | 0.30 |
-906566859 | 2010-3-3 0:00:0 | PW | No Violations | |
0199508599 | 2010-07-20 | Administrative Inspection | No Violations | Talked to Mrs. McDougle - says Attorney Yoss has filed court documents showing landowners have now acquired wells legally. She says she is selling wells to another operator and will she have to be bonded? Called Columbus and Erica says she can fill out the Form 7 and sign as owner, including court paperwork - will have to pay $100/well, but will not have to be bonded and insured just to pass them to someone else. Called Mrs. McDougle and passed along information. |
0714286620 | 2018-01-10 | Production Wells | No Violations | The inspection this day revealed that this well is equipped with an 8 5/8 inch diameter surface casing and a 4 1/2 inch diameter production casing. The valves on the wellhead are closed. There has been no effort to get this well into production and the well is idle. |
0763526583 | 2015-12-02 | Production Wells | No Violations | Upon inspection, it was observed that this well is currently in production of domestic gas only. The pumping unit and rods have been pulled from the well. No changes have been made to the well location since the last inspection on 3/4/2014. I spoke to landowner Mr. Terry Sampson and he stated that he acquired ownership of the wells on his land along with his mineral rights as the outcome of a lawsuit against Sunny Shores of Ohio Inc. I explained the process of becoming an exempt domestic well owner to Mr. Sampson and provided him with a phone number for the ODNR DOGRM Central Office to call and get more information. Mr. Sampson made it clear that he did not want to own the wells, but will do what he needs to do to stay legal. Mr. Sampson also expressed intent to sell the wells to a local producer. |
0906566859 | 2010-03-03 | Production Wells | No Violations | FOLLOW UP TO NOV # 1267706681 Inspection this day with Sup. Stonerock, fou nd well in production, producing thru casing, ID sign at well but no information. Tank over across the fence with 3 ID stickers on it but unable to read information. Landowner getting gas but none being sold. Jack sitting in corn field - has been pulled off well but never removed. Post IDs. |
1267706681 | 2010-03-03 | Production Wells | Violations Noted | Inspection this day with Sup. Stonerock, fou nd well in production, producing thru casing, ID sign at well but no information. Tank over across the fence with 3 ID stickers on it but unable to read information. Landowner getting gas but none being sold. Jack sitting in corn field - has been pulled off well but never removed. Post IDs. |
1663107879 | 2014-03-04 | Production Wells | No Violations | Well is equipped to produce out of 2 in. tubing inside the 4.5 in casing. Valves were closed on the 2 in. The annulus side was hooked up and provides house gas to the landowners house (Mr. Terry Sampson). No identification was posted on the well. I spoke with the landowner Mr. Terry Sampson and he believes that he owns this well as per courthouse records. I will research the courthouse records. |
1675068790 | 2016-08-09 | Production Wells | No Violations | The purpose of my inspection is a follow up on a compliance notice. The compliance notice stated failure to legibly identify well. During my inspection the well was equipped with 8.625 surface casing, 4.5 inch production casing, and 2.375 inch tubing. The 2.375 inch tubing valve was shut. The 4.5 inch production casing valve was opened with a domestic gas line attached and a gauge reading 99 pounds per square inch. Inspection was completed on foot due to the fact the well is located in the middle of a corn field with no lease road. No action has been taken to gain compliance. Pictures were taken to assist with this inspection. |
199508599 | 2010-7-20 0:00: | AM | No Violations | 1.00 |
734952347 | 2019-11-13 0:00 | PW | No Violations | 0.50 |
763526583 | 2015-12-2 0:00: | PW | No Violations | 2.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1267706681 | US-OH-107184 | 2010-03-04 | Failure to legibly identify well |
For data sources see[9]