X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-167-27749

Well Details

Well ID: 34-167-27749
Loading map...
Country: United States
State: Ohio
County: Washington
Municipality: Waterford Township
Operator Name: BANCEQUITY PETROLEUM CORPORATI
Well Pad ID:
Farm/Lease Name: HUCK DENNIS
License Status: Final Restoration
License Date: 2014-10-28
Spud Date: 1984-10-08
Spud Drilling Contractor: MID ATLANTC DRLG
Final Drill Date: 1984-10-12
Well Total Depth: 5384.00 ft
Configuration: Vertical
Latitude: 39.580000
Longitude: -81.660000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-05-09 Issued Date 5/9/84 Expired Date 11/5/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05384 Proposed Drill Depth 05384
Original Spud 1984-10-08
Completed 1984-10-12
Reached Total Depth 1984-10-12
Change of Owner 1984-10-15 500 SHANAHAN DONALD P GeoDate 5/9/84
CO 1984-10-15 500 SHANAHAN DONALD P GeoDate 5/9/84
Completion Report Received 1986-02-13
CO 1991-12-13 28 CGAS EXPLORATION,INC GeoDate 5/9/84
Change of Owner 1999-04-24 Operator changed from 28, CGAS EXPLORATION to 4801, BANCEQUITY PETROLEUM CORP
APP 2014-10-28 Proposed Formations:CLINTON, Issued Date:10/28/2014, Expired Date:10/27/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2014-12-15
Construction Permit Expires 2016-10-27
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5260 5270 1
5260 5270 1
5260 5270 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 4700 Gal 80000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 SHANAHAN DONALD P 12260.00 124.00 365
1985 SHANAHAN DONALD P 10092.00 31.00 365
1986 SHANAHAN DONALD P 31382.00 75.00 365
1987 SHANAHAN DONALD P 1198.00 0.00 365
1988 SHANAHAN DONALD P 1410.00 0.00 365
1989 SHANAHAN DONALD P 1163.00 0.00 365
1990 SHANAHAN DONALD P 1300.00 17.00 365
1991 CGAS EXPLORATION 144.00 0.00 365
1992 CGAS EXPLORATION 956.00 0.00 366
1993 CGAS EXPLORATION 804.00 0.00 366
1994 CGAS EXPLORATION 861.00 0.00 365
1995 CGAS EXPLORATION 874.00 0.00 365
1996 CGAS EXPLORATION 914.00 0.00 365
1997 CGAS EXPLORATION 687.00 0.00 365
1998 CGAS EXPLORATION 465.00 0.00 365
2011 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 0
2012 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 0
2013 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 0
2014 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 SHANAHAN DONALD P Brine 0 365
1985 SHANAHAN DONALD P Brine 0 365
1986 SHANAHAN DONALD P Brine 0 365
1987 SHANAHAN DONALD P Brine 0 365
1988 SHANAHAN DONALD P Brine 0 365
1989 SHANAHAN DONALD P Brine 0 365
1990 SHANAHAN DONALD P Brine 0 365
1991 CGAS EXPLORATION Brine 0 365
1992 CGAS EXPLORATION Brine 61 366
1993 CGAS EXPLORATION Brine 0 366
1994 CGAS EXPLORATION Brine 0 365
1995 CGAS EXPLORATION Brine 0 365
1996 CGAS EXPLORATION Brine 0 365
1997 CGAS EXPLORATION Brine 0 365
1998 CGAS EXPLORATION Brine 53 365
2011 BANCEQUITY PETROLEUM CORPORATI Brine 0
2012 BANCEQUITY PETROLEUM CORPORATI Brine 0 0
2013 BANCEQUITY PETROLEUM CORPORATI Brine 0 0
2014 BANCEQUITY PETROLEUM CORPORATI Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1635860324 2010-7-21 0:00: PW No Violations 1.00
-1745746201 2010-7-21 0:00: PW No Violations 1.00
-231911071 2010-7-21 0:00: PW No Violations 1.00
-675704110 2014-11-5 0:00: PW No Violations 2.00
0000PL1719 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0231911071 2010-07-21 Production Wells No Violations FOLLOW UP TO NOV # -1635860324 Plug or produce. Post IDs.
0402652558 2015-09-24 Final Restoration No Violations Upon inspection, it was observed that the pit has been filled, location has been graded, a full vegetative cover has been established, all production equipment has been removed, and the lease road has been restored. Final restoration passed 9/24/2015.
0675704110 2014-11-05 Production Wells No Violations Upon inspection, it was observed that this well is shut in and is idle. No attempt has been made by the operator to gain compliance. I will contact Bancequity Petroleum Corp. and inform them that prompt action must be taken to bring this well into compliance in lieu of legal enforcement action.
1113496118 2008-11-21 Production Wells No Violations Inspection this day found well with rabbit, not producing, no chart in meter, no IDs, but service rig sitting down below on the road, so anticipate wells going soon. Will check back next week.
1238818963 2014-12-15 Production Wells No Violations This well was plugged on 12/15/2014. The original compliance notice can be written off.
1635860324 2010-07-21 Production Wells Violations Noted Plug or produce. Post IDs.
1740548981 2014-06-17 Production Wells No Violations Upon inspection, it was observed that this well is still shut in and is idle. A faint natural gas odor was present around the valve on the 1.5 production tubing. Vegetation has grown up around the well head, indicating it has not been serviced in a long time. There was a bunk of severely corroded 1.5 tubing laying beside the well head from the last time the well was serviced. There is a meter run and a 100 bbl production tank for this well. No ID is present on the well head or at the production tank.
1745746201 2010-07-21 Production Wells No Violations Inspection this day found well not producing, tubing laying off to side, could have H2S, hole in casing. Records show well has been idle since 1998. Computer maps way off in this area, very confusing.
1858508545 2015-02-26 Plug / Plug Back No Violations On location to witness plugging operations for this well. Upon arrival, the 4.5 casing had been ripped at 2865 and pulled OOH. 2.375 tubing was set in the hole at 2822. Cemenco pumped a 300 plug with 90 sks class A cement with 2% calcium chloride, 40 lbs LCM, and 9.7 bbls of freshwater displacement. The cement was then left to set up for 1.5 hrs and a 200 bottom of surface plug was set from 1731-1531 with 60 sks class A cement, 20 lbs LCM, and 5.9 bbls of freshwater displacement. Tubing was then pulled to 200 and good circulation was established. A 200 surface plug was then circulated to surface using 65 sks class A cement and 20 lbs LCM. After pulling the remaining tubing, it was observed that the surface plug had dropped to 200. A brush and stone bridge plug was then sent downhole to the fluid level and the well was topped off open-ended with 50 sks of 2% gel cement.
402652558 2015-9-24 0:00: FR No Violations 0.50
PL1719 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1635860324 US-OH-116082 2010-07-22 Well shall be plugged

For data sources see[9]

References