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| Well ID: 34-167-28006 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Washington | |
| Municipality: Adams Township | |
| Operator Name: ALLIANCE PETROLEUM CORPORATION | |
| Well Pad ID: | |
| Farm/Lease Name: VERNON AUGENSTEIN | |
| License Status: Final Restoration | |
| License Date: 2013-01-31 | |
| Spud Date: 1985-02-23 | |
| Spud Drilling Contractor: CT DRILLING | |
| Final Drill Date: 1985-03-03 | |
| Well Total Depth: 6139.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.520000 | |
| Longitude: -81.560000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Oil and Gas | 1985-01-23 | Issued Date 1/23/85 Expired Date 7/22/85 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 06139 Proposed Drill Depth 06139 |
| Original Spud | 1985-02-23 | |
| Completed | 1985-03-03 | |
| Reached Total Depth | 1985-03-03 | |
| CO | 1985-03-14 | 1383 OHIO L & M CO INC GeoDate 1/23/85 |
| Completion Report Received | 1985-03-22 | |
| Change of Owner | 2007-07-24 | Operator changed from 1383, OHIO L & M CO INC to 6288, ALLIANCE PETROLEUM CORPORATION |
| APP | 2010-07-06 | Proposed Formations:OHIO SHALE (MAY NOT PRODUCE BEREA), Issued Date:7/6/2010, Expired Date:7/6/2011 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class:POOL |
| APP | 2013-01-31 | Proposed Formations:DEVONIAN/GORDON/THIRTY FOOT, Issued Date:1/31/2013, Expired Date:1/31/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
| Plugged/Abandoned | 2013-05-16 | |
| Construction Permit Expires | 2015-01-31 | |
| Record Last Modified | 2015-09-24 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 5876 | 5966 | 0 |
| 5876 | 5966 | 0 | |
| 2006-09-11 | 5895 | 5911 | 19 |
| 5895 | 5911 | 19 | |
| 5876 | 5966 | 0 | |
| 2006-09-11 | 6008 | 6018 | 35 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 95000 Gal | 60000 | FRAC;H2O,SAND | ||
| H2O | 0 | 82180 Gal | 29000 | CLINTON |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1985 | L & M PETROLEUM CO | 52526.00 | 267.00 | 0 |
| 1986 | L & M PETROLEUM CO | 52268.00 | 152.00 | 365 |
| 1987 | L & M PETROLEUM CO | 25250.00 | 62.00 | 365 |
| 1988 | OHIO L & M CO INC | 13910.00 | 0.00 | 365 |
| 1989 | OHIO L & M CO INC | 12410.00 | 0.00 | 365 |
| 1990 | OHIO L & M CO INC | 8311.00 | 0.00 | 365 |
| 1991 | OHIO L & M CO INC | 6703.00 | 0.00 | 365 |
| 1993 | OHIO L & M CO INC | 4984.00 | 0.00 | 365 |
| 1994 | OHIO L & M CO INC | 3756.00 | 0.00 | 365 |
| 1995 | OHIO L & M CO INC | 3701.00 | 0.00 | 365 |
| 1996 | OHIO L & M CO INC | 3550.00 | 0.00 | 365 |
| 1997 | OHIO L & M CO INC | 3627.00 | 0.00 | 365 |
| 1998 | OHIO L & M CO INC | 2783.00 | 0.00 | 365 |
| 1999 | OHIO L & M CO INC | 2244.00 | 0.00 | 365 |
| 2000 | OHIO L & M CO INC | 1881.00 | 0.00 | 365 |
| 2001 | OHIO L & M CO INC | 952.00 | 0.00 | 365 |
| 2002 | OHIO L & M CO INC | 2105.00 | 0.00 | 365 |
| 2003 | OHIO L & M CO INC | 2161.00 | 0.00 | 365 |
| 2004 | OHIO L & M CO INC | 2121.00 | 0.00 | 365 |
| 2005 | OHIO L & M CO INC | 1809.00 | 0.00 | 365 |
| 2006 | ALLIANCE PETROLEUM CORPORATION | 1446.00 | 0.00 | 365 |
| 2007 | ALLIANCE PETROLEUM CORPORATION | 39.00 | 0.00 | 365 |
| 2008 | ALLIANCE PETROLEUM CORPORATION | 0.00 | 0.00 | 365 |
| 2009 | ALLIANCE PETROLEUM CORPORATION | 0.00 | 0.00 | 365 |
| 2010 | ALLIANCE PETROLEUM CORPORATION | 0.00 | 0.00 | 365 |
| 2011 | ALLIANCE PETROLEUM CORPORATION | 0.00 | 0.00 | 365 |
| 2012 | ALLIANCE PETROLEUM CORPORATION | 0.00 | 0.00 | 366 |
| 2013 | ALLIANCE PETROLEUM CORPORATION | 0.00 | 34.00 | 243 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1335241474 | 2002-3-26 0:00: | AD | No Violations | |
| -2073037790 | 2013-5-7 0:00:0 | PB | No Violations | 9.00 |
| -510129602 | 2013-5-13 0:00: | PB | No Violations | 5.00 |
| -804765920 | 2013-5-9 0:00:0 | PB | No Violations | 8.50 |
| 0000PL1603 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
| 0510129602 | 2013-05-13 | Plug / Plug Back | No Violations | My inspection today finds the well operator is performing a bond log on the 8.625 casing to find the cement top on the back side of the pipe. They will attempt to cut the casing as deep as possible. |
| 0804765920 | 2013-05-09 | Plug / Plug Back | No Violations | Witnessed the 4.5 in. production casing being shot off. A rip plug was set after that. Casing was shot at 3671 ft. Plug was pumped immediately after that because the casing was free. |
| 1335241474 | 2002-03-26 | Annular Disposal | No Violations | ad not used |
| 1368533460 | 2013-05-06 | Plug / Plug Back | No Violations | Witnessed plugging activities in progress. After talking with Mr. Marty Miller, he stated that there was a hole in the production casing. We decided to shoot perforations in the Big Lime section. I witnessed the perforations being set. |
| 1411063522 | 2014-09-18 | Final Restoration | No Violations | Upon inspection, it was observed that the former location of this well is now a planted agricultural field. No production equipment was observed on the location, and the lease road has been retained for farm vehicle use. This fulfills the requirements of the final restoration. |
| 1499973449 | 2013-05-15 | Plug / Plug Back | No Violations | Witnessed plugging activities on this day. Top of cement was tagged at 1707 ft. Spoke with company man Marty Miller on site. |
| 1564195406 | 2013-05-14 | Plug / Plug Back | No Violations | Witnessed plugging activities in progress. Tubing was ran to 2025 ft. and the Berea plug was pumped. Good circulation was established during the pumping of this plug. |
| 2073037790 | 2013-05-07 | Plug / Plug Back | No Violations | Witnessed the setting of the bottom hole plug, and the Big Lime plug. Hole was loaded with heavy brine to keep H2S gas down hole. |
| PL1603 | PL | No Violations |
For data sources see[9]