X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-167-28516

Well Details

Well ID: 34-167-28516
Loading map...
Country: United States
State: Ohio
County: Washington
Municipality: Wesley Township
Operator Name: BROAD STREET SERV LLC
Well Pad ID:
Farm/Lease Name: PINKERTON
License Status: Final Restoration
License Date: 2010-11-01
Spud Date: 1987-12-21
Spud Drilling Contractor: SWANK-ULLMAN
Final Drill Date: 1988-01-12
Well Total Depth: 5253.00 ft
Configuration: Vertical
Latitude: 39.430000
Longitude: -81.810000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1987-08-19 Issued Date 8/19/87 Expired Date 8/18/88 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05253 Proposed Drill Depth 05253
Original Spud 1987-12-01
Completed 1988-01-12
Reached Total Depth 1988-01-12
CO 1988-03-09 3437 CEMCO OPERATING INC GeoDate 8/19/87
Completion Report Received 1988-03-16
CO 1995-01-30 4350 CENTURY WELL SERVICE GeoDate 8/19/87
Last Compliance Report 2005-07-13
Change of Owner 2007-10-03 Operator changed from 4350, CENTURY WELL SERVICE to 7033, BROAD STREET ENERGY COMPANY
Change of Owner 2008-02-19 Operator changed from 7033, BROAD STREET ENERGY COMPANY to 8312, BROAD STREET SERV LLC
APP 2008-08-20 Proposed Formations:CLINTON/MEDINA, Issued Date:8/20/2008, Expired Date:8/20/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2009-09-01 Proposed Formations:CLINTON, Issued Date:9/1/2009, Expired Date:9/1/2010 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
APP 2010-11-01 Proposed Formations:CLINTON/MEDINA, Issued Date:11/1/2010, Expired Date:10/31/2012 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2010-11-01
Construction Permit Expires 2012-10-31
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5052 5092 0
5052 5092 0
2006-09-11 5088 5168 8
5088 5168 8
5052 5092 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 45000 Gal 65000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 CEMCO OPERATING INC 50515.00 0.00 340
1990 CEMCO OPERATING INC 38061.00 0.00 340
1991 CEMCO OPERATING INC 31571.00 0.00 350
1992 CEMCO OPERATING INC 18386.00 0.00 365
1993 CEMCO OPERATING INC 19629.00 0.00 365
1994 CENTURY WELL SERVICE 7109.00 0.00 365
1995 CENTURY WELL SERVICE 5501.00 0.00 365
1996 CENTURY WELL SERVICE 13003.00 0.00 365
1997 CENTURY WELL SERVICE 9031.00 0.00 365
1998 CENTURY WELL SERVICE 6.00 0.00 365
1999 CENTURY WELL SERVICE 0.00 0.00 365
2000 CENTURY WELL SERVICE 0.00 0.00 365
2001 CENTURY WELL SERVICE 0.00 0.00 365
2002 CENTURY WELL SERVICE 0.00 0.00 365
2003 CENTURY WELL SERVICE 0.00 0.00 365
2004 CENTURY WELL SERVICE 0.00 0.00 365
2005 CENTURY WELL SERVICE 0.00 0.00 365
2006 CENTURY WELL SERVICE 0.00 0.00 365
2007 BROAD STREET SERV LLC 0.00 0.00 365
2008 BROAD STREET SERV LLC 0.00 0.00 0
2009 BROAD STREET SERV LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 CEMCO OPERATING INC Brine 720 340
1990 CEMCO OPERATING INC Brine 630 340
1991 CEMCO OPERATING INC Brine 690 350
1992 CEMCO OPERATING INC Brine 375 365
1993 CEMCO OPERATING INC Brine 0 365
1994 CENTURY WELL SERVICE Brine 0 365
1995 CENTURY WELL SERVICE Brine 25 365
1996 CENTURY WELL SERVICE Brine 148 365
1997 CENTURY WELL SERVICE Brine 0 365
1998 CENTURY WELL SERVICE Brine 165 365
1999 CENTURY WELL SERVICE Brine 0 365
2000 CENTURY WELL SERVICE Brine 0 365
2001 CENTURY WELL SERVICE Brine 0 365
2002 CENTURY WELL SERVICE Brine 0 365
2003 CENTURY WELL SERVICE Brine 0 365
2004 CENTURY WELL SERVICE Brine 0 365
2005 CENTURY WELL SERVICE Brine 0 365
2006 CENTURY WELL SERVICE Brine 0 365
2007 BROAD STREET SERV LLC Brine 0 365
2008 BROAD STREET SERV LLC Brine 0 0
2009 BROAD STREET SERV LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1005376677 2009-9-22 0:00: PW No Violations
-1006507970 2010-8-11 0:00: PW No Violations 1.00
-1297692172 2011-3-24 0:00: FR No Violations 1.00
-1435994534 2010-10-26 0:00 PW No Violations 1.00
0000PL1371 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0020258842 2010-10-12 Administrative Inspection No Violations Talked to landowner - he says rig on well all day 10/11/2010 trying to swab down. Lowered only 50 and were getting H2S gas. Needs plugged, should not be allowed for TA.
0273479221 2010-10-29 Plug / Plug Back No Violations Inspection this day tested water from stock tank near the well and found no brine or oil. Was cautious, as yesterday set bottom plug and hole circulated out the 8 casing - definitely hole in 4.5 casing. Circulated 10-15 bbl oil, looked like from Berea and was concerned it might show up in the spring, traveling thru the sandstone. Ripped at 2665 - will bring 4.5 casing out, then back in to rip depth with 2 -back in to 2662.
0454123543 2005-05-17 Production Wells No Violations Reinspected this day and found no change. Well still not producing or tied into line. Consists of 2 oil tanks, lay-down separator and meter run with meter.
1005376677 2009-09-22 Production Wells Violations Noted Re-issue NOV for idle well due to landowner complaint - originally issued 9/17/2004 to Century - Re-issue new NOV to Broad Street. Plug or produce. Post IDs. Failure to comply may result in bond forfeiture. NOV originally sent 9/17/2004. RESOLVED - well plugged
1006507970 2010-08-11 Production Wells No Violations Inpsection this day with landowner, Sunny Hearn, who had complained that wanted well plugged. Broadstreet working to get a valid lease and do something with well, Ed Butler had talked to Sunny on 7/15 and said would be back in less than a month. The day found well with swedge, shut-in, 100 bbl tank and smaller steel water tank back at well, separator and meter run with old chart in it. Well is in non-compliance of 1509.12. Pictures. Annual production shows this well last produced in 1998.
1095357333 2004-09-16 Production Wells Violations Noted Inspection this day found well not tied into line, capped and valve shut, line going to tank ate in two and laying on ground, tank is 100 bbl plus water tank, good IDs, fair to poor dike. Landowner says these wells havent produced and has no yearly rental payment - wants them plugged or sold to him. Not capable of producing Plug or produce. Payment of yearly rental payment does not exempt operator from having to produce or plug. NOV re-issued on 5/14/2009 11/8 - RESOLVED - well is plugged, still needs reclamation done.
1274870929 2010-10-18 Production Wells No Violations Met with landowner, Sonny Hearn, regarding contamination in the spring he waters dairy cows in. Took samples at the cattle trough, site where the spring comes out of the ground (which is 225 from well - trough is 220 further out from spring), and also sampled other, uncontaminated spring (it is 580 from well). From taste, I would agree has brine in it. Used Quantab at cattle trough and it checked 1600 ppm. Checked water at main spring and it appears to still be clean. Took pictures, water samples and measurements. Sonny had collected water on Saturday from the spring and we used Quantab to check it - it showed 1900 ppm. He said from taste, it might be a little cleaner today. He speculates that they brought gas into casing when swabbing and possibly has hole in production casing and surface casing and gas forced the brine out into the surface water. Said coal outcrops down over the hill. Left samples at lab today, called Leslie and told them to plug well as soon as possible - she said they were trying to find a service rig and plugging application should have been received in Columbus. This well has had a violation for 7 years - still not resolved.
1287444688 2010-10-16 Production Wells No Violations Call received on 10/16/10 AM from landowner Sonny Hearn regarding brine in his spring that he waters his dairy cows out of. Said he had tasted water and tastes salty - told him I would contact operator and get someone to come out and see if they could figure out what was going on. Called Ed Butler and left message, then Leslie Gearhart and she sent pumper out - suggested if well was shut-in and had pressure on it, that might be forcing brine into surface water. She said they had swabbed it on 10/7 and had no sign of gas, could not swab well down. Suggested they take water sample. Also advised landowner to take sample, that I would be out on Monday. Sonny has spent many years working in oilfield and believe his to be knowledgeable about brine. Said spring is 150 from well they swabbed and cattle trough where brine showing up is another 100 below spring. Concerned about his other spring which he says appears to not be contaminated, as they use it for the dairy operation and the house.
1288882014 2010-11-04 Plug / Plug Back No Violations Inspection found cement about 30 down, have not cut off casing yet. Some equipment removed. Checked water with Quantab and was clear - no chlorides.
1297692172 2011-03-24 Final Restoration No Violations Inspection this day found ground had been smoothed, grass growing, all debris removed. Still small tank and master meter inside dike area but location looks good. Talked with farmer and he is also satisfied.
1325521203 2010-08-06 Administrative Inspection No Violations Talked to Leslie - she says rig still has not been on well. Informed her permit to plug expires 9/1/10. Talked to landowner and he says they have recently been out to talk with him, says they do not have a lease but he will let them work on wells or plug. He says no rig has been there.
1398255557 2010-09-23 Production Wells No Violations No change, well not producing, service rig has not been there.
1435994534 2010-10-26 Production Wells No Violations Inspection this day with supervisor, showed him water stock tank which spring feeds into where brine was discovered, also showed him spring and well with equipment. Quantabs in spring showed water tests 500 ppm chlorides, lower than last test. Frac tank at well where they were swabbing into on 10/7/10 has leaked on ground, showing a kill area of 10 x 5 and tests above the scale on the high Quantab. Supervisor speculates water from frac tank has contaminated spring - I believe since spring is testing lower in chlorides every day, that swabbing of well somehow contaminated the spring and it is gradually cleaning itself up after quit swabbing on well. Service rig should be on well this week to plug. Good IDs at well. 10/28 - Reexamine area around frac tank - tank still has brine in it but is below the leak point or is going down in the ground instead of out. Did not locate old pit from drilling but did find very soft sandstone just under the grounds surface - could be leaching thru the sandstone doing into the spring.
20258842 2010-10-12 0:00 AM No Violations 0.20
273479221 2010-10-29 0:00 PB No Violations 4.00
454123543 2005-5-17 0:00: PW No Violations
PL1371 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1005376677 US-OH-100197 2009-09-22 Failure to legibly identify well
1005376677 US-OH-100198 2009-09-22 Well shall be plugged
1095357333 US-OH-102256 2004-09-16 Well shall be plugged

For data sources see[9]

References